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8/10/2019 Case Study on Bearing Failure
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BEARING FAILURE OF BITUMEN PUMP
13P14
EQPT NO : 13P14
MODEL/MAKE : M/S RUSSIAN
MECH. SEAL MAKE : M/S EPIL
MECH. SEAL TYPE : 1502-52 SPL
BEARING TYPE : 6216, 7414
SERVICE : BITUMEN
TEMPERATURE : 220deg C
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BEARING FAILURE OF BITUMEN PUMP
13P14
ASSEMBLY OF PUMP WAS DONE ON 22/7/2000, AFTERRECEIPT OF SEAL.
PUMP WAS STARTED ON 10/09/2000 AND PUMP THRUSTBEARING FAILED JUST AFTER 4 HOURS OF ITS RUN.
PUMP AGAIN SENT TO WORKSHOP AND ITS BEARINGSWERE REPLACED & SEAL FITTED AFTER CLEANING.
PUMP AGAIN SENT TO SITE AND STARTED ON 25/09/2KAND AFTER 3-4HRS OF ITS OPERATION, ITS THRUSTBEARINGS AGAIN FAILED.
PUMP AGAIN SENT TO WORKSHOP FOR BEARING
REPLACEMENT.
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BEARING FAILURE OF BITUMEN PUMP
13P14
OBSERVATION MADE AT WORKSHOP AFTEROPENING:
BOTH THE THRUST BEARINGS BRASS CAGES WERE
FOUND BROKEN AND ITS BALLS GOT DEFORMED.
ALL OTHER COMPONENTS OF PUMP AND SEAL WERE
FOUND INTACKED.
THERE WAS 10MM GAP FOUND ON OD OF RADIALBEARING AND ID OF BRG. HOUSING, RADIAL BEARINGWAS NOT RESTING AT ALL ON HOUSING.
ANALYSIS:
SLEEVING ON HOUSING WAS DONE ON RADIAL BEARINGPORTION , WHICH WAS CAME OUT WHILE REMOVAL OFBEARING FROM HOUSING. AS PUMP WAS KEPT OPENEDAT WORKSHOP FOR ALMOST 6MONTHS ,
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BEARING FAILURE OF BITUMEN PUMP
13P14
ANALYSIS:
SLEEVE WAS MISSED AND BOTH THE OCCASIONBEARING WAS FITTED WITHOUT SLEEVE. SINCE RADIALBEARING WAS NOT RESTING ON HOUSING TOTALRADIAL LOAD TRANSMITTED TO THRUST BEARINGS. ASTHRUST BEARINGS ARE DESIGNED FOR AXIAL LOADAND NOT FOR RADIAL LOAD , ITS WAS FAILEDIMMEDIATELY.
REPAIR /REPLACEMENT CARRIED OUT:
BEARING HOUSING WAS REPLACED WITH SPAREBEARING HOUSING AND BOTH THE BEARINGS WERE
REPLACED. NOW PUMP IS RUNNING NORMAL
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D M GE TO RET INER
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BEARING FAILURE OF BITUMEN PUMP13P14
8/10/2019 Case Study on Bearing Failure
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REPEATED BEARING FAILURE OF BARARI
PUMP 603P3
EQPT NO :603P3
MAKE :M/S KIRLOSKAR BROTHERSERVICE :TREATED EFFULENT
WATER (BOOSTER)
TEMPERATURE :AMBIENTBEARING :3311,6311
Past Failure Event:1996 -New pump provided in BARARI minor Pump
house for boosting up the fire water pressure.Pump is taking suction from discharge of603P2 pump.
16/10/96 -Thrust Bearing failed & oil seal damaged.
04/12/97 -Both the bearing (radial & thrust )damaged,wear ring loose.
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REPEATED BEARING FAILURE OF BARARI
PUMP 603P3
15/01/98 -Shaft key way damaged, welding & M/C done.19/06/98 -Sleeve damaged, gland leak, sleeve made in
workshop.10/06/99 -Thrust bearing seized & shaft damaged.25/10/99 -Both the radial & thrust bearing damaged.08/02/2000 -Bearing & oil seal damaged.both the bearing &
oil seal changed.06/03/2000 -Bearing & oil seal damagedObservation-
1. Bearing housing cover bush, provided for fixing ofoil Seal,found detached from cover and got rotated.2. Oil seal found damaged.3. Radial bearing races found rubbed against rollers4. Thrust bearing clearances increased.
5. Bearings got rotated and found loose on housing.
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REPEATED BEARING FAILURE OF BARARI
PUMP 603P3
09/05/2000 -Overhauling done, bearing Replaced.
24/05/2000 -Bearing damaged.Bearing housing supportplate replaced with thicker plate andperpendicularity maintained.
19/07/2000 -Bearing failed.Heavy love-joy couplingreplaced with lighter shim pack type coupling.
26/08/2000 -Bearing failed.Pump manufacturer M/sKirloskar Brother called and assembly done in
their presence.
18/09/2000 -Bearing failed.Elect.cabling checked, as motorwas tripping at high load.
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FL KING
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REPEATED BEARING FAILURE OF BARARI
PUMP 603P3
23/09/2000 -Bearing damaged.foundation boltswelding done.
10/10/2000 -Bearing failed. Foundation RCC
filling done, to strengthen thebase plate.
28/11/2000 -Bearing & oil seal damaged.Askedoperation to run the pump withfull opening of discharge valve.
08/01/2001 -Overhauling Done, bearing
changed.
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REPEATED BEARING FAILURE OF BARARI
PUMP 603P3
29/01/2001 -Pump bearing again failed.Impeller diameterchecked with the data folder of the pump andfound that impeller OD is 14mm higher thanthe rated diameter of the impeller
Impeller OD trimmed to required rateddiameter and pump was assembled withtrimmed impeller and new bearing.Now pump isrunning since 05/02/2001.
Cause of failure:Due to higher impeller diameter of the pump it wasdeveloping high axial thrust, which was causing repeated
thrust bearing failure of the pump.
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REPEATED BEARING FAILURE OFBARARI PUMP 603P3
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
EQPT. DETAIL :
Tag. No.. : 12P5S Column bottom pump Eqpt. type : Centrifugal pump
Make : M/S Sulzer pump (I) ltd.
Model : ZE-100-4500 Service : Short residue Working temp. : 380-400 Deg. C. Bearing - Thrust : 7312 BG 2 nos
- Radial : NU312 Capacity Rated : 200 m3/hr
Minimum : 90 m3/hr
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
PAST HISTORY AND CHAIN OF EVENTS:
Old Russian Pump 12P5S was replaced in year2000 revamp shutdown.
Pump 12P5S was attended due to bearing failure on 25/08/2000 andfollowing spares were replaced.a- Bearing 7312 (2nos) & NU 312 (1 no)b- Complete Mech. Seal .
Pump 12P5S was commissioned at 17.00hrs on 28/8/01.
At 19.00 hrs. pump bearing failed after a run of 2hrs. As perproduction log book Pumpbearing housing was found abnormally hot
& steam was coming out from CW out let line. Immediately pumpwas stopped & 12P5A was put on service.
Pump 12P5S was opened and sent to work shop for maintenance. thepump thrust and radial bearings were found badly damaged and
seized on shaft. The following spares were replaced.
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
a. Bearing 7312 (2nos) & NU 312 (1 no)b. Complete Mech. Seal .c. Pump Shaft.d. Bearing housing cover repaired
On 5/9/2001 at 9hrs pump was started and its bearings again failedat 1645hrs. event before failure of the pump bearing is as follows
as per production log book. Pump 12P5S started at 9hrs in presence of MLE. Informed to
SELE. Vibration checked by MLE and found normal at 9.15hrs.12P5A stopped.
12P5S tripped at 10.10hrs. motor bearing temperature is also high.
12P5A started again. 12P5S again started at 11.15hrs informed to MLE and SELE. 12P5A
also running. 12P5 stopped at 14.30hrs and the load checked from sub station
for 12P5A & 5S and found 250 & 260 A respectively. As per SELE
12P5S load not to be kept beyond 250Amp. So 12P5 restarted at15.00hrs. all the 3pumps kept running.
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
At 16.45hrs, 12P5S bearing housing found smoking,its lube oil
burnt out, oil cup was out and fumes were coming. Pumpstopped immediately in presence of SPNM(U). M/M & E/Mkept informed.
Observation
-Before opening of pump.
a)Lube oil was found burnt and having bearing wear particle.b)Coupling DBSE is found 190mm against 180mm.c)Coupling shims were found distorted and broken.d)Coupling spaces was found damaged.
-After opening at work shop.a)both the thrust and radial bearings are found damaged andseized with shaft ( identical to earlier failure).b)Shaft found 0.20mm bent at radial bearing seating.
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
c)Bearing cover labyrinth found rubbed with bearing inner race
got damaged.d)Mech. seal collar found rubbed with purge bush.e)Deep rubbing marks on Wear ring observed and clearance1.5mm and 1.0mm found in front & back respectively.
f)Throat bush clearance 1.0mm found.
g)Ovality of 0.05mm found in outer thrust bearing seating.
Repair replacement done.
1.All the thrust and radial bearing replaced with new one.
2.Bearing housing cover labyrinth repaired.
3.Bearing housing ovality removed and bearing center checked.4.Pump shaft replaced with new one.5.All the wear rings except case wear ring replaced and itsclearance maintained. Throat bush also replaced andclearance maintained.
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
6.Mech. Seal faces are lapped and reused as new bellow is
not available,7.New coupling is issued and hub boring is done, which is to bereplaced along with its spacers.
Suspected cause of failure:
Thrust bearing failure may be due to following reason.1.Lack of lubrication in housing.2.Excessive hydraulic thrust on bearings.3.Improper mounting of bearings.4.Improper loading of thrust bearing during operation.
Lack of lubrication in housing.The possibility of lack of lubrication is ruled out as afterfailure of bearing there was oil found in housing and it has runfor approx.7 hrs.
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
Excessive hydraulic thrust on bearings.
The pump is single stage and fitted with both side wear ringsand balancing holes and its clearances are also not abnormallyhigh, which can not create that much thrust load on bearing.However during starvation of pump thrust balancing of rotorwill be disturbed.
Improper mounting of bearings.As the pump has run for approx. 7hrs on load and no abnormalsound or vibration was observed. This possibility may be ruledout.
Improper loading of thrust bearing during operationDue to high Distance between shaft ends 190mm (DBSE)maintained, compared to recommended DBSE of 180mm,coupling will cause pulling of pump rotor in motor side, whichwill result in improper loading of outer thrust bearing.
REPEATED BEARING FAILURE OF VDU PUMP 12P5S
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REPEATED BEARING FAILURE OF VDU PUMP 12P5S
Improper loading of thrust bearing will cause sliding of rolling
elements. As sliding friction of bearing elements, will causehigh heat generation and continue rise in bearing temperatureand subsequent failure of thrust bearings. The failure ofthrust bearing will allow the pump rotor assembly moving inpump side and it will cause rubbing of cover, purge bush and
case wear ring.
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CCRU RGC TURBINE 15KT1
THRUST BEARING FAILURE
The Recycle Gas Compressor (15-K-1) of CRU is
driven by a back pressure type steam turbine.
EQPT. DETAIL :-TAG NO. : 15KT1
MAKE : EBARA JAPAN
MODEL : SBHEG4-4
SPEED : 7446 RPMTYPE OF BLADE : 4 STAGES CURTIS WHEEL
STEM INLET PR. : 60 KG/CM2
STEAM OUT LET PR. : 4 KG/CM2
CCRU RGC TURBINE 15KT1
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CCRU RGC TURBINE 15KT1
THRUST BEARING FAILURE
PAST HISTORY AND CHAIN OF EVENT ON 28-2-01, 15K1 COMPRESSOR TRIPPED ON HIGH AXIAL
DISPLACEMENT.
ON 28-2-01, 19.10HRS COMP. ROLLED AFTER CHECKING.TRIPPED AT 6000 RPM ON HIGH THRUST BEARING TEMP &AXIAL DISPLACEMENT.
AFTER ANALYSIS THE PROBLEM, DECIDED TO OPEN THETHRUST BEARING FOR CHECKING.
OBSERVATION THRUST PAD (ACT.SIDE) FOUND COMPLETELY WIPED OFF.
NO OTHER ABNORMALITY OBSERVED.
CCRU RGC TURBINE 15KT1
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CCRU RGC TURBINE 15KT1
THRUST BEARING FAILURE
REPAIR REPL. DONE ALL THE 6NOS ACTIVE SIDE THRUST PADS REPLACED.
COMPLETE LUBE OIL REPLACED AND FILTER CHANGED.
SOLO RUN OF TURBINE CHECKED.
TURBINE ROLLED ON 6-3-01 AND FOLLWINGPARAMETER WERE OBSERVED
AXIAL DISP. : 0.23/.19
TH. BEARING TEMP : 85,91,85OC
CHEST PR. : 25 KG/CM2
1STSTAGE PR. : 19 KG/CM2
FROM 1STWEEK OF MAY THESE READINGS HAVE STARTEDINCREASING WITH OUT ANY CHANGE IN OPERATING
PARAMETER
CCRU RGC TURBINE 1 KT1
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CCRU RGC TURBINE 15KT1
THRUST BEARING FAILURE
ON 29-6-01 TURBINE TRIPPED, DUE TO HIGHTHRUST BRG. TEMP. AND AXIAL THRUST. DECIDEDTO OPEN THE TURBINE.
OBSERVATION MADE AFTER OPENING:
THRUST(ACT.SIDE) FOUND DAMAGED. 3RD& 4THROW BLADES OF TURBINE FOUND 80% CHOCKED
DUE TO SEVERE SILICA DEPOSITION. DIAPHRAGM NOZZLES WERE FOUND ERODED.
REPAIR REPL. DONE ROTOR AND DIAPHRAGM OF TURBINE WERE CLEANED BY
HYDRO-SAND BLASTING . ERODED PORTION OF DIAPHRAGM NOZZLES WERE WELD
BUILD UP AND GRINDED OFF. ACTIVE SIDE THRUST BEARING REPLACED WITH NEW
ONE.
CCRU RGC TURBINE 15KT1
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CCRU RGC TURBINE 15KT1
THRUST BEARING FAILURE
AFTER REPAIR / REPLACEMENT TURBINE ROLLEDON 12-7-01 AND TURBINE IS RUNNING WITHFOLLOWING PARAMETER.
AXIAL DISP. : (-)0.02/(+).01TH.BEARING TEMP. : 50,51,53 DEG. CCHEST PR. : 21KG/CM2
1ST
STAGE PR. : 13 KG/CM2
THRUST BEARING FAILURE OF CCRU RGC
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THRUST BEARING FAILURE OF CCRU RGCTURBINE 15KT1
REASON OF REPEATED FAILURE OF THRUST BEARING:
Brief on Existing systemThe HP steam requirement of CRU RGC turbine (Ebaramake) is met partly from captive generation with thebalance (about 45%) thru import from TPS. The
turbine is designed for an inlet steam temperature of420oC @60 Kg/cm2g. However, the actual steamtemperature remains in the range of 360-370oC.
Reasons of failures
The rise in thrust bearing temperature and high axialdisplacement of turbine rotor were due to deposition onthe moving and static blades of the turbine.
The suspected reasons for metal erosion of turbinediaphragm nozzles is the supply of steam at lower
temperature and impurities present in it
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THRUST BEARING FAILURE OF CCRU RGC
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THRUST BEARING FAILURE OF CCRU RGCTURBINE 15KT1
a) Lab test on regular basis for DM water and BFWseparately to monitor silica concentration. This will alsohelp detection of possible contamination of condensatethrutube leaks of STG condensers.
b)
The exhaust at the turbine to be maintained at4.0+kg/cm2g on sustained basis to retard silica rejectionby steam. All the MP to LP PRDS are being checked forperformance so that LP steam header pressure is alwaysmaintained.
c) Action being initiated for providing improved insulationto ensure steam availability to RGC at design level.Steam generator at 15 F-1 of CRU are being lookedintofor ascertaining reasons for low superheat temperatureof steam generated.
THRUST BEARING FAILURE OF CCRU RGC
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THRUST BEARING FAILURE OF CCRU RGCTURBINE 15KT1
CHOKAGEOFBLADES EROSION ON DIAPHRAGM