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8/12/2019 TK13 LS Hydrate Study
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TK13 LS HydrateStudyTukau Subsurface Team
19 March 2013
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Agenda
Background
Input Data
Findings
Conclusion
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Background
General Tukau oil field located approx. 25km from offshore Lutong Sarawak.
Water depth : 160 ft
Operated under Baram Delta Operation (BDO).
Tukau Revisit Project
During drilling program under NAG
reservoir was discovered.
This NAG reservoir proves to be new
source to compliment gaslift injection.
TK-13 LS was completed to have the
flexibility to produce oil or gas upon
demand.
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PCSB Input Data
TK 46 RFT sample 1 dated 1982:
Reservoir condition; Pressure: 1766 psi, Temperature: 155F
Max CITHP: 1475 psi as recorded during unloading job.
FTH; Pressure: 1370 psi, Temperature: 104F
Ambient condition: Pressure: 14.7 psi, Temperature: 75.2F Sea bed condition: Max Temp: 80.6F, Min Temp: 65.8F
WellRFT
SampleDate
H2S_pp
mCO2 N2 C1 C2 C3 iC4 nC4 iC5 nC5 C6 C7+
TK-46 1 11/07/82 0 4.33 0.26 88.08 5.62 0.88 0.33 0.1 0.1 0 0.1 0.3
TK-46 2 11/07/82 0 3.13 0.53 89.69 4.72 0.91 0.42 0.1 0.1 0 0.3 0.1
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Input Data Comparison
TECHNIP Tukau Actual
Condition
Remarks
P (psia) T (F) P (psia) T (F)
Reservoir 2500 95.06 1766 155
Ambient 14.7 75.2 14.7 75.2FTH 1516 85 1370 104 WTR during
unloading
Start up 1550 -49 1330 98 WTR during
unloading
Min Seabed 1447 68 65.84 69.28
Moderate Seabed 1263 77 - -
Max Seabed 1090 86 80.6 69.28
CITHP 1550 - 1475 - WTR during
unloading
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Findings
Plot shows variation of FTHP which is at hydratefree zone
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Plot shows variation of CITHP which is at hydrate
free zone
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Plot shows at different operational condition, hydrateformation is unlikely to happened.
Cond. P (psia) T(F)
Ambient 14.7 75.2
FTH 1370 104
Reservoir 1766 155
CITHP 1475 100
U/S 1370 104
Stat up D/S 150 60
Max seabed 69.3 80.6
Start up
(U/S) 1330 98
reservoirCITHP
FTH/US
ambientDS
Max seabed
Start up*
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Conclusion
No hydrate formation at Tukau 13 LS based on atFTHP.
No hydrate formation at Tukau 13 LS based on atCITHP.
No hydrate formation is expected at TK13 LS duringstart up.
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TK13 LS Hydrate Curve based on sample RFT 1
Hydrate zone
Hydrate free zone
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0
500
1000
1500
2000
2500
0 10 20 30 40 50 60 70 80
RFT 1
RFT 2
RFT 1 and RFT 2 matched
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Plot shows variation of pressure during stableproduction (5 MMscf/d) which is at hydrate free
zone
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D/S and U/S
Downstream 150 66 WTR during
unloading
Upstream 1370 104 WTR duringunloading
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-500
0
500
1000
1500
2000
2500
0 20 40 60 80 100 120 140 160 180 200
Pressure,
psia
Temperature,F
Hydrate Formation Curve for TK13 LS
Operational
Prosper
HWU
Phase envelope
FTH and
U/S
CITHP
Ambient
D/S
reservoir