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7/30/2019 Internal Kaizen for OEE Improvement-Team8
1/24
1GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Design. Build. Ship. Serv
ice.
OEE Improvement
Document Title : OEE Improvement (Operations)
Document No : GBE-KPO-4-001-00
Doc. Revision : 06
Document Date : Oct27, 2008
Bus iness Excel lence
Project Title :OEE ImprovementSite : Shenzhen
Line/Area :All project
Team No :Team
Date :Oct27 ,08
Category :Operation
Type : Internal Kaizen
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2GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
[email protected] of Contents
PDCA (Plan Do Check Adjust) 3
Independent Study on Kaizen Needs 4
Kaizen Team Members 5
Goals & Objectives 6
Target Sheet 7
Process & Information Flow 8
Value Stream Map 9
Standard Work Sheet (Before) 10
Standard Work Combination Sheet 11
Takt / Cycle time Graph (Before) 12
Spaghetti Chart (Before) 13
5 Why Analysis 14
7 Ways 15
Contents Slide(s) Contents Slide(s)
Idea Evaluation Sheet 16
Golf Score Tools 17
Golf Score tools (Before & After) 18
Before & After Kaizen 19
Spaghetti Chart (After) 20
Standard Work Sheet (After) 21
Takt / Cycle Time Graph (After) 22
Kaizen News Paper 23
Kaizen Log (Homework Moving Forward) 24
Lesson & Tools Learned 25
Kaizen Log (Proposal for Yokoten) 26
Attendance List 27
Financial Performance Dashboard 28
VSM Icon & Symbols 29
VSM Dotting Process & Keynotes 30
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3GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
1. Adjust
4. Check
2. Plan
Lean in Operations - PDCA
0-70% 71%-90% 91%-100% Above 100%
Machiner
y
Environme
nt
Inaccurate OEE
Data
Method
Incomplete
Data
OEE 60%
Man
Short manpower to
solve the issues
Lack of Skilled to
handle issue on
m/c
Materials
Offline setup setup not
readyMaterial missing or short
in kit
Material coming
issue
Package
changed without
informed in
advance
wrong material
Material not deliveryon time
program NOT
Optimized
Line NOT
Balanced
Reduced Speed
due to Machine
conditions
Blocked or Starved
within the line
feeder problemLack of
Employee
Awareness to
the OEE
Problem
Non-level Loading
Measurem
ent
First Article takes
too longChange-Over takes
long time
Wrong Target
CPH/UPH
parts fall out
Lack of trainin
g
Too many WIP
waiting for Top
and B/EZero spare part
inventory for
level 1
Shenzhen Site OEE Improvement
OEE Trend Chart
10%20%30%40%50%60%70%80%90%100%
Monthly
OEEand
LU
OEE Tgt
OEE
LU Tgt
LUOEE Tgt 5 5% 5 5% 5 5% 5 5% 5 5% 5 5% 5 5% 5 5% 5 5% 5 5% 6 0% 6 0% 6 0%
OEE 47.2%50.1%50.6%50.5%46.2%50.8%53.0% 52% 56.0054.8%
LU Tgt 35.0%35.0%35.0%35.0%35.0%35.0%35.0% 40.0%40.0%40.0%40.0%40.0%40.0%
LU 32% 32% 26% 32.4%25.2%35.2%37.7% 39% 36.1038.7%
Dec'
07
Jan'
08
Feb'
08Mar Apr May June July
Augu
stSep Oct Nov Dec
GraspThe
Situation
Date: 10/27/2008
Team Title : OEE improvement
CTQs
Unit Of
Measur
ement
StartTarget
Date:
Week 1
Date:
Week 2Day 1 Day 2 Day 3 Day 4 Day 5 % Improved Status
OEE(FCM II) % 57% 65.0% 57% 57%OEE(NXT) % 61% 70.0% 61% 61%OEE(Pace ) % 50% 55.0% 50% 50%OEE(NEC) % 44% 55.0% 44% 44%OEE(HMLV) % 38% 50.0% 38% 38%downtime Min 508% 3% 5.08% 5.08%
Customer/Model :ALL
ine/Area/ Module :ALL line
Downtime breakdownQ1'09 Q2'09
Apr May Jun Jul Aug SepDescription AverageNo schedule downtime 29.48%
43.4% 27.4% 22.8% 24.8% 35.6% 22.9%
Planned downtime 4.75% 2.7% 3.5% 4.5% 4.0% 5.4% 8.4%Equipment downtime 5.08% 5.0% 4.9% 5.9% 5.3% 3.9% 5.5%Materila downtime 0.43% 1.0% 0.9% 0.1% 02% 0.4% 0.2%Production/process D/T 0.20% 0.3% 0.1% 0.2% 02% 0.3% 0.3%On-line setup, C/O D/T 2.10% 1.2% 1.3% 1.4% 2.9% 2.7% 3.1%Qulity related 0.37% 0.5% 0.4% 0.5% 0.4% 0.2% 0.2%Actual production time 57.42% 46.0% 61.0% 64.5% 62.1% 51.5% 59.4%
3. Do
Identify the Gap
All issues highlighted here
should be captured under A3.
Target Sheet Progress
Show a breakdown of the subject matter
and identify area that is being focused.
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4GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
[email protected] Study on Kaizen Needs
Present Situation and Problems :
1. 8 FCM lines contributed to more downtime
2.Panasonic machine low ECPH
3. variety pickup/placer in site
4. lack of offline repair station to repair PIP
5. feeder mainteance
Needed Output :
1.Reduce FCM machine/line downtime
2.Improve ECPH for Panasonic machine
Potential Risk and Metrics to be Monitored :
(based on kaizen needs) :Required Kaizen needs :
The cascade changeover implementation on pace
offline setupwater stride involve in Changeover
FCM offline repair station setup
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5GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Note : Pls ensure that all G&O identified in this page is captured under the target sheet.
Goals & Objectives
Objectives
1. Improve OEE from current 55% to 60%
2. Reduce Machine related downtime 5.08% to 3%
3. Improve MV2F ECPH
Goals
CTQs
Unit Of
Measur
ement
StartTarget % Improved Status
OEE(FCM II) % 57% 65.0% 89.0%
OEE (NXT) % 61% 70.0% 102.1%
OEE(Pace-MV2F) % 50% 55.0% 120.3%
OEE (NEC-CP6) % 44% 55.0% 73.4%
OEE (Pace-CM602) % 85.0% 106.2%
0-70% 71%-90% 91%-100% Above 100%
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6GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
[email protected] Team Members
No of Shingijutsu
Workshop attended1 SJ Ma Leader ME 5
2 Guo Qing Li Co-leader ME 3
3 James Peng Co-leader ME 4
4 Road Lu Co-leader ME 1
5 Fu Guangyuan Engieer ME 1
6 Zhou zhongqiang Co-leader ME 4
7 Tx lee Co-leader ME 6
8 Liu Liming Engieer ME 5
9 HuangJinghua Engieer ME 2
10 Clifford Zheng Engieer ME 3
11 Sun Susan Engieer ME 2
12
13
No of Shingijutsu
Workshop attended
1
2
3
Team Members Name Job Title Department
No
NoExternal Team Members Name Job Title Department
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7/247GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Target Sheet
Notes :
Use this Target Sheet if project is not tracking ETE
Please ensure all the G&Os identified in Page 5 is captured.
Site lean leader is responsible in reviewing this and ensuring that a follow thru is done till the closure.
0-70% 71%-90% 91%-100% Above 100%
Date: 10/27/2008~10/31/2008
Team Title : OEE improvementSep WW43 WW44 WW44
CTQs
Unit Of
Measur
ement
StartTarget
Date:
Week 1
Date:
Week 2Day 1 Day 2 Day 3 Day 4 Day 5 % Improved Status
OEE(FCM II) % 57% 65.0% 57.8% 58.0% 57.8%OEE (NXT) % 61% 70.0% 71.2% 68.0% 75.2%
OEE(Pace-MV2F) % 50% 55.0% 57.2% 58.3% 83.0%OEE (NEC-CP6) % 44% 55.0% 46.4% 31.0% 43.7%OEE (Pace-CM602) % 85.0% 52% 86.8% 90.0% 94.0%downtime Min 5.08% 3% 6.4% 3.5% 4.0%
Customer/Model :ALL
ine/Area/ Module :ALL line
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Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Before Kaizen After Kaizen
Title: Shenzhen Site OEE Improvement
Sub-Tit le : SMT Line B alance
Metrics(UOM) Before After % Improved
HardSavings(USD/month)
SoftSavings(USD/month)
Lean
81.25%
Method forSustaining
ResultsAction Taken
Sankyo
perations
SMTProduction
Customer:
Problem
92.50%
Do right thing atfirst time.
Programmershould deliverwell balanced
program to SMT
Study machineprocess time one by
one and try toimprove line LBRand increase line
productivity
Sankyodemand
increased, andone line cannotmeet customer
requirement
Tools Used
13%
UPH 120 140 17%
LBR
Cycle Time
24
20 18 16
0
10
20
30
S/P MV1 MV2 IC Placer
Station
Second
C/T
Cycle Time
20 2018
16
0
5
10
15
20
25
S/P MV1 MV2 IC Placer
Station
Second
C/T
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Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Before Kaizen After Kaizen
Title : Shenzhen Site OEE Improvement
Sub -Tit le : SMT Lin e Balance
Metrics(UOM) Before After % Improved
HardSavings(USD/month)
SoftSavings(USD/month)
Lean
Six Sigma
Do right thing atfirst time.
Programmershould deliverwell balanced
program to SMT
Study machineprocess time one by
one and try toimprove line LBRand increase line
productivity
Sankyodemand
increased, andone line cannotmeet customer
requirementTools Used
15%
UPH 44 60 36%
LBR
Method forSustaining
ResultsAction Taken
Pace
perations:
SMTProduction
Customer:
Problem
98.00%
ECPH 33.68% 50.08% 48%
84.80%
Cycle time
57 5975
00
50
100
S/P MV2 MV2 MPAV2
stations
second
C/T
Cycle time
48 49 50
0
20
40
60
80
S/P MV2 MV2 MPAV2
stations
secon
d
C/T
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Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Before Kaizen After Kaizen
Title : Shenzhen Site OEE Improvement
Sub -Tit le : SMT Lin e Balance
Metrics(UOM) Before After % Improved
HardSavings(USD/month)
SoftSavings(USD/month)
Lean
Six Sigma
Do right thing atfirst time.
Programmershould deliverwell balanced
program to SMT
Study machineprocess time one by
one and try toimprove line LBRand increase line
productivity
Sankyodemand
increased, andone line cannotmeet customer
requirementTools Used
15%
UPH 44 60 36%
LBR
Method forSustaining
ResultsAction Taken
Pace
perations:
MT productio
Customer:
Problem
98.00%
ECPH 33.68% 50.08% 48%
84.80%
Cycle time
10085
110
00
50
100
150
S/P MV2 MV2 MPAV2
stations
secon
d
C/T
Cycle time
9085
90
0
50
100
150
S/P MV2 MV2 MPAV2
stations
second
C/T
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11GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Before Kaizen After Kaizen
Metrics
(UOM)Before After % Improved
Hard
Savings
(USD/
month)
Soft
Savings
(USD/
month)
LeanSix Sigma
Do right thing in first
time. Programmer
should deliver well
balanced program to
SMT
16
10%
Method for
SustainingResults
96% 2%
39.44% 50%
44
98%
Action Taken
pace
perations:
SMT
operation
Customer:
Problem
Use MPS to
optimize the
program
Tools Used
60
Low ECPH
and LBR
LBR
UPH
ECPH
SMT21-1 machine cycle time
57 5975
0
20
40
60
80
MV2F(1) MV2F(2) MPAV2B
SMT21-1 machine cycle time
48 49 50
10
30
50
70
MV2F(1) MV2F(2) MPAV2B
Time(s)
Title : Shenzhen Site OEE Improvement
Sub -Tit le : SMT Lin e Balance
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12GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Before Kaizen
After Kaizen
Metrics(UOM)
Before After % Improved
Hard
Savings
(USD/
month)
Soft
Savings
(USD/
month)
LeanSix Sigma
Method for
Sustaining
60 16UPH
Do right thing in first
time. Programmer
should deliver well
balanced program to
SMT
44
ECPH 33.67% 50.08%
Action Taken
PACE
perations
SMT
Operation:li
ne22-1
Customer:
Problem
Low ECPH
and LBR
Use MPS to
optimize the
program
Tools Used
16%
LBR
Results
90.39% 96.07% 5%
SMT22-1 PVR3 cycle time
5769 75
0
20
40
60
80
MV2F(1) MV2F(2) MPAV2B
SMT22-1 PVR3 cycle time
48 48 51
10
20
3040
50
60
Time(s) 48 48 51
MV2F(1) MV2F(2) MPAV2B
After Kaizen
Title : Shenzhen Site OEE Improvement
Sub -Tit le : SMT Lin e Balance
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13GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Metrics Before After % Improved $ Hard $ Soft
LeanSix Sigma
Tools Used
Method forSustaining
ResultsAction Taken
Thomson
perations
SMT
Operation:14-1
Customer:
Original
supporting pincan not satisfywith demandofquality,whichtakeproductionprint issue
98%
Use supporting
block to replacesupporting pin tosupport PCB better
Problem
standard
procedue todefine supporting
block using insolder paste
station
solderpaste
printing
quality 99.96% 2%
Before Kaizen After Kaizen
Title : Shenzhen Site OEE Improvement
Sub-Tit le : Suppo rt ing B lock
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
7/30/2019 Internal Kaizen for OEE Improvement-Team8
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14GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Metrics Before After % Improved $ Hard $ Soft
LeanSix Sigma
standardprocedue to
define careeptable using insolder paste
station when pilotrun
qualitymake a careeptable to attachplasitic on board toprotect PCB fromcleaning
Tools Used
Method forSustaining
ResultsAction Taken
All
perations
SMTOperation
Customer:solder pastemisprintingcausepotencialquality issue
Before Kaizen After Kaizen
Title : Shenzhen Site OEE Improvement
Sub -Tit le : Special Stick up Too ls
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Tape is
difficult to
cover PCB
Design special
stickup tools to
finish film cover
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15GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Before Kaizen After Kaizen
Metrics Before After % Improved $ Hard $ Soft
Lean
Six Sigma
Tools Used
Method for
SustainingResultsAction Takenperations
SMTOperation
Customer:
Problem
PACE&THM
Two persons to
remove PIP fromM/C for repai r
Waste manpower
Make use of trolly to
help remove PIP of FCMTraining alltechnicians tooperate PIPrepair trolly
Manpower
Title : Shenzhen Site OEE ImprovementSub -Title: PIP Repair Tro lly
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Just need
one
technician
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16GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Metrics Before After % Improved $ Hard $ Soft
Lean
Six Sigma
D/T
Add a filter to make
machine get dry air
Problem
Maintenancefilter periodically
Tools Used
Method forSustaining
ResultsAction Taken
PACE&THM
perations
SMT
Operation
Customer:
Water&oil
was found incompressair,whichbrought a lotof down timeup
Before Kaizen After Kaizen
Title : Shenzhen Site OEE Improvement
Sub -Tit le : FCM Water Filter
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Setup a filter
to make
compress air
dry
Titl Sh h Sit OEE I t
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17GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Metrics Before After % Improved $ Hard $ Soft
LeanSix Sigma
Fuji all NXT lineYokoten the line.
Tools Used
Method forSustaining
ResultsAction Taken
ALU
perations
Changeover
Customer:
Some
support pinsneed move insmt machinewhen eachchangeover.
Only use one soft
support pin ,itneedn't move wheneach changeover.
Problem
Yield
D/T
Before Kaizen After Kaizen
Only one soft
supporting pin and it
neednt move when
changeover
Some supporting pins
need re-setup when
changeover
Title : Shenzhen Site OEE Improvement
Sub-Tit le : Soft Suppo rt ing Pin
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
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18GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Action Item Who Due Date Time % Completed RemarksPlanned ClosedLine22-1 SMT balance Liu Liming Oct28 Oct27 Oct28 UPH increased 16 pcs
Line10-1 SMT program optimization Hu Yushan Oct28 Oct27 Oct28 UPH increase 6 pcs
Pallet Change Unit of NXT modification Lee TX/Fu Oct31 Oct27 Oct31 NXT changeover
Soft supporting pin introduction Lee Tx/Fu Oct31 Oct27 Oct31 NXT changeover
Line6-1 SMT cycle time balance Lu Road Oct29 Oct28 Oct29
UPH increase 10 pcs
Line22-1 SMT machine c/t balance Liu Liming Oct29 Oct28 Oct29 UPH increased 16 pcs
Kaizen News Paper
No Money
No
No Space
25% Complete 75% Complete
50% Complete 100% Complete
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19GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Note :
Please include follow up action items that needs to be continued after the workshop.
The follow thru targets will need to be included in the long term target sheet in the next slide.
Site lean leader is responsible in following thru the actions identified in the kaizen log.
Kaizen Log Homework Moving Forward
Action Item Who Due Date Time % Completed RemarksContinue to work with facility department to improve compress
air,which will help to assure our machine work in good condition James Peng 2008/11/15
Programmer optimizes program to satisfy with machine configure. Fanghui Li 2008/12/1
25% Complete 75% Complete
50% Complete 100% Complete
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20GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Lessons & Tools Learned
NoApplication in our jobs
(Please be specific)
1 Help to find out root cause of down-time
2 Program optimization will improve LBR
3 BrainStorm
4
5
Lessons & Tools Learned
Make use of 5why to solve issue
Program optimization is the base of
production.
Team work is the way to success
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21GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Note:
Please include follow up action items that needs to be continued after the workshop.
Site lean leader is responsible in following thru the actions identified in the kaizen log.
Site lean leader will select the items identified here for yokoten and will be transferred to the
yokoten tracking.
Kaizen Log Proposal for Yokoten
Items proposed for Yokoten Who Due Date Time % Complete RemarksGet dry air by setup valve to keep water away from SMT machine James Peng 2008/11/15
Setup soft supporting pin to replace original support pin to reduce
changeover time Lee TX 2008/11/15
25% Complete 75% Complete
50% Complete 100% Complete
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22GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
[email protected] Why Analysis
Enforcement
Limit
Why FCM
vacuum alarm.
Machine filter have not water.
Need buy spare part and do monthly maintain.
Because tube
compression air
have water.
Because of some
valve running
defect,Why have
the defect.
Because valve is
unstable,Why
valve is unstable.
Counter
Measure
Cause Because tube compression air have water.
Because valve
conpression air
uncleanly,Why
compression air
uncleanly.
Line 23-1
Responsible
DivisionHuang Jh
5 WHY1 WHY 2 WHY 3 WHY 4 WHY
5 WHY CONCEPT
Defect THOMSON FCM VACUUM ALARM
Condition Machine PIP running that vacuum alarm
Date
Occurred1 Step.
Area
Find The Cause (5 WHY)
Line name 17 18 20 21 23 24total
time rate
10 20 10 0 30 100 170 35.4%
30 0 0 0 20 10 60 12.5%
0 0 0 0 0 10 10 2.1%
0 0 0 0 20 0 20 4.2%
30 20 0 20 110 20 200 41.7%
5 10 0 0 5 0 20 4.2%
THOMSON FCM DOWNTIME ANALYSE
per line down time analysis chart
35.4%
12.5%2.1%
4.2%
41.7%
4.2%
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23GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
: Process
Flow(Black)
: Supplier : Fork lift
: Store
: Picking cart
: Truck
: Material
Flow(Blue)
: Inventory: Receipts : PC
: Process : ElevatorEV
: Information
Flow(Black)
WT : Waiting Time
PT: Processing Time
T: Touches
Value Add
Value Enabler
Non-Value Add
SMT Value Stream Map
Program
Administrator ForecastProduction
Control
Loading Plan
weekly
daily
HUB
ProductionFlow
Loader&
Conveyor
S/P
SPI
C/P
IC/P
R/O AOI
Conveyor
Conveyor
Conveyor
Conveyor
Conveyor
H/L W/S Touch Up Assembly
ICT FT Packing
Suppliers
Firm Weekly
Daily
Shipment
Plan
2*UPH
WIP
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24GBE-KPO-4-001-00 Kaizen Template (Operations) Rev. 06
Source :Internal Kaizen
Shenzhen Fu Yong
Oct. 2008
Thank you Design. Build. Ship. Service.