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8/12/2019 M&M Cost Kaizens
1/11
Activity in Kaizen Idea :
KK JH QM PM HSE OTPM DM E&T
Team Members :
Problem/Present Status :
Benefits in P
1.
Sustainance Plan
S.N. Activity
Horizontal Deploy
S.N.
Different size
IMPR/TPM/F 01 Rev. 02 : Effective date 25.06.2005
2
Separate spare pulleys/belt set need to be maintained for
ASU 04
Key word :-
High Spares inventory cost
1
Analysis :
Belt tension
checking
Result :
9724
4420
KAIZEN SHEETL8 PM
Common sizeTarget
Loss :
Finish date
Bench Mark
Kaizen Theme :
To reduce spares inventory cost on ASU 04 fan & motor
pulleys & belts.
Pulley/belt of ASU 04 of different size
than that of ASU 01,02 & 03.
Pulley sizes of ASU 04 fans of different size than that of
ASU 01, 02 & 03
30.0Start date
15.0
PU
CELL
REF. NO.
New Paint Shop
Cell 04
NPS\F-06\PM\C2\TT\090
Before Sketch
1
J D Nikam, P.K.Borka
Belt replacement
2
After Sketch
Countermeasure :
Replaced ASU # 04 Fan & motor pulleys with
standard pulley, same as ASU 01,02 & 03.
Saving in electr
Area
97240
44200
25000
50000
75000
100000
Before After
SPC 5000 belt Inventory cost
Costin
Rs
V Belt Pulley V Belt Pulley
8/12/2019 M&M Cost Kaizens
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ValueBefore
replacement
After
replacement
Before
replacement
After
replacementFan RPM 690 692 689.0 693
Pulley diameter driver 410 325 410.0 325
Pulley diameter driven 810 640 810.0 640
V-belt SPC 5600 SPC 5000 SPC 5600 SPC 5000
Average Current (amps) 184.5 179 186 181.5
KWH 119.35 115.80 120.32 117.41
Units/day 2029.01 1968.52 2045.50 1996.02
Units/Year 568122.27 551186.38 572741.15 558884.51
Rs per year 1914572.06 1857498.10 1930137.69 1883440.81
Total
Net saving Rs
Saving calculation
57073.96 46696.88
103770.84
Fan 01 Fan 02
8/12/2019 M&M Cost Kaizens
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ctivity in Kaizen Idea :
KK JH QM PM HSE OTPM DM E&T
aizen Theme : Countermeasure :
Team Members :
roblem/Present Status :
Benefits in P Q C D
1
2
Sustainance Plan :
S.N. Activity
Horizontal Deployment :
S.N.
High vapourisation rate.
MPR/TPM/F 01 Rev. 02 : Effective date 25.06.2005 TPM
3
Target D
2
cell leader
Resp Frequen
Cell leader weekly
01.04.05
01.05.05
6-Mar
1 Check lubrication
oil level
2
RespArea
All process
conveyors
Low evapouration rateTarget
Start date
Finish date
Bench Mark
1
NPS/F-06/PM/401
ey word :-
Afterefore
KAIZEN SHEETLoss :U
ELL
EF. NO.
New Paint Shop
Result :
High evapouration rate of lubrication oil
PM
nalysis :
High lubrication oil consumption
High lubrication cost on Sealer Oven conveyor
High lubrication frequency
Lubrication frequency reduced from w
monthly
Cleaning time of oven reduced by 8 m
during deep cleaning activity.
o reduce the lubrication cost on process conveyor
igh lubrication cost on process conveyor and buffer
hains. Yellowish stain marks oberved on insides of oven.
Use of low vapourisation rate lubrication oil.
P. K. Borkar, V. G. Ugale
TPM in
268950
178920
5000
105000
205000
305000
Before After
Cost per year per conveyor
Rs
Parameter Value
Base Oil Synthetic ester
Base Oil Viscosity 40 deg 398 cst
100 deg 29.2 cst
Evapourisation rate 0.3% per hour
Chain wetness 20 days
Carbonisation of oil No traces observed.
GI panels insidesoven
No stains observed
Parameter Value
Base Oil Not known
Base Oil viscosity 40 deg 220 cst
100 deg 9 cst
Evapouration rate 5 % every hour
Chain wetness 07 days
Carbonisation of oil Yes
GI panels insides oven Yellowish stains
OKS 352/2 Rocol chain guard 230
8/12/2019 M&M Cost Kaizens
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PU : New Paintshop Loss :
CELL : NPS/04/39 Breakdown KAIZEN SHEETREF. NO. :
Activity in Kaizen Idea : Bench Mark 6 breakdown/y
KK JH PM QM OTPM E&T SHE IFC Arrangement for re-using pump by-pass water Target 0 breakdown
Kaizen Theme : Start date
Finish dateTeam Members :
To eliminate breakdown on Paint stripping pump.
Before Sketch
Problem / Present Status :
Cavitation of pump due to entrapped air in feed water
Heavy vibration and knocking in pump head
7-Nov-04
Counter Measure : Connecting by-pass water to tank Benefits in P, Q, C, D, S, M
12-Nov-04
P. K. Borkar, A. M. Khond
After Sketch
Discharge ventil and sleeve broken
Feed water line directly connected to plant supply line
1) 96 manhours saving/year
2) Spares cost saved 1.2 lac
3) Water saving 15000 m3/ye
(Rs saved 1.87 Lac/year)
Horizontal Deployment :ResultsAnalysis : Paint stripping pump not working
Nil
TPM
F04
06
Nov 04Breakdownincidences
0
To spray lance
Feed waterBy-pass waterSpray lance water
Feed waterBy-pass waterSpray lance water
Waste water tank To spray lance Waste water tank
Overheadtank
Mar 05
TPM Secretariat - Nasik
8/12/2019 M&M Cost Kaizens
5/11
Activity in Kaizen Idea :
KK JH QM PM HSE OTPM DM E&T
Team Members :
Benefits in P Q C D
1.
2.
Sustainance Plan :
S.N. Activity
Horizontal Deployment :
S.N.
2
Inefficient equipment
Analysis :
Sealer oven
holding fanCell 02
1
Targ
Ma
High power consumption at Surfacer oven ciruclation fan
Fan Motor drawing higher current
Ma
Key word :-
After SketchBefore Sketch
Result :
Less overall efficiency of blower/motor.
High power required to deliver required output.
Energy
Kaizen Theme :
To reduce energy consumption on Surfacer Oven
circulation fans.
Cell-02
NPS\F-06\PM\C2\KAIZEN SHEET
Loss :PU
CELL
REF. NO.
New Paint Shop
119819 Electical units
60000 Electrical units
10.04.05
20.05.05
Countermeasure :
To change 45kw motor to 37kw motor.(Heat up 01, Holding
01 and Holding 02 circulation fans.)
Bench MarkEfficient motor.
Target
Start date
Finish date
Problem/Present Status :
High power consumption on Hot Air Circulation fan
V. G. Ugale P. K. Borkar.
Elimination of Soft starter 03 nos
outflow Rs 1.00 lac
Pm time reduction by 30 minutes
tobetter mountings of motor.
Check motor
current
Cell 02
1
Sealer oven Heat
up fan
Area Resp
2
Resp Freq
cell 02 Mo
TPM in
500000
1000000
1500000
Before After
units
3,61,363Electrical units/year
2,01370Electrical units/year
Savings
8/12/2019 M&M Cost Kaizens
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Holding 02
Motor capacity 45 KW Motor capacity 37 KW
RPM 2910 RPM 1465
Flow rate 150 m3/hr Flow rate 150 m3/hr
Head 35 mtr Head 37 mtr
Average current 37.27 Average current 20.13
KWH 24.11 KWH 13.02
KWH per day 433.98 KWH per day 234.40
Rs per day 1462.51 Rs per day 789.92
Rs per Year 409504.17 Rs per Year 221178.40
KWH per year 121514.59 KWH per year 65631.57
Holding 01 UnitMotor capacity 45 KW Motor capacity 37 KW Rs
RPM 1440 RPM 1440
Discharge 45000 m3/hr Discharge 45000m3/hr Average current 37.27 Average current 20.13
KWH 24.43 KWH 13.54
KWH per day 439.74 KWH per day 243.72
Rs per day 1481.92 Rs per day 821.34
Rs per Year 414938.66 Rs per Year 229974.19
KWH per year 123127.20 KWH per year 68241.60
8/12/2019 M&M Cost Kaizens
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Heat UP 01Motor capacity 45 KW Motor capacity 37 KW
RPM 2910 RPM 1465
Flow rate 150 m3/hr Flow rate 150 m3/hr
Head 35 mtr Head 37 mtr
Average current 35.80 Average current 20.60KWH 23.16 KWH 13.33
KWH per day 416.86 KWH per day 239.87
Rs per day 1404.83 Rs per day 808.37
Rs per Year 393352.54 Rs per Year 226342.52
KWH per year 116721.82 KWH per year 67163.95
361363.61 201037.13 160326.49
8/12/2019 M&M Cost Kaizens
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Before After
361364 201037
1217795 677495
8/12/2019 M&M Cost Kaizens
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641305.9433
8/12/2019 M&M Cost Kaizens
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Saving Per Year ( Rs. In L
Sr Area
1 Electrical Energy
2 LPG
3 Other
8/12/2019 M&M Cost Kaizens
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cs)
Saving / Year( In Lac)
52.3
37.19
9.65