Shutdown Report July 10

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    SHUT DOWN REPORT

    JULY 2010

    SAMRUDDHI SITE

    1 X 12.5 MW THERMAL POWER PLANT

    Shutdown from : 05 July 2010 - 00:10 Hrs

    Synchronized at : 23 July 2008 - 20:28 Hrs

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    CONTENTS

    DESCRIPTION PAGE No

    1) MAJOR EVENTS : 3

    2) ACTIVITIES ON BOILER : 5

    3) ACTIVITIES ON ASH HANDLING SYSTEM : 8

    4) ACTIVITIES ON COAL HANDLING PLANT : 9

    5) ACTIVITIES ON TURBINE AUXILIARIES : 9

    6) ACTIVITIES ON RO/DM & COOLING TOWER : 10

    7) OTHER ACTIVITIES : 11

    8) SAFETY VALVE SETTINGS REPORT : 12

    9) DISPLACEMENT / SPEED, VIBRATION / SENSORS

    INSPECTION / MEASUREMENT REPORT : 13 - 20

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    MAJOR EVENTS

    Fabrication & Erection of over bed fuel feeding chute for 2nd & 3rd Compartment.

    DCF#1, #2, #3 & #4 new chain replaced.

    DCF #1, #2 & #4 - DE & NDE Shaft with sprockets and bearings replaced.

    ID Fan DE & NDE bearing and Plummer block renewed.

    PA fan #2 DE & NDE bearings renewed.

    FD Fan DE and NDE bearing renewed.

    Boiler all bed drains below and pipe renewed.

    All vertical and Horizontal PA line pipes renewed and extra gate additionally

    added

    Reverse Shuttle Feeder conveyor Belt renewed.

    BFW Pump #2 DE & NDE Bearing hosing, stuffing box and bearing renewed.

    Ash silo bag filter inspection and renewed.

    CHP Dust extraction bag filter inspection and renewed.

    CHP Dust extraction hopper modification.

    CHP Bucket elevator discharge chute renewed.

    Cooling tower fan # 1 gear box renewed.

    TPP & DG all HT panel and LT panel, GCP, GRP panel relays testing coordination

    done.

    TPP All LT Breakers servicing coordination done.

    TPP All HT Breakers servicing and O/G terminal side inspection work done.

    TPP to DG-2 DSLC panel cable termination, programming and commissioned work

    U/p

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    TPP Aux TR-1&2, ESP TR-1&2 Oil filtration and checked Oil BDV test coordination

    done.

    TPP Main Battery Bank and Stand by Battery Bank Load test coordination and

    checked found working normal.

    DG All HT Breaker servicing work done.

    TPP Alternator, Exciter, PMG cleaning and inspection work done.

    TPP Alternator LASCPT panel, NGR panel, GCP, GPR, AVR panel cleaning and

    inspection work done.

    Turbine major O/H Bolt heating equipment power cable, JB fixed and termination

    work done.

    All Boiler & Turbine area MOV valves and actuators cleaned and signal cables

    terminations checked and operation checked from DCS Found normal.

    All local Instrument JBs cleaned and terminations checked found normal.

    All vibration probes & speed probe in Turbine and Alternator side removed for

    major O/H then fixed back found all probes are normal the gap voltage measured

    is enclosed for reference at Page No : 14 - 21

    All Boiler & Turbine aux. system PGs and TGs calibrated and found normal.

    Five numbers of bed thermo well and all thermocouples renewed.

    All Control valves & RPCs calibrated as well as stroke checked found normal.

    All transmitters were calibrated found all in order.

    TPP UPS battery cell voltage checked and found ok.

    FD, PA & ID vibration probe and Temperature sensor serviced and fixed back.

    All FD & PA line power cylinders & all bleed valves and SOVs serviced and fixed

    back.

    MOV valves were stroke & found ok

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    ACTIVITIES ON BOILER

    Remaining fuels emptied from Lignite & Coal bunkers and all bunker lumps

    removed.

    RSFD #1 conveyor Belt renewed.

    All DCFs were cleaned.

    All DCFs were provided with new rail plates.

    DCF #1, #2, #3 & #4 new chain provided.

    DCF #1, #2 & #4 renewed DE & NDE Shaft with sprockets and bearings.

    DCF # 3 DE and NDE both bearing renewed. Boiler PA drain #1, #2, #3 and #4 compartment all pipe line renewed and

    extra gate 16 nos provided.

    Boiler PA horizontal #1, #2, #3 and #4 compartment all pipe line from Air

    box to Mixing nozzle renewed.

    Boiler- compartment #2 and #3rd OBF chute renewed.

    Boiler MCC panel bus, cable chamber and all feeders maintenance work done.

    All Lignite and Coal Pocket feeder motors DE & NDE side bearing renewal and

    winding cleaning varnish applied.

    Phase to Earth IR Value WR Value

    #1 100 meg 11.1 /ph

    #2 100 meg 11.3 /ph

    #3 100 meg 11.5 /ph

    #4 100 meg 11.4 /ph

    #5 100 meg 10.2 /ph

    #6 100 meg 10.9 /ph

    #7 100 meg 10.5 /ph

    #8 100 meg 11.4 /ph

    All Drag Chain Feeder motors DE & NDE side bearing renewal and winding

    cleaning varnish applied.

    Phase to Earth IR Value WR Value

    #1 100 meg 9.1 /ph

    #2 100 meg 9.3 /ph#3 100 meg 9.5 /ph

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    #4 100 meg 9.4 /ph

    Mixing nozzles downstream spool in

    1st Comp. All 4 Nos

    2nd Comp. All 4 Nos3rd Comp. All 4 Nos.

    4th Compt. All 4 Nos. renewed.

    PA drain pipes --- 1st Compt. All 4 nos Renewed

    2nd Compt. All 4 nos Renewed

    3rd Compt. All 4 nos Renewed

    4th Compt. All 4 nos Renewed

    Cross ------ 1st Compt. 3 Renewed

    2nd Compt. 2 Renewed

    3rd Compt. 1 & 2 Renewed

    4th Compt. All cross found in good condition

    Coal nozzle cap 1st Compt. 2 Renewed

    2nd Comp. All caps found in good condition

    3rd Comp - 2,3 & 4 Renewed

    4th Compt. 2 & 3 Renewed

    PA fan #1 fan bearings inspected found normal grease renewed. PA fan

    #1 Discharge damper inspected found gasket and bearing damaged. It was

    renewed and then trial run taken found normal.

    PA fan #1 Motor winding and cable Phase to earth & phase to phase I.R Value :

    200m, Phase to phase; W.R Value : 0.5 /ph. Bearing both ends lubrication,

    feeder side checking work done.

    PA fan #2 Discharge damper inspected found gasket and bearing damaged. It was

    renewed and then trial run taken found normal PA fan #2 Motor winding and cable Phase to earth & phase to phase I.R Value :

    200m, Phase to phase; W.R Value : 0.5 /ph. Bearing both ends lubrication,

    feeder Power and control cable terminal inspection work done.

    FD fan motor side power cable melted, so cable-1&2 new glanded, lugged and

    terminated, DE and NDE bearing and grease renewed, megger value was checked-

    750 meg /phase.

    FD Fan, lignite, Coal, Lime stone VFD panel cleaning and Power and control cable

    terminal inspection work done.

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    ID Fan motor DE and NDE bearing and grease renewed, megger value was

    checked-750 meg /phase, VFD panel cleaning and Power and control cable

    terminal inspection work done.

    ID fan DE and NDE Bearings and Plummer block renewed, alignment work wasdone.

    Furnace, PSH and RSH were cleaned and all air nozzles air flushed.

    BFW Pump #2 DE & NDE side bearing housing, bearing and stuffing box renewed.

    All air boxes cleaned and boxed up.

    Boiler drum was opened and inspected, found normal and boxed up.

    BFW Pump both suction strainers cleaned and fixed back.

    Deaerator was opened inspected, found normal and boxed up.

    Economiser all inspection doors opened and inspected found normal then tube

    surfaces cleaned with compressed air, boxed up and then taken on line.

    Both Drum safety valves, HP Heater safety valve, LP Heater safety valve and Line

    safety valve were serviced. Then, safety valve floating done the setting detail is

    enclosed in Page No : 13

    Oxygen analyzer calibrated.

    BFW pump-1&2 Motor Megger value checked found to be R, Y&B Infinity, DE

    and NDE bearing and grease renewed, air tubes cleaned.

    TPP Auxiliary transformer #1 Break Down value (BDV) was checked.45KV-30SEC;

    55KV-1min; 60KV-2min. Primary winding IR Value 1000 meg , Secondary

    winding - 1000 meg . Bushing, cable & Bus inspection, breather silica gel reneweddone.

    Auxiliary transformer #2 Break Down value (BDV) was checked.40KV-1 min;

    50KV-1min; 60KV-10sec. Primary winding IR Value 1000 meg , Secondary

    winding - 1000 meg . Bushing, cable & Bus inspection, breather silica gel renewed

    done.

    DG auxiliary transformer Break Down value (BDV) was checked - 40KV-1 min;

    50KV-1min; 60KV-1min.

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    ACTIVITIES ON ASH HANDLING SYSTEM

    ESP field I & II was cleaned by Compressed air wash.

    Sys-110 hopper was observed with full level of ash, drained and all system hoppers

    cleaned.

    Ash collected at APH tube sheets on both passes was cleaned.

    ESPI field collecting 1st 3rd and 6th hammer found missing was replaced and Shaft

    support bearing housing worn out-2 nos and renewed.

    ESP Transformer #1 Break Down value (BDV) was checked - 40KV-1 min; 50KV-

    1min; 60KV-10sec. Primary winding IR Value 500 meg , Secondary winding -500 meg . Bushing, cable & Bus inspection, breather silica gel renewed done.

    ESP Transformer #2 Break Down value (BDV) was checked - 45KV-1 min; 50KV-

    45sec; 60KV-15sec. Primary winding IR Value 500 meg , Secondary winding -

    500 meg . Bushing, cable & Bus inspection, breather silica gel renewed done.

    All rapping motors general maintenance done.

    ESP-1&2 all insulators, field collecting plate and emitting rods inspection work

    done.

    AHP MCC panel, ESP MCC panel, ESP controls panel-1&2, P&V Blower MCC panel,

    ACDB Panel, APDB MCC panel bus, cable chamber and all feeders maintenance

    work done.

    Battery charger panel-1&2, DCDB panel bus, cable chamber and all feeders

    maintenance work done.

    Ash hopper all level probes serviced and fixed back.

    AHP all system BFVs & MCVs serviced and fixed back.

    All oil AFRL were renewed.

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    ACTIVITIES ON COAL HANDLING PLANT

    CHP MCC panel bus, cable chamber and all feeders maintenance work done.

    Crusher motor DE and NDE bearing and grease renewed, megger value was

    checked-150 meg /phase.

    All hammers of coal crusher turn it.

    Dust extraction bag filter inspection and cleaning work was done.

    Dust extraction bag filter hopper bottom side modification work was done.

    In dust separator line back filter area all SOVs were calibrated and found ok.

    ACTIVITIES ON TURBINE AUXILIARIES

    Turbine lube oil cooler was opened cleaned and taken on line after leak check.

    Lube oil filter elements 6 Nos renewed for A Filter and for B all elements

    cleaned and fixed back.

    All CEP, MCW Pumps and ACW Pumps suction strainers cleaned and fixed back.

    Alternator cooler tubes were checked found OK. Third alternator cooler was

    cleaned with rod with brush and water jet with service water.

    In Main condenser front and rear inspection doors opened and found the tube

    sheet and tubes are free from deposits, fouling etc. general checked up done and

    boxed up.

    I&C Air Compressor-1&2 winding and cable Phase to earth & phase to phase I.R

    Value : 100m, Phase to phase; W.R Value : 0.6 /ph. Bearing both ends

    lubrication, feeder side Power contactor renewed, power & control cable terminal

    inspection work done

    Turbine MCC panel bus, cable chamber and all feeders maintenance work done.

    CEP-1&2, CWP-1,2&3 winding and cable Phase to earth & phase to phase I.R Value :

    100m, Phase to phase; W.R Value : 0.4 /ph. Bearing both ends lubrication,

    feeder side power & control cable terminal inspection work done

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    CT Fan-1&2, ACWP-1&2, AOP, EOP, Turning gear, VEM-1&2 Motor side

    maintenance work done.

    After the turbine O/H HP Governing actuator operation was checked andcalibrated found normal.

    Turbine ESV limit switches & turning gear engage limit switch serviced and fixed

    back.

    ACTIVITIES ON RO / DM PLANT & COOLING TOWER

    MGF open backwash was done after soaking the media in Hcl for 30 minutes.

    ACF open backwash carried out.

    Service water tank, RO-I & II rejects sumps were cleaned.

    DM Plant MCC panel, Fire & Raw water MCC panel & 2 nd RO plant MCC panel bus,

    cable chamber and all feeders maintenance work done.

    DM Plant HPP-1&2 Power contactor renewed work done.

    CT Fan-1, ACWP-1 Power contactor renewed work done.

    Cooling water sump was cleaned and Fills were cleaned with water jet up to the

    reachable distance.

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    OTHER ACTIVITIES

    The 12.5 MW Captive power plant along with its auxiliary systems were taken

    shutdown on 05-07-2010 at 00.10 Hrs for taking annual maintenance. Apart from thejobs done by us, we have also coordinated for the works done by other agencies

    during the shutdown like :

    1. Turbine Major overhauling was carried out by M/s S V Turbo Engg. Works.

    2. Cooling tower fan # 1 gear box and base frame renewed by M/s Dynamic

    Engineering.

    3. Bucket elevator repairing work was carried out by M/s DRK contractors.

    4. PCC-1&2, all MCCs, BFWP-1&2, GCP, GRP and TG incomer relays testing was done

    by M/s Elsy Tech.

    5. All LT ACBs serviced by M/s L&T.

    6. TPP to DG-2 DSLC panel commissioning work U/P by M/s Wartsilla.

    7. TPP Main/Stand by battery bank load tested by M/s HBL.

    During the course of 18 days long shut down activities stringent safety practices

    were followed and the shutdown is completed safely with zero incidents reported.

    On completion of all planned shut down activities, DP test was done and TPP was

    started and synchronized on 23.07.2010 at 20.28 Hrs .

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    SAFETY VALVE SETTINGS REPORT

    Drum safety valve 2 Nos. and super heater safety valves were serviced assembled

    back to original settings.

    Drum LHS / RHS Safety Valve Model / size : 2 J2 4 HCI

    Super heater Safety Valve Model / size : 1.5 H2 3 HCI

    During the safety valve floating / setting on 22.07.2010 the following settings were

    done:

    Name of the

    safety Valve

    Set

    pressure

    Actual lift

    Pressure

    Resetting

    PressureBlow down

    Drum LHS 78 kg/cm2 77.4 kg/cm274.5

    kg/cm23.75%

    Drum RHS 77 kg/cm276.5

    kg/cm274.4 kg/cm2 2.75%

    Super heater 69 kg/cm2 69.7 kg/cm2 67.7 kg/cm2 2.86%

    At normal operation above valve performance result found satisfactory.

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    TURBINE DISPLACEMENT / SPEED / VIBRATION PROBES INSPECTION &

    MEASUREMENT REPORT

    TAG NO : ZE 3400-A

    SERVICE : Turbine Axial (thrust) displacementMAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOLT

    AGE

    BENTLY

    NEVEDA

    PANELDISPLAY

    DCS

    MONITOR

    DISPLAY

    SENSO

    R

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.1

    0

    BEFORE

    DISMANTLIN

    G- 11.85V

    1.930 m

    /pp0.07 mm OK OK

    21.07.1

    0

    AFTER

    MOUNTING -10.0V0.0 m/p

    p0.0mm OK OK

    TAG NO : ZE 3400-B

    SERVICE : Turbine Axial (thrust) displacement

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLYNEVEDA

    PANEL

    DISPLAY

    DCSMONITO

    R

    DISPLAY

    SENSOR

    STA

    TUS

    PROXIMITO

    R STATUS

    06.07.1

    0

    BEFORE

    DISMANTLI

    NG- 11.39V 1.549 m/pp 0.05mm

    OK.OK

    21.07.1

    0

    AFTER

    MOUNTING -10.0V 0.0 m/pp 0.0mmOK

    OK

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    TAG NO : KQE 3400

    SERVICE : Turbine speed measurementMAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOLT

    AGE

    BENTLY

    NEVEDA

    PANEL

    DISPLAY

    DCS

    MONITOR

    DISPLAY

    SENSOR

    STA

    TUS

    PROXIMIT

    OR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 9.7V OK OK

    06.07.10AFTER

    MOUNTING -10.0V OK OK

    TAG NO : VE 3400-A

    SERVICE : Turbine front shaft vibration

    MAKE : BENTLY NEVADAPROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 10.1 V0.920

    m/pp

    0.49

    micronOK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.872

    m/pp

    0.49

    micronOK OK

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    TAG NO : VE 3400-B

    SERVICE : Turbine front shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 10.02 V0.920

    m/pp

    0.49

    micron OK OK

    21.07.10AFTER

    MOUNTING -10.0 V0.960

    m/pp

    0.49

    micronOK OK

    TAG NO : VE 3401-A

    SERVICE : Turbine rear shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METERPROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOLT

    AGE

    BENTLY

    NEVEDA

    PANEL

    DISPLAY

    DCS

    MONITOR

    DISPLAY

    SENSO

    R

    ST

    AT

    US

    PROXIMIT

    OR STATUS

    06.07.10

    BEFORE

    DISMANTLIN

    G- 9.9 V

    0.630

    m/pp

    0.49

    micronOK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.630

    m/pp

    0.49

    micronOK OK

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    TAG NO : VE 3401-B

    SERVICE : Turbine rear shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLAY

    DCS

    MONITOR

    DISPLAY

    SENSOR

    STA

    TUS

    PROXIMITOR

    STATUS

    06.07.1

    0

    BEFORE

    DISMANTLING - 9.7 V0.561

    m/pp

    0.49

    micron OK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.581

    m/pp

    0.49

    micronOK OK

    TAG NO : VE 3402-A

    SERVICE : Gear box high speed shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MMP/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10 BEFOREDISMANTLING - 9.16V

    0.530

    m/pp

    0.49

    micronOK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.533

    m/pp

    0.49

    micronOK OK

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    TAG NO : VE 3402-B

    SERVICE : Gear box high speed shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 9.26 V0.580

    m/pp

    0.49

    micron OK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.533

    m/pp

    0.49

    micronOK OK

    TAG NO : VE 3403-A

    SERVICE : Gear box low speed shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METERPROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 9.90.633

    m/pp

    0.49

    micronOK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.533

    m/pp

    0.49

    micronOK OK

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    TAG NO : VE 3403-B

    SERVICE : Gear box low speed shaft vibrationMAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 10.1 V0.588

    m/pp

    0.49

    micronOK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.533

    m/pp

    0.49

    micronOK OK

    TAG NO : VE 3404-A

    SERVICE : Generator front shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSORST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 9.8 V0.681

    m/pp

    0.53

    micronOK OK

    21.07.10AFTER

    MOUNTING -10.01 V0.630

    m/pp

    0.49

    micron

    OK OK

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    TAG NO : VE 3404-B

    SERVICE : Generator front shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 9.6 V0.681

    m/pp

    0.59

    micron OK OK

    21.07.10AFTER

    MOUNTING -10.01 V0.581

    m/pp

    0.49

    micronOK OK

    TAG NO : VE 3405-A

    SERVICE : Generator rear shaft vibration

    MAKE : BENTLY NEVADAPROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00

    OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 9.6 V0.630

    m/pp

    0.58

    micronOK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.632

    m/pp

    0.49

    micronOK OK

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    TAG NO : VE 3405-B

    SERVICE : Generator rear shaft vibration

    MAKE : BENTLY NEVADA

    PROBE CABLE LENGTH : 5 METER

    PROXIMITOR MODEL: 3300 XL 5/8 MM

    P/N : 330180-50-00OUTPUT : 7.87 V/mm (200 mV / mil)

    GAP

    VOL

    TAG

    E

    BENTLY

    NEVEDA

    PANEL

    DISPLA

    Y

    DCS

    MONITOR

    DISPLAY

    SENSOR

    ST

    AT

    US

    PROXIMITOR

    STATUS

    06.07.10BEFORE

    DISMANTLING - 9.4 V0.680

    m/pp

    0.49

    micron OK OK

    21.07.10AFTER

    MOUNTING -10.00 V0.581

    m/pp

    0.49

    micronOK OK