ENG.REPORT 10.04.2013

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    Date:10.04.2013

    GENERAL INFORMATION AT LAST HOUR A B C

    COOLING TOWER LEVEL 300M3 (mtr) 1.7* 1.7 1.7

    WATER ADDED IN COOLING TOWER(300)KL 12 10 13

    COOLING TOWER LEVEL 150M3 (%) _ Full Full

    NITROGEN PRESSURE (KG/CM2) 3.5 4 3

    AIR PRESSURE (KG/CM2) 5.6 5.6 5.8

    CORN-COB HOPPER CHARGED (NO.) 15 46 45

    CCP BAG TRANSFERRED TO DRY (NO.) _ 7 ccp

    CCP BAG FILLED AND KEPT IN PLANT (NO.) 7 15 ccp 3 ccp

    BRINE TANK LEVEL(%) Full

    BRINE WATER TEMPRATURE ( C ) 6 6 6

    NH3 RECEIVER LEVEL(BOLTS) OUT + IN 7.5+3 7+3 7.5+4

    KNOCK OUT DRUM LEVEL BOLTS) Nil Nil Nil

    NO OF NH3 CYLINDERS AVAILABLE IN PLANT 5 5 5

    BOILER FEED WATER CONSUMPTION(KL) 3 6 4

    BOILER STEAM GENERATED(MT) 700kg 6 3

    BOILER S/D + GRIT CONSUMPTION(BAGS) 60 140 80

    EXPECTED DRY PLANT PRODUCTION(MT) _

    VPL BATCH DUMPED (REACTOR No.) B

    MAN-POWER

    SHIFT INCHARGE (ENGINEERING) Shivraj Kaushal Nilesh JalondharaMECHANICAL TECHNICIAN(S)/[HELPER] Naik\VRP[1] Mahesh(1) Shankar Desai

    INSTRUMENT TECHNICIAN(S) IL Parmar Vaghela Jignesh

    ELECTRICIAN(S) RC Patel Prajapati Darji

    BOILER/UTILITY OPERATOR(S)/[HELPER] Suthar\Rajesh[1] Bhagyesh(1) Manish

    COB OPERATOR CUM TECHNICIAN/(DRIVER+HELPR) Mayur Mayur(1+1)

    General Shift

    OVER TIME DETAILS

    A

    DAILY ENGINEERING REPORT

    JUBILANT LIFE SCIENCE & JACPL

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    IMP.COMMUNICATION B

    C

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    Remark/Total

    *Make up done from raw water line From 10-15hrs. There is problem in make up line.

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    WORK ORDER

    NUMBER START COMPL TIME(MIN)

    A Workshop P-208 Mech _ 8:00 9:30 90 Box up to be done

    A BD Bullet Tanker Mech 85066 10:30 10:45 15 Hose connection

    A VPL ETP PUMP Mech 814wo-7259 10:15 10:30 15 Coupling displaced

    A VPL Pilot Mech _ 10:00 11:30 90 Leakage from Seal

    A DG DG ALL _ 10:55 11:55 60 Power faliure

    A DRY Cooler Mech _ 8:00 2:00 6hr I\L side rollers to be fit & alingment

    A TMA Bullet Tanker Mech 65119 13:30 13:45 15 Hose connection

    A Utility 150tr pump B Mech - 13:50 To be fit at position.

    A Utility DG cooling water line. Mech _ 14:20 Cooling water line leakage Before HX

    through the valve is damaged.

    A Utility 300TR level switch Inst _ Cleaning done.

    A Cob SC-8,SC-17 Elect O/L Trip

    A VPL Main breaker Elect Not workingB MCC Substation Elect Breaker to be shift at MCC 2 and fixe

    B ETP Submersible pump Elect In power cable pintop to be provide

    B Security room Tube lights Elect New tube light 28 watt to be fit

    B VPL R 301A Elect Vessel lamp to be change

    B MCC Spray pump Elect Sintex box ,contactor and push butto

    B Dry C/T Mech _ 3:30 6:00 2:30 P 405B to be fit at position

    B Dry Cooler Mech _ Drive side roller tyre greasing to be d

    B VPL Brine line Mech _ 5:00 7:00 2:00 Brine line modification done for 2 TR

    B VPL Pilot reactor Mech _ 7:00 8:00 1:00 Seal leakage

    B Liquid EDC tank Mech 85218 Strainer to be open for dechoking

    B VPL Flash tank A Mech 85220 Nipple to be open for dechoking

    B Dry Ribbon mixture Mech 85236 10:45 11:00 00:15 Manhole to be open for dechoking

    B VPL ETP pump Mech 8510 Seal leakage

    C LIQUID CDC Pump Mech. 00.30 1.15 45 Strainer to be open for dechoking

    C LIQUID R 208 Mech. Pump seal Leakage

    C VPL ETP pump 713A Mech. 23.30 00.30 60 Pump to be fit at postion

    C LIQUID R 203 Mech. 84996 6.00 6.30 30 Pump suction valave flange leakage

    C DRY Ribbon Mixure Mech. 85241 00.00 1.00 60 Plate to be open for dechoking

    C DRY XV 3101 Inst. 85250 1.00 1.15 15 Valve operation problem

    C COB HM2 Mech.\Elect. VFD tripped 6 times

    C MCC Cooler Elect. Amp. To be check

    C DRY Cooler Mech. 23.00 6.00 Condition monitoring

    JOB TIMING

    PROBLEM/P

    Date:10.04.2013

    SHIFT PLANT EQUIPMENT DEPT

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    REMARKS/INSTRUCTION

    (IF ANY)

    Fitting at position pending..

    Leakage found during pr test from seal. Seal to beopen

    Motor fail as trail pending.

    Under progress

    Civil structure needs to be break . & hot work to be make.

    To be attend tomorrow in G shift.

    Pending..

    Dechoking work U/P.

    Pending..

    Temp. very from 33 to 35 C and Current very from 10 to 14 Amp.

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    Sr.No PLANT EQUIPMENT

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    JOB DESCRIPTION

    MECHANICAL

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    WORK STATUS EPORTED DAT mpletion D

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    Sr.No JOB DESCRIPTION Completion Date Sr.No

    ELECTRICAL

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    JOB DESCRIPTION Completion Date

    INSTRUMENT

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    Sr.No PLANT EQUIPMENT JOB DESCRIPTION ompletion Dat Sr.No

    MECHANICAL

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    JOB DESCRIPTION Completion Date Sr.No JOB DESCRIPTION

    ELECTRICAL INSTRUMENT

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    Completion Date

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    Sr.No Equipment

    1 sc-1

    2 al-7

    3 sc-10

    45

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    JOB DESCRIPTION

    hopper plate inserted

    spoket fitting

    outlet nozzle fit

    MECHANICAL

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    Work Status Sr.No

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    JOB DESCRIPTION Completion Date Sr.No

    ELECTRICAL

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    JOB DESCRIPTION Completion Date

    INSTRUMENT

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    HISTORY CARD INFORMATIONPLANT EQUIPMENT TYPE OF PROBLEM

    VPL C 401 vaccum pumpPM

    Abnormal sound and gland leakage

    VPL C 301 Vaccum Pump PM Abnormal sound

    BOILER Bucket Elevator GB BD Worm Wheel DamagedDRY Cooler fluid copling PM Low RPM

    EO+CO2 CO2 PUMP BD Abnormal sound

    CHILLING 7.5 TR COMPRESSOR-A BD Abnormal sound

    BD TANK BD Transfer Pump G 901 D PM Abnormal sound

    EO Tank EO transfer pump 106 CM Seal Leakage

    DRY PLANT VIBRTING SCREEN-A (S-304 - A) BM Screen damaged

    LIQUID P 202 PM Seal Leakage

    DRY V 302 PM Alignment not okDRY Y 304 BD Abnormal sound found

    DRY P 301A CM Seal Leakage

    DRY P 301B CM Seal Leakage

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    CORRECTIVE ACTION REMARK

    Cleaning of all parts done. Gasket changed. Bearing

    Changed & gland replaced

    Both DES and NDE side bearing changed

    New spare GB provided form COB plant Worm wheel not available so to be indentOIL changed OIL enklo 46 (4.5 lit)

    Overhauling done in work shop Bearing and piston damaged

    Piston and partision plate found damaged so tobe

    change

    Bearing failed and seal damaged

    New seal fitted

    New screen fitted Both screen changed

    Rotary seal bellow changed

    All four bearing changed,New scrapper blades fitted

    and alignmen done Some of the blades damaged so changed

    Chain slipped from sproket and slates found bent Slates found bent due to overload

    Rotary bellow changed

    Rotary bellow changed

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    REPLACED/REPAIRED PART OTHER IMPORTANT DETAILS

    oilROLL BEARING NUP 308ECJ,SKF , BEARING MR 22

    SRS ,BEARING MR 48 SRS New machined shaft fitted

    Both piston and partion plate

    Bearing-6206(1nos), 6306(1 nos)

    Mech. Seal

    Screen

    Bearing UCF 209,Scrapper plates

    Slates changed and 50 new lock pin provided alignment done

    Bellow 1.275

    Bellow 1.275

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    MONTH NAME OF

    COMPLETE

    14.12.2012 DEC. Kaushal

    17.12.2012 DEC. Nilesh Jaondhara

    30.12.2012 DEC. Nilesh Jaondhara8.1.2013 JAN. Nilesh Jaondhara

    1.2.2013 JAN. Kaushal/Nilesh

    25.01.2013 JAN.

    JAN. Kaushal

    24.02.2013 FEB. Nilesh\Kaushal

    25.02.2013 FEB.

    25.02.2013 FEB. Mahesh\VR Patel

    16.03.2013 March Nilesh Jaondhara

    18.03.2013 March Shivraj

    01.04.2013 April

    01.04.2013 April

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    ENTRY IN

    YES

    YES

    noYES

    no

    no

    no

    YES

    YES

    YES

    YES

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    Title:

    Date/Tim

    Correctiv

    e &

    Preventive Action

    Plan (

    Counter

    measure

    Suggeste

    d

    Trouble

    points:-

    (Rootcause /

    Inspectio

    n result

    Details

    Root Cause Analysis

    What is final action (Immediate corrective action)

    Why-1 Why-2 Why-3 Why-4

    -Plant Trouble Report-

    Reported by:-

    Shift Engineer

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    Person Responsible:-

    Why-5