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NLC India Ltd(Formerly Neyveli Lignite Corporation Ltd)
(A ‘Navratna’ Govt. of India Enterprise)
Thermal Power Station - II
Welcomes You All
QUALITY CIRCLE
1
CREATING WEALTH FOR WELL BEING
OUR ORGANISATION
2
NLC INDIA LTD
( formerly Neyveli Lignite Corporation Ltd)
Our Vision :To emerge as a leading mining and Power Company, with Social Responsiveness accelerating Nation’s growth.
A NAVARATNA COMPANY UNDER THE MINISTRY OF COAL IN THE 60 TH YAER OF EXISTANCE
MOVED FROM AN ONLY LIGNITE MINING AND POWER GENERATION COMPANY TO BECOME AN ENERGY COMPANY.
PRESENT CAPACITY: MINING :30.6 MTPA
TOTAL POWER GENERATION :4287.5 MW
THERMAL:4531 MW
WIND :51 MW
SOLAR :240 MW
DIVERSIFYING INTO COAL BASED POWER GENERATION AND RENEWABLE ENERGY WITH A
VISION TO ACHIEVE 19831 MW BY 2025 FROM 4287.5 MW
PRESENCE IN TAMIL NADU, RAJASTAN, ORISSA,
UP, WEST BENGAL AND ANDAMAN
3
ABOUT NLC INDIA LTD
CONSISTS 7 UNITS OF 210 MW EACH.
TOTAL CAPACITY 1470 MW
ANNUAL TURNOVER OF MORE THAN RS1000 CRORES, TPS II CATERS TO THE REQUIREMENTS OF THE SOUTHERN STATES
FIRST LIGNITE FIRED STATION WITH 210MW UNITS
MERITORIOUS PRODUCTIVITY REWARD BY CENTRAL ELECTRICITY AUTHORITY CONTINOUSLY FROM 1988 ONWARDS.
STATION WITH ISO 9001& 14001 CERTIFICATIONS
4
THERMAL POWER STATION - II
55
INTRODUCTION
QC NAME: GREEN ENERGYOUR INSPIRATION Mr.M. KASINATHAN /CGM
OUR HOD Mr. G.BAPUJEE/DGM
OUR MOTIVATORS Mr.M. KANAGALINGAM GM/O&MMr. K.S.GOPALAKRISHNAN /GM/MTCE
CO ORDINATOR Mr. B.MATHIVANAN /DGM
FACILITATOR Mr. N.ABDUL JALEEL PH 09486586527
LEADER Mr. S.RAVICHANDRAN PH 09486111070
DY. LEADER Mr. V.ELAVARASAN PH 07598614229
MEMBERS Mr. D.KASINATHAN PH 09443882108Mr. G.NEELAKANDAN PH 09442231635
66
QUALITY CIRCLE PROFILEQCFI NO : 081799100038
QC NAME GREEN ENERGY
UNIT TPS –II, NLC INDIA
DIVISIONTURBINE MAINTENANCE
CIRCLE REGISTERED IN
MARCH - 2013
PROBLEMS IDENTIFIED
57
PROBLEMS SOLVED
7
CASE STUDIES PRESENTED
6
QC MEETING SCHEDULE
FrequencyEvery Second &
Fourth Friday
Duration Two Hour / Month
Total Hours
Spent for this
project 24 Hrs
Attendance90%
No of Meeting
Held for this
Project12
7
WON THE
GOLDEN
AWARD AT
CCQC
2013
HYDERABAD
2016
COIMBATORE
2017
CHENNAI
PAR
EXCELLANCE
AWARD IN
NCQC-2016
HELD AT
RAIPUR
88
CASE STUDY ON
OIL TOPPING UP IN BOILER
FEED PUMP HYDRO COUPLING
9
THIS IS OUR
SEVENTH CASE STUDY PRESENTATION
QC TOOLS INVOLVED
1010
STEP ACTIVITY QC TOOLS SLIDE NO.
1 Identification of problem Brain storming 11- 14
2 Selection of problem ABC analysis and 3P analysis 15 – 22
3 Definition of problem Flow diagram 23 – 30
4 Analysis of problem Data collection, 4W 1H 31-32
5 Finding out the causes Brain Storming,Fish bone diagram
33-35
6 Root cause analysis Why-Why analysis 36-37
7 Data analysis Brain Storming, Paretto Diagram 38-42
8 Development of solution Brain storming,ECT Chart 43-45
9 Foreseen probable resistance Brain storming 46
10 Trial implementation PDPC & PDCA Chart 47-52
11 Regular implementation PDCA Chart 53
12 Follow-up and review Data collection, Paretto,AA chart 54- 61
1111
STEP-1: IDENTIFICATION OF PROBLEM
BRAIN STORMING
Sl.No. Problems Identified TYPE
1 HIGHER POWER CONSUMPTION IN BOILER FEED PUMPS C
2 ACCUMULATION OF SILT IN CONDENSER C
3 PASSING IN R/C VALVE OF BFPS A
4 DAMAGE OF CIRCULATING WATER PUMP SUCTION SCREENS A
5 LESS CIRCULATING WATER PRESSURE IN STAGE-I C
6 FREQUENT BEND PUNCTURE IN HPH OPERATING VENTS A
7 CORROSION IN INTERMITTENT COLUMN OF CWPS C
8 PARTING PLANE EROSSION IN BFP BOOSTER PUMP A
9 NRV STRUCK UP IN SEAL DRAIN PUMP A
10 FREQUENT LEAK IN BOILER FEED PUMP SUCTION FILTER B
11 CONDENSER VACUUM LOWER THAN NORMAL IN UNIT-V B
12 HIGH HP TURBINE VIBRATION IN UNIT-VII C
13 HOSE DAMAGE IN HP BYPASS OIL SYSTEM A
14 PROBLEM IN MACHINIG OF VALVE GATES B
15 EXCESS OIL CONSUMPTION IN MAIN OIL TANK DUE TO VAPOUR LOSS A
1212
IDENTIFICATION OF PROBLEM
BRAIN STORMING
Sl.No. Problems Identified TYPE
16 VIBRATION PROBLEM IN OIL VAPOUR EXTRACTION FANS A
17 PROBLEM IN REMOVING OF CIRCULATING WATER PUMP IMPELLAR SHAFT B
18 BURST OF RUBBER EXPANSION JOINTS IN CIRCULATING WATER LINES C
19 FAILURE OF MAIN STEAM AND HOT REHEAT STRAINER GASKETS A
20 HUNTING OF TURBINE GOVERNING VALVES C
21 PUNCTURE OF T-LINE HOSES IN HP BYPASS SYSTEM A
22 FREQUENT SCALING OF CONDENSER TUBES. C
23 FREQUENT PUNCTURE OF COOLING TOWER UPRAISER PIPES B
24 CHOKE IN AIR CONDITIONING PLANT COOLING TOWER BASIN A
25 LEAKS IN CIRCULATING WATER TUNNEL MANHOLE DOORS. B
26 FREQUENT LEAK IN HRH AND MS STRAINERS A
27 CHOKES IN AIR HANDLING UNIT FILTERS A
28 CW PUMPS SHAFT RUN OUT PROBLEM B
29 CRACKS IN AIRCONDITIONING PLANT COMPRESSOR CRANK SHAFTS C
30 FREQUENT BONNET LEAK IN HP HEATER DRAIN CONDENSATE NRVs A
STEP-1
1313
IDENTIFICATION OF PROBLEM
BRAIN STORMING
Sl.No. Problems Identified TYPE
31 FREQUENT FLANGE & BONNET FAILURE IN HP HEATER DRAIN CONDENSATE PCVS & ISOLATION VALVES
A
32 HIGH O & M COST OF MAW 10 AND MAW 50 B
33 PUNCTURES IN TURBINE DRAIN PIPES A
34 STEAM LEAK THROUGH TURBINE GLANDS A
35 SAFETY VALVE PASSING A
36 STEM FAILURE IN HP B/P VALVE A
37 FAILURE OF BFP DISCHARGE VALVE A
38 PASSING IN CEP RECIRCULATION VALVE A
39 FREQUENT BONNET LEAK IN DR34 BEFORE GATE VALVE A
40 FREQUENT BONNET LEAK IN THE PCV DR11 B
41 FREQUENT FLANGE LEAKS IN AST TO SEALS LINE A
42 OIL CONTAMINATION IN BOILER FEED PUMPS C
43 FREQUENT FAILURE OF DIAPHRAGM IN HOTWEL MAKE UP VALVES C
44 OIL CONTAMINATION IN TURBINE BRG. & MOT C
STEP-1
14
Sl.No. Problems Identified
45 HIGH AUXIALIARY STEAM TEMPERATURE C
46 BEARING FAILURES IN MAL VALVES A
47 BEARING FAILURES IN BALL CLEANING SYSTEM PUMPS A
48 FREQUENT BONNET FAILURE IN BFP DISCHARGE NRV A
49 METALLIC BELLOW PUNCTURES C
50 MAL VALVE GLAAND LEAK A
51 SAFETY VALVE FLANGE FAILURE A
52 HP HEATER SOV PASSING A
53 MOTOR OPERAED VALVE STEM THREAD FAILURE A
54 OPERATING VENT BEND FAILURE A
55 BFP BALANCING LEAK OFF FLANGE FAILURES A
56 CWP THRUST BEARING TEMP HIGH A
57 DELAY IN OIL TOPPING UP IN BFP HYDRO-COUPLING A
IDENTIFICATION OF PROBLEM
BRAIN STORMINGSTEP-1
STEP-2: SELECTION OF PROBLEM
1515
In day to day operation, we have identified 57 Problems in our work
area.
✓ All the problems have been studied in detail and are listed as Type
A,B,C.
✓ We have decided to study Type – A problem as this can be solved by
QC team itself.
✓ A Type : 34 problems (Problem in the capacity of the QC team itself)
✓ B type : 9problems (Problems which can be solved with the help of
other division)
✓ C type :14 problems (Problems which can be solved with the help of
top management )
34
16
Problem Categorization
Total Problems
57
TO BE SOLVED BYTHE CIRCLEMEMBERS
OTHER DEPT. HELP REQUIRED
MANAGEMENTAPPROVAL REQD.
9 14
BA C
17
STEP-2: SELECTION OF PROBLEM
3P – Analysis
Proprietary, priority, Preference
PROPRIETARY - I STAGE (GROUPING – P1)
PRIORITY - II STAGE (SELECT A FEW IMPORTANT FROM THE ABOVE - P2)
PREFERENCE - III STAGE (FINAL SELECTION OF ONE/TWO PROBLEM - P3)
17
We have decided to undertake 3P analysis for A type
problems i.e to decide Proprietary, Priority and final
selection with preference to the problem
STEP-2: SELECTION OF PROBLEM
PROPRIETARY GROUPING: UNDER PROPRIETARY GROUPING WAS DONE
1818
While visualizing the proprietary classification, we had conceptual base
of our divisions, objective & goals in the following categories and the
34 problems under category A were segregated according to
proprietary (4 aspects)
S.No PROPRIETARY GROUP PROBLEM No TOTAL
1 Cost related 16,31,33,37,38,41,46,51 8
2 Safety related 19,26,27,30,,36,47,50,55 8
3 Environment related 8,13,15,21,24,48,54 7
4 Process related 3,4,6,9,34,35,39,52,53,56,57 11
STEP-2: SELECTION OF PROBLEM
1919
Priority by QC members – P2
After analyzing the problems one by one in QC meeting, members
decided to take process related problems as these problems if left not
attended may result in loss of generation.
Priority given by QC members are tabulated here
PROBLEM SELECTED BY MEMEBERSPROBLEM
NO PROBLEM PRIORITY GIVEN BY
57 DELAY IN OIL TOPPING UP IN BFP
HYDRO-COUPLING
V.ELAVARASAN
3 PASSING IN R/C VALVE OF BFPS D.KASINATHAN
26FREQUENT LEAK IN HRH AND MS
STRAINERS
G.NEELAKANTAN
STEP-2:SELECTION OF PROBLEM
2020
Preference- To decide the preference, weightage
method used. Marks given by each member is
recorded below
PROBLEM
NO
PROBLEM
PRIORITY GIVEN
BY MEMBERS 1 TO
10
TOTAL
SCORE
E K N
57
DELAY IN OIL TOPPING UP IN BFP HYDRO-
COUPLING 9 8 7 24
3PASSING IN R/C VALVE OF BFPS
6 9 6 21
47FREQUENT LEAK IN HRH AND MS
STRAINERS7 6 9 22
STEP-2: SELECTION OF
PROBLEM
By using all the above tools and techniques, datacollection and data analysis, our team has arrived at adecision that the problem No. 56 has maximum impacton the process, which was given top preference.
Problem No. 57 scored maximum, so our problem now is
2121
DELAY IN OIL TOPPING UP IN
BFP HYDRO-COUPLING
MILE STONE CHART FOR
ACTION PLAN
2222
STEP ACTIVITY MONTH
OC
T
2017
NO
V
2017
DE
C
2017
JA
N
2018
JF
EB
2018
MA
R
2018
AP
R
2018
MA
Y
2018
JU
N
2018
JU
L
2018
AU
G
2018
SE
P
2017
1 Definition of problem
2 Analysis of problem
3 Cause and effect diagram
4 Root cause analysis
5 Data analysis
6 Development of solution
7 Foreseen probable resistance
8 Trial implementation
9 Completion in all Pumps
Starting Date: 01.10.2017 Ending date: 31.08.2018
Note : Follow-up and review is a continuous process
STEP – 3 DEFINING THE PROBLEM
24
BFP 5000 RPM
HYDROCOUPLING
5200 RPM
MOTOR 1400 RPM
3500 KW
DRIVE FOR BOILER FEED PUMP
320 T/Hr flow
180 Ksc pressure
170 deg Temp
STEP – 3 DEFINING THE PROBLEM
• There are 3 no BFPs for each unit , 2 no will be kept in service and the third one is kept as auto reserve.
• Boiler feed Pump supplies Feed water to Boiler at 180 Kscpressure and 170 degree centigrade temp.
• Each BFP pumps approximately 320 T/Hr of feed Water to Boiler.
• If any of the running pump trips, reserve pump will start automatically and if reserve pump is not available, unit load has to be reduced by 50% i.e. From 210 MW to 105 MW.
BOILER FEED PUMP
STEP – 3 DEFINING THE PROBLEM
• Each BFP is driven by a Hydro Coupling which in turn gets the drive from a 3.5 MW motor.
• The Hydro Coupling Oil Tank not only supplies working fluid to hydro Coupling but also supplies Lub oil to Pump & Motor.
BOILER FEED PUMP
27
➢Capacity of the Hydro Coupling oil tank is 700 lit
Oil Tank level can be seen through a level view glass
marked LOW, NORMAL, HIGH
➢It is customary to top up oil when the oil level
drops below Normal.
➢Oil level drops due to evaporation & leakage losses
STEP-3: DEFINING THE PROBLEM
Hydro Coupling oil tank
28
HI LEVEL
NORMAL LEVEL
LOW LEVEL
STEP-3: DEFINING THE PROBLEM
29
STEP-3: DEFINING THE PROBLEM
Oil Topping Up
➢ Oil is Topped up by a hand
pump after opening the lid
at the top of the oil tank
➢ In a running pump
Oil temp is around 110 degree
centigrade.
Speed of the Hydro Coupling
will be around 5000 rpm.
If the lid is opened in a
running pump oil will be
splashing out of the tank at
high speed and will lead to
injuries to the workmen.
Hence it is advisable to stop
the running pump and then top
up oil.
❖Before stopping the pump, reserve pump has to be started and loaded slowly and paralleled with the running pumps.
❖The pump for which oil is to be topped has to be unloaded slowly and then stopped.
❖The entire process of pump change over takes approximately 30 minutes during which all the 3 BFPs will be in service.
❖Due to the change over process not only the oil topping gets delayed, but also there is considerable increase in power consumption.
❖During oil top the pump will not be available for service. Hence LINE CLEAR has to be obtained.
❖Since non availability of one pump may have consequence of 50% load reduction if another pump trips, permission has to be obtained from CHIEF GENERAL MANAGER 30
STEP-3: DEFINING THE PROBLEMPump Change Over
31
STEP-4 ANALYSIS OF PROBLEM
4 W 1H
WHAT IS THE PROBLEM ? DELAY IN OIL TOPPING UP IN BFP HYDRO COUPLING
WHEN IT IS NOTICED? WHEN OIL LEVEL IS LOW IN BFP HC
WHERE IT OCCURRED? IN RUNNING BFPS
WHICH WAS AFFECTED? OIL TOPPING UP
HOW IT HAPPENED? DUE TO PUMP CHANGE OVER
ANALYSIS OF PROBLEM
USING 4W 1H
32
Copy of log sheet
on 01/10/2017
when pump was
changed over for
oil top up in
Boiler Feed Pump
2A
33
STEP-5: IDENTIFICATION OF CAUSES
Oil Topping is split into the following Activities
1. Applying Line Clear 5min
2. Getting approval from CGM 15min
3. Pump changeover 30min
4. Issuing Line Clear 5min
5. Opening the top up lid 5min
6. Topping up Oil 20min
7. Closing the Lid 5min
8. Returning Line Clear 5min
TOTAL TIME TAKEN FOR OIL TOPPING
UP IS 90 MIN.
34
STEP-5: IDENTIFICATION OF CAUSES
TOTAL TIME TAKEN
FOR OIL TOPPING UP 90 MIN.
PROCEDURAL DEALY 60min
PROCESS DELAY 10min
PROCESS 20min
PEOPLE3535
STEP-5: CAUSE & EFFECT ANALYSIS
EFFECT
DELAY IN OIL
TOPPING UPCAUSES
APPLY LINE CLEAR
MANUAL TOP UP
HIGH SPEED MACHINE
OPEN LID MANUALLY
CLOSE LID MANUALLY
4 P Analysis
INTIMATION TO CGM THROUGH PROPER CHANNEL
PUMP CHANGE OVER
PLANT
POLICIES PROCEDURES
SAFETY PROCEDURES
CLOSE LINE CLEAR
36
STEP-6: FINDING OUT THE ROOT CAUSE
WHY
WHY
WHY THERE IS DELAY IN OIL TOP UP IN BFP
LINE CLEAR TO BE OBTAINED
WHY LINE CLEAR TO BE OBTAINED
THE PUMP WILL NOT BE AVAILABLE FOR SERVICE WHILE
TOPPING UP OIL
37
STEP-6: FINDING OUT THE ROOT CAUSE
WHY
WHY
PUMP SHOULD NOT BE STARTED DURING OIL TOP UP
THERE IS NO PROVISION FOR OIL TOP IN A RUNNING PUMP.
WHY THE PUMP WILL NOT BE AVAILABLE
WHY THE PUMP SHOULD NOT BE STARTED
38
STEP-7: DATA ANALYSIS
38
Delay due to
Administrative Procedures 15min
Line clear 15min
Pump Changeover 30min
Maintenance Procedure 10min
PARETO DIAGRAM
80/20 LINE
100
90
80
70
60
50
40
30
20
10
0
PE
RC
EN
TA
GE
X
CAUSE
PUMP C/O ADMIN LINE
CLEAR
22
42
BEFORE MODIFICATION
Y
1
22 14
MTCE
40
STEP-7: DATA ANALYSIS
40
During Pump Change Over
For 30 min all the three BFPs will be in
service resulting in higher auxiliary power
consumption
41
STEP-7: DATA ANALYSIS
Power consumption for 30 min
Considering an average Amps as 190A during
the pump change over, the power consumed
for 30 min is
190 A*30/60 Hr*6.6KV*1.732*0.85
=1085 Kw Hr
42
STEP-7: DATA ANALYSIS
Power consumption for 30 min
On an average there is one oil top up in every
two months in each pump.
There are 21 BFPs
Power consumption for 21 pumps/Year
1085 *6*21=1,36,710 Kw Hr
REGULAR TOP UP OILIN RESERVE PUMP
PERMISSION FROM
CGM OBTAINED.LC
NEED NOT BE APPLIED.
OBTAINING
PERMISSION FROM
CGM IS REDUNTENT
FABRICATE A METHOD
FOR ONLINE TOP UP
OF OIL.
4343
STEP-8: DEVELOPMENT OF SOLUTION
44
STEP-8: DEVELOPMENT OF SOLUTION
44
ALTERNATIVESOLUTION REMARKS RESULT
ALT 1. REGULAR TOP UP OIL IN RESERVE PUMP
IN STOPPED CONDITION OIL LEVEL WILL BE HIGH
NOT ACCEPTED
ALT 2.PERMISSION FROM CGM OBTAINED.LC NEED NOT BE APPLIED
SAFETY PROCEDURE CANNOT BE BY-PASSED
NOT ACCEPTED
ALT 3.OBTAINING PERMISSION FROM CGM IS REDUNTENT
ADMINISTRATIVE PROCEDURE. CANNOT BE BYPASSED.
NOT ACCEPTED
ALT 4.
DESIGN A METHOD FOR ONLINE TOP UP OF OIL. FEASIBLE
ACCEPTEDAccepted
4545
ECT CHART
S.No OPTIONS EFFECT COST TIME PRIORITY
1 REGULAR TOP UP OIL INRESERVE PUMP
NOT GOOD
VERY HIGH MORE 2
2 PERMISSION FROM CGM OBTAINED.LC NEED NOT BE APPLIED
NOT GOOD
NIL MORE -
3 OBTAINING PERMISSION
FROM CGM IS REDUNTENT
NOTGOOD
NIL MORE -
4 DESIGN A METHOD FOR
ONLINE TOP UP OF OIL.
VERY GOOD
LESS LESS 1
STEP-8: DEVELOPMENT OF SOLUTION
46
STEP-9: FORESEEN PROBABLE RESISTANCE
46
S.No.
FORESEEING PROBLEM
ACTION
1 Approval by HOD QC members explained the reason behind the
modification and the benefits Obtained a positive reply
from HOD.
2 Procurement of
required Materials.
The required 1 inch pipe and bend is readily available.
3 Process affected Operation division was briefed about the advantages and
they immediately agreed for the modification. The
modification can be carried out during shut down of the
unit.
4 Approval by HOD Operation Division
Turbine Operation HOD was briefed and he readily agreed
5 Approval of top
management
The whole data were presented and explained to top
management and the advantages were briefed. After going
thro the ground work done by the team the top
management got convinced that this will work and readily
agreed.
4747
DECIDED TO ERECT AN AIRVENT OVER THE TOP UP LID
AGREED
MOBILIZATION OF MATERIALS TO SITE
ERECTION DURING SHUT DOWN
BEARING TEMP NORMAL AND
NO OIL LEAKCHECK FOR ANY
LEAK WHILE TOP UPIMPLEMENT
MODIFY THE LINES
TO DISCUSS WITH DIVISION HEAD
STOP
NOT AGREED
CHECK
STEP-10: TRIAL IMPLEMENTATION PDPC CHART
48
STEP-10: TRIAL IMPLEMENTATION P-D-C-A CYCLE
PLAN
Proposed to erect an air vent on the top up lid.
Required materials were collected
RESPONSIBILITY :- MR. Sameer & MR. Pavadai
TIME SCHEDULE :- START DATE : 10.04.18;
COMPLETION DATE: 01.05.18
DO
Modification carried out in BFP 2A.
RESPONSIBILITY :- MR. Sameer & MR. Pavadai
TIME SCHEDULE :- DATE; 02.05.2018 ;
ACTIONThe performance was found good. Hence the modification was .
Carried out in BFP2B & BFP2C.Continuous feedback is
being collected through operation division. It was decided to
study the performance & implement in other BFPs
RESPONSIBILITY : MR. Narayanan & Sameer
TIME SCHEDULE : START DATE: 01.06.18 ;
PROPOSED COMPLETION DATE: 31.08.18
4949
CHECK
Oil top up done by connecting the delivery hose of the hand pump
to the air vent. No leak observed while topping up when the pump
is in service.
RESPONSIBILITY : MR. Narayanan & Sameer
TIME SCHEDULE :- DATE : 31.05.2018 ;
STEP-10: TRIAL IMPLEMENTATION P-D-C-A CYCLE
5050
A P
DC
Modification carried
out in BFP 2A.
On 02.05.2018
Oil top up done by
connecting the delivery
hose of the hand pump
to the air vent when the
pump is in service
on 31.05.2018. No
leak observed
while topping
up.
DOCHECK
STEP-10: TRIAL IMPLEMENTATION
Proposed to erect
an air vent on the
lid. Required
materials were
collected by
01.05.2018
The performance
was found
good. Hence the
modification was
Carried out in
BFP2B & BFP 2C.
It was decided to
implement in
other BFPs
.
51
STEP-10: TRIAL IMPLEMENTATION
Modification wascarried out inBFP 2A. Oil topup done byconnecting thedelivery hose ofthe hand pump tothe air vent.
Modificationwas completedon 02.05.2018
No leakobserved whiletopping up oil.
51
ONLINE OIL TOPPING UP
52
• The performance was found good. Hence the
modification was Carried out in BFP2B & BFP2C.
• Continuous feedback is being collected through
operation division.
• The modification was carried out in other BFPs also.
5353
STEP-11: REGULAR IMPLEMENTATION
Oil was topped up in the BFPs where modification was carried out keeping
the pump in service. There was no problem in oil top up.
5454
L
QC members with their excellent dedication & team work is continuously
monitoring the oil levels in boiler feed pumps and implementing the new
modified methoed of oil topping up whenever necessary
STEP-12: FOLLOW UP & REVIEW
55
STEP-12: FOLLOW UP & REVIEW
MILE STONE CHART FOR
ACTION PLAN
5656
STEP ACTIVITY MONTH
OC
T
2017
NO
V
2017
DE
C
2017
JA
N
2018
JF
EB
2018
MA
R
2018
AP
R
2018
MA
Y
2018
JU
N
2018
JU
L
2018
AU
G
2018
SE
P
2017
1 Definition of problem
2 Analysis of problem
3 Cause and effect diagram
4 Root cause analysis
5 Data analysis
6 Development of solution
7 Foreseen probable resistance
8 Trial implementation
9 Completion in all Pumps
Starting Date: 01.10.2017 Ending date: 31.08.2018
Note : Follow-up and review is a continuous process
☺ No Pump change over required. Oil can be topped up even if the
pump is running.
☺ There is a power saving of 1085 units Per oil top up
☺ Selling cost / unit is Rs3.375
☺ Cost saving per oil top up is approximately equal to Rs 3660 /-
☺ Cost saving per annum Rs 4,61,400
5757
STEP-12: FOLLOW UP & REVIEW
☺ Pump change over is not required.
☺ Safe oil top up
☺ No delay in oil top up. Oil can be topped up evenif the pump is in service.
☺ Line Clear not required. Work permit is enough.
☺ Reliable operation is ensured
☺ Avoids frustration to operating Engineers
☺ Improved self confidence
☺ Pride over own modification work
58
STEP-12: FOLLOW UP & REVIEW
59
STEP-12: FOLLOW UP & REVIEWPAY BACK PERIOD
1/2 meter pipe (used) = 500.00
Labor cost for modification = 1,000.00
Labour cost for testing = 1,000.00
TOTAL COST OF MODIFICATION = 2,500.00
PAY BACK PERIOD = IMMEDIATE
59
COST OF MODIFICATION
6060
AA CHART
ACHIEVEMENT
BY PROVIDING AN AIR VENT OIL CAN BE
TOPPED UP IN A RUNNING PUMP.THE AIM
IS ACHIEVED.
AIM
TO TOP OIL WITHOUT
DELAY AND WITHOUT
STOPPING THE PUMP.
QC TEAM TARGET ACHIEVED
61
STEP-12: FOLLOW UP & REVIEWRECURRENCE PREVENTION
61
After modification, Regular feed back is beingcollected from operating engineers.
CONCLUSION
BY SUCCESSFULLY INTRODUCING AN AIR VENT
SAFE OIL TOP UP IS ACHIEVED. THE PROBLEM OF
PUMP CHANGE OVER IS ELIMINATED. THE QC
TEAM’S TARGET WAS ACHIEVED.
626262
Our sincere Thanks to
Turbine operation & services division
63
6464
65