M&M Cost Kaizens

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  • 8/12/2019 M&M Cost Kaizens

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    Activity in Kaizen Idea :

    KK JH QM PM HSE OTPM DM E&T

    Team Members :

    Problem/Present Status :

    Benefits in P

    1.

    Sustainance Plan

    S.N. Activity

    Horizontal Deploy

    S.N.

    Different size

    IMPR/TPM/F 01 Rev. 02 : Effective date 25.06.2005

    2

    Separate spare pulleys/belt set need to be maintained for

    ASU 04

    Key word :-

    High Spares inventory cost

    1

    Analysis :

    Belt tension

    checking

    Result :

    9724

    4420

    KAIZEN SHEETL8 PM

    Common sizeTarget

    Loss :

    Finish date

    Bench Mark

    Kaizen Theme :

    To reduce spares inventory cost on ASU 04 fan & motor

    pulleys & belts.

    Pulley/belt of ASU 04 of different size

    than that of ASU 01,02 & 03.

    Pulley sizes of ASU 04 fans of different size than that of

    ASU 01, 02 & 03

    30.0Start date

    15.0

    PU

    CELL

    REF. NO.

    New Paint Shop

    Cell 04

    NPS\F-06\PM\C2\TT\090

    Before Sketch

    1

    J D Nikam, P.K.Borka

    Belt replacement

    2

    After Sketch

    Countermeasure :

    Replaced ASU # 04 Fan & motor pulleys with

    standard pulley, same as ASU 01,02 & 03.

    Saving in electr

    Area

    97240

    44200

    25000

    50000

    75000

    100000

    Before After

    SPC 5000 belt Inventory cost

    Costin

    Rs

    V Belt Pulley V Belt Pulley

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    ValueBefore

    replacement

    After

    replacement

    Before

    replacement

    After

    replacementFan RPM 690 692 689.0 693

    Pulley diameter driver 410 325 410.0 325

    Pulley diameter driven 810 640 810.0 640

    V-belt SPC 5600 SPC 5000 SPC 5600 SPC 5000

    Average Current (amps) 184.5 179 186 181.5

    KWH 119.35 115.80 120.32 117.41

    Units/day 2029.01 1968.52 2045.50 1996.02

    Units/Year 568122.27 551186.38 572741.15 558884.51

    Rs per year 1914572.06 1857498.10 1930137.69 1883440.81

    Total

    Net saving Rs

    Saving calculation

    57073.96 46696.88

    103770.84

    Fan 01 Fan 02

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    ctivity in Kaizen Idea :

    KK JH QM PM HSE OTPM DM E&T

    aizen Theme : Countermeasure :

    Team Members :

    roblem/Present Status :

    Benefits in P Q C D

    1

    2

    Sustainance Plan :

    S.N. Activity

    Horizontal Deployment :

    S.N.

    High vapourisation rate.

    MPR/TPM/F 01 Rev. 02 : Effective date 25.06.2005 TPM

    3

    Target D

    2

    cell leader

    Resp Frequen

    Cell leader weekly

    01.04.05

    01.05.05

    6-Mar

    1 Check lubrication

    oil level

    2

    RespArea

    All process

    conveyors

    Low evapouration rateTarget

    Start date

    Finish date

    Bench Mark

    1

    NPS/F-06/PM/401

    ey word :-

    Afterefore

    KAIZEN SHEETLoss :U

    ELL

    EF. NO.

    New Paint Shop

    Result :

    High evapouration rate of lubrication oil

    PM

    nalysis :

    High lubrication oil consumption

    High lubrication cost on Sealer Oven conveyor

    High lubrication frequency

    Lubrication frequency reduced from w

    monthly

    Cleaning time of oven reduced by 8 m

    during deep cleaning activity.

    o reduce the lubrication cost on process conveyor

    igh lubrication cost on process conveyor and buffer

    hains. Yellowish stain marks oberved on insides of oven.

    Use of low vapourisation rate lubrication oil.

    P. K. Borkar, V. G. Ugale

    TPM in

    268950

    178920

    5000

    105000

    205000

    305000

    Before After

    Cost per year per conveyor

    Rs

    Parameter Value

    Base Oil Synthetic ester

    Base Oil Viscosity 40 deg 398 cst

    100 deg 29.2 cst

    Evapourisation rate 0.3% per hour

    Chain wetness 20 days

    Carbonisation of oil No traces observed.

    GI panels insidesoven

    No stains observed

    Parameter Value

    Base Oil Not known

    Base Oil viscosity 40 deg 220 cst

    100 deg 9 cst

    Evapouration rate 5 % every hour

    Chain wetness 07 days

    Carbonisation of oil Yes

    GI panels insides oven Yellowish stains

    OKS 352/2 Rocol chain guard 230

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    PU : New Paintshop Loss :

    CELL : NPS/04/39 Breakdown KAIZEN SHEETREF. NO. :

    Activity in Kaizen Idea : Bench Mark 6 breakdown/y

    KK JH PM QM OTPM E&T SHE IFC Arrangement for re-using pump by-pass water Target 0 breakdown

    Kaizen Theme : Start date

    Finish dateTeam Members :

    To eliminate breakdown on Paint stripping pump.

    Before Sketch

    Problem / Present Status :

    Cavitation of pump due to entrapped air in feed water

    Heavy vibration and knocking in pump head

    7-Nov-04

    Counter Measure : Connecting by-pass water to tank Benefits in P, Q, C, D, S, M

    12-Nov-04

    P. K. Borkar, A. M. Khond

    After Sketch

    Discharge ventil and sleeve broken

    Feed water line directly connected to plant supply line

    1) 96 manhours saving/year

    2) Spares cost saved 1.2 lac

    3) Water saving 15000 m3/ye

    (Rs saved 1.87 Lac/year)

    Horizontal Deployment :ResultsAnalysis : Paint stripping pump not working

    Nil

    TPM

    F04

    06

    Nov 04Breakdownincidences

    0

    To spray lance

    Feed waterBy-pass waterSpray lance water

    Feed waterBy-pass waterSpray lance water

    Waste water tank To spray lance Waste water tank

    Overheadtank

    Mar 05

    TPM Secretariat - Nasik

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    Activity in Kaizen Idea :

    KK JH QM PM HSE OTPM DM E&T

    Team Members :

    Benefits in P Q C D

    1.

    2.

    Sustainance Plan :

    S.N. Activity

    Horizontal Deployment :

    S.N.

    2

    Inefficient equipment

    Analysis :

    Sealer oven

    holding fanCell 02

    1

    Targ

    Ma

    High power consumption at Surfacer oven ciruclation fan

    Fan Motor drawing higher current

    Ma

    Key word :-

    After SketchBefore Sketch

    Result :

    Less overall efficiency of blower/motor.

    High power required to deliver required output.

    Energy

    Kaizen Theme :

    To reduce energy consumption on Surfacer Oven

    circulation fans.

    Cell-02

    NPS\F-06\PM\C2\KAIZEN SHEET

    Loss :PU

    CELL

    REF. NO.

    New Paint Shop

    119819 Electical units

    60000 Electrical units

    10.04.05

    20.05.05

    Countermeasure :

    To change 45kw motor to 37kw motor.(Heat up 01, Holding

    01 and Holding 02 circulation fans.)

    Bench MarkEfficient motor.

    Target

    Start date

    Finish date

    Problem/Present Status :

    High power consumption on Hot Air Circulation fan

    V. G. Ugale P. K. Borkar.

    Elimination of Soft starter 03 nos

    outflow Rs 1.00 lac

    Pm time reduction by 30 minutes

    tobetter mountings of motor.

    Check motor

    current

    Cell 02

    1

    Sealer oven Heat

    up fan

    Area Resp

    2

    Resp Freq

    cell 02 Mo

    TPM in

    500000

    1000000

    1500000

    Before After

    units

    3,61,363Electrical units/year

    2,01370Electrical units/year

    Savings

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    Holding 02

    Motor capacity 45 KW Motor capacity 37 KW

    RPM 2910 RPM 1465

    Flow rate 150 m3/hr Flow rate 150 m3/hr

    Head 35 mtr Head 37 mtr

    Average current 37.27 Average current 20.13

    KWH 24.11 KWH 13.02

    KWH per day 433.98 KWH per day 234.40

    Rs per day 1462.51 Rs per day 789.92

    Rs per Year 409504.17 Rs per Year 221178.40

    KWH per year 121514.59 KWH per year 65631.57

    Holding 01 UnitMotor capacity 45 KW Motor capacity 37 KW Rs

    RPM 1440 RPM 1440

    Discharge 45000 m3/hr Discharge 45000m3/hr Average current 37.27 Average current 20.13

    KWH 24.43 KWH 13.54

    KWH per day 439.74 KWH per day 243.72

    Rs per day 1481.92 Rs per day 821.34

    Rs per Year 414938.66 Rs per Year 229974.19

    KWH per year 123127.20 KWH per year 68241.60

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    Heat UP 01Motor capacity 45 KW Motor capacity 37 KW

    RPM 2910 RPM 1465

    Flow rate 150 m3/hr Flow rate 150 m3/hr

    Head 35 mtr Head 37 mtr

    Average current 35.80 Average current 20.60KWH 23.16 KWH 13.33

    KWH per day 416.86 KWH per day 239.87

    Rs per day 1404.83 Rs per day 808.37

    Rs per Year 393352.54 Rs per Year 226342.52

    KWH per year 116721.82 KWH per year 67163.95

    361363.61 201037.13 160326.49

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    Before After

    361364 201037

    1217795 677495

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    641305.9433

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    Saving Per Year ( Rs. In L

    Sr Area

    1 Electrical Energy

    2 LPG

    3 Other

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    cs)

    Saving / Year( In Lac)

    52.3

    37.19

    9.65