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EMEREGNCY HANDLING PROCEDURES FOR
HCU/DHT-IV
MAJOR LEAK/FIRE IN HP REACTION SECTION
BY
D I L I P
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December 10, 1991
North Rhine, Westphalia, Germany
A pipe failure in the T-junctions area of an air cooler in thehigh pressure section of the HCU resulted in a release of HC
and H2, which subsequently ignited.
Reason
-severe corrosion/erosion in pipeline
Result
- A substantial part of unit was destroyed by the
explosion and subsequent fire.
-HCU was shut down for approx. seven months with
loss of nearly $90,000,000
WHY TO BE DISCUSSED?
Reference-The 100 Largest Losses 1972-2001
Large Property Damage Losses in the Hydrocarbon-Chemical Industries.MARSH-Property Risk Consulting
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This may be the result
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This may be the result
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Corrosion
Erosion
Mechanical failure of equipment/instrument/
lines
De chocking of Low Point Drains (LPDs)
Leaks may take place by
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WHY TO BE DISCUSSED?
A leak in the HP system-A serious emergency ,
requires immediate action to prevent harm topersonnel and equipment.
The first moves- Dont panic ,Be decisive and actpromptly.
In case of leak in the HP reaction system, theentire high pressure system will start todepressurise through the leak. These escapinggases can provide fuel for a serious fire.
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Normal Operation Fire/leak
Reactor Heater Fires Watch Stop
Make-up H2 Rate Watch Stop
Oil Feed Rate Watch Stop
System Pressure Watch Depressurize
Recycle Compressor Watch Maximum
Reactor Quench Watch Maximum
F/E Bypass Rate Watch MaximumSeparator CTL Valves Watch Watch
Injection Water Watch Stop
Action items...
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Immediate Actions
1. Depressurize the reactor loop by opening the
emergency depressuring valve.
2. Trip (extinguish) all furnace fires (main
burners and pilots).
3. Maximize quench to the reactor beds.
4. Stop all make-up hydrogen flow to the unit.
5. Maximize feed/effluent exchanger bypassrate.
Call Refinery Fire Dept. to respond to fire
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Immediate Actions
6. Continue recycle gas as long as possible to assist
cooling.
A. If recycle gas compressor is the source of the leak,
trip the machine and close the isolation valves.
Follow the procedure for loss of recycle gascompressor.
7. Close the feed control valves to the 1st,2nd stage
HCR & DHT reactors. Verify the chopper valvestrip closed.
8. Trip the reactor feed pumps -16-PA-CF-101/201A/B/301A/B
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Secondary Actions
9. Manually block in the fuel gas supply (pilot and
main burners),
Open air resister fully of each burners,
Stack damper to be kept full open
10. If possible (depending on the location of the emergency),
preparations should be made to operate one of
the MUG compressors on nitrogen.
11. If safe to do so, start emergency nitrogen to
the discharge of the RGC
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12. Monitor the liquid oil levels in the separators and carefully
control liquid levels to prevent blowing high pressure gasinto the low pressure system. Manually close level valveswhen levels go low.
13. Stop and secure water injection and amine systems.
14. Block in the fuel gas supply (pilot and main burners) to allfurnaces and admit snuffing steam into the fireboxes. (Incase of fire inside firebox)
15. If the leak has not been contained, maintain a nitrogenflow out of the leak to prevent pulling air into the system.
Secondary Actions
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ACCIDENTS IN HCU- CASE STUDIES-1
1-Major Reactor Runaway-Fatality at a U.S. Refining
Company
Background-Incident occurred in a
2ndstage reactor at a HCU
Refinery throughput -140 KBPD.
Reference-CLG seminar on hydro cracker
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Incident Summary
Temperature excursion began with a hot spot
in Bed 4 of a 5-bed reactor.
Hot spot most likely caused by poor flow andmisdistribution (cause unidentified).
Confusion was due to a variety of factors including:
Fluctuating temperature readings
Stopping of make-up flow to second stage
Misleading recycle H2 purity analysis
Absence of audible high temperature alarms after the
first high temperature occurrence
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Penal officers did not depressurize reactor when
temperatures exceeded maximum levels because theywere confused about whether an excursion was actually
occurring.
Penal officers were attempting to verify temperaturesin the reactor by having an person obtain temperaturereadings from the field panels under the reactors
Poor radio communications hampered relaying thesereadings to the control room.
Incident Summary (Contd)
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Even after reactor inlet temperatures were >
800F (4270
C), they did not depressurize. They didbegin to take steps to cool the reactor by increasingquench and reducing the heater outlet temperature.
Temperatures continued to rise out of control
while field person continued to verify fieldinstrumentation at the panel located at the bottomof the reactor
Unit was still not depressured!!Once temperature were in excess of 1400F(7600C), the reactor outlet piping ruptured causing amassive explosion and fire
Incident Summary (Contd)
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Incident Summary (Contd)
The person checking the field panel was killed.
46 Company and contract personnel were injured.
13 injured personnel were taken to the hospital,treated, and released.
Rx 3 4th and 5th bed
0
200
400
600800
1000
1200
1400
1600
7:33
:00
7:33
:40
7:34
:20
7:35
:00
7:35
:40
7:36
:20
7:37
:00
7:37
:40
7:38
:20
7:39
:00
7:39
:40
7:40:20
7:41:00
7:41:40
deg
F
Bed 4
outletBed 5
inletBed 5
outlet
Bed 5
OutletBed 5
outletBed 5
outletRx 3
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Incident Causes and Contributing Factors
Conditions to support and encourage employees to
operate reactors in a safe manner were inadequate.
Human factors were poorly considered in the design andoperation of the reactor temperature monitoring system.
Supervisory management was inadequate.Operational readiness and maintenance was inadequate.
Training and support was inadequate.
Procedures were outdated and incomplete.
Process Hazard Analysis was flawed.
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ACCIDENTS IN HCU- CASE STUDIES-2
2.Major Incident InvolvingPiping Failure and Fire at a
HCU.
Unit Overview
2 Stage Hydrocracker Unit
Running at maximum rate (~25KBPD)
Sequence of EventsInvestigation Findings
Lesson Learned
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Sequence of Events
Plant running normally at maximum feed and
ascending reactor profile.
Hydrogen make-up system started to sag.
Only token feed cuts made (1000 bbl and 500 bbl).
Recycle loop starts to sag.
Increased quenching robbed recycle hydrogen.
Reactors start to overheat, temperature waves start.Field team did opening and closing the F/E exchangerB/P
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Sequence of Events (Contd)
Furnace TCV going fully closed off
Reactor temperatures reached as high as 1200F(649C).
A small flange fire found and extinguished with a
steam ring on the reactor bottom.A second small fire was observed under the reactorat the bottom head.
Flame impingement on the quench piping causedthe piping to fail.
A large fire erupted and the unit was subsequentlyshutdown.
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Lessons Learned
The Panel officers should have moved more
aggressively in decreasing feed to stay within theavailable hydrogen make-up.
Operator moves were reactive rather thanproactive,
Once quenching proved ineffective to control bedtemperatures, temperature excursion proceduresshould have been executed.
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Unit Overview
60 KBPD 2-StageHydro cracking Unit
Running atmoderate rate (~45KBPD)
ACCIDENTS IN HCU- CASE STUDIES-3
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Sequence of Events
Plant running normally at moderate rates
2:25- H2S monitor alarmed
Vapor release observed
Called Refinery Fire Dept. to respond topotential fire
Sounded local evacuation in plant
Field team used SCBAs and set fire monitor onway out of unit
Plant emergency shutdown activated
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Sequence of Events (Contd)
2:28 - Deflagration of vapor cloud.
2:28 - Called in fire to Refinery Fire Dept.
Plant Protection and First Response Teamvolunteers respond.
2:30 - Refinery Fire Dept. called City Fire Dept. torespond.
~2:43 -Instrumentation lost to unit.
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First-StageLow Pressure
Separator
Second-Stage
Low Pressure
Separator
Power Recovery Turbine
(Was Out of Service at the Time)
To
Distillation
Section
Pressure Drop
Control Valve
Level Controller
Level Controller
- Valve That Failed
Simplified Flow Diagram of Immediate Area
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Isolation Block Valve on Pressure Drop Control ValveFrom Combined First-Stage and Second-StageEffluent Stream (From Low Pressure Separators) tothe Distillation Section Failed
Isolation Block Valve Bonnet
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Second-Stage Air Coolers
Location of Valve That Failed
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Damage at Field Work Center
Most of the crew was located in this building at the time of the
release
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Conduit runs for instrumentation and other electrical
equipment lasted approximately 15 minutes before collapse.
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Lessons Learned
Key items that led to safe shutdown and evacuation of
unit:
Training, Training, Training
Utilization of emergency shutdown devices
Sequential dump system utilized to depressure units
Make-up hydrogen choppers activated
Remote shutdowns of all feed pumps.
Site specific training of ALL personnel working in theunit, which included evacuation training.
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Lessons Learned (Contd)
One key item found is that this units EDS was set up to
fail closed on loss of electrical signal.
This caused the EDV system to close once the conduitrun failed.
Fireproofing needs to be evaluated on all emergencyshutdown devices (EBVs, EDVs, choppers, etc.)
ACCIDENTS IN HCU CASE STUDIES 4
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ACCIDENTS IN HCU- CASE STUDIES-4
A 2-inch line carrying hydrogen gas at 3,000 psi failed at aweld, resulting in a high pressure hydrogen fire.
The fire resulted in flame impingement on the calcium
silicate insulation of the skirt for a 100-foot high reactor in aHCU.
The steel skirt for this reactor, which was 10 to 12 feet in
diameter and had a wall thickness of seven inches,subsequently failed.
The falling reactor damaged air coolers and other process
equipment, greatly increasing the size of the loss
April 10, 1989
Richmond, California, United States
ACCIDENTS IN HCU CASE STUDIES 4
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At the time of the loss, the HCU was being shut down
for maintenance and the reactor was in a hydrogen
purge cycle.
Approx. 25 percent of the refinery throughput capacity,including the complete HCU production, was lost for a
period offive months.
Restoration of the hydro cracker itself required nearlytwo years.
ACCIDENTS IN HCU- CASE STUDIES-4
ACCIDENTS IN HCU CASE STUDIES 5
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The explosion was caused by the failure of a valve bonnetin a HP section of a 60,000 barrels-per-day HCU
A vapor cloud formed from the release, ignited, and was
followed by a large fire fed by escaping hydrocarbons athigh pressure.
The explosion resulted in the collapse of a large section of
pipe rack and destruction of a large fin fan cooler mounted
above the rack.
March 25, 1999
Richmond, California, United States
ACCIDENTS IN HCU- CASE STUDIES-5
ACCIDENTS IN HCU CASE STUDIES 5
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Many pumps were destroyed and a separator was
badly damaged.
Approximately 300 fire-fighters and 33 fire trucksparticipated in the two and a half hour effort to
control the fire.
Foam concentrate consumed totalled 3,200 gallons.
The hydro cracker was out of service for 12 months.
ACCIDENTS IN HCU- CASE STUDIES-5
ACCIDENTS IN HCU CASE STUDIES 6
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ACCIDENTS IN HCU- CASE STUDIES-6
January 27, 1997
Martinez, California, United States
At 7:41 p.m. an effluent line from a reactor in the HCUfailed , resulting in an explosion and fire.
Observation:Seconds before the explosion, a section of
the pipe was reported as glowing red.
Reason:The line apparently ruptured due to excessively
high temperatures, & the failure to depressurize the unit
upon detection of high temperature.
The hydrocarbons apparently auto-ignited shortly after
the initial release.
ACCIDENTS IN HCU CASE STUDIES 6
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ACCIDENTS IN HCU- CASE STUDIES-6
The rupture of the 12-inch effluent line was discovered on
a straight run of pipe, not at a weld.
Analysis of the failed section of pipe, at the point of
failure, indicated that the pipe had expanded in
circumference by approximately 5 inches. This caused a
localized bulge in the pipe prior to rupture
Loss:Approx.$80,000,000
ACCIDENTS IN HCU CASE STUDIES 7
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ACCIDENTS IN HCU- CASE STUDIES-7
October 8, 1992
Wilmington, California, United States
An explosion originating in the HCU occurred at 9:43 p.m.in this 75,000 barrels-per-day refinery
The explosion resulted from the rupture of a six-inch
carbon steel 90-degree elbow (outside radius) and releaseof a hydrocarbon/hydrogen mixture to the atmosphere.
The vapour cloud ignited within seconds after the rupture
at an undetermined point in the plant
ACCIDENTS IN HCU CASE STUDIES 7
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This explosion, which damaged nearby buildings &
shattered windows several miles away, was recorded as asonic boom at the California Institute of Technology
in Pasadena, approximately 20 miles from this 350-acre
refinery.
An inspection after the failure found the line at
nearly full design thickness a short distance away from the
failure.
ACCIDENTS IN HCU- CASE STUDIES-7
ACCIDENTS IN HCU CASE STUDIES 7
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On these facts, it was concluded that the line failure wasthe result of the thinning of the Schedule 120 carbon steel
elbow due to long term erosion/corrosion.
The fire was finally extinguished at 2:00 a.m. on October11.(Approx.52 hrs.)
Loss: $96,000,000
ACCIDENTS IN HCU- CASE STUDIES-7
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