63
AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE OF SEWAGE EFFLUENT AT THE MARINE CORPS AIR STATION KLIPPER GOLF COURSE . Steven Y.K. Chang Reginald H.F. Young Technical Memorandum Report No. 53 January 1977 Project Completion Report fur INVESTIGATION OF THE KANEOHE MARINE CORPS AIR STATION LAND DISPOSAL SYSTEM OWRT Project No. A-064-HI Grant Agreement No.: 14-34-0001-6012 Principal Investigator: Reginald H.F. Young Project Period: 1 July 1975 to 30 September 1976 The programs and activities described herein were supported in part by funds provided by the United States Department of the Interior as authorized under the Water Resources Act of 1964, Public Law 88-379; and the Water Resources Research Center, University of Hawaii. AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE OF SEWAGE EFFLUENT AT THE KANE'OHE MARINE CORPS AIR STATION KLIPPER GOLF COURSE by Steven Y.K. Chang Reginald H.F. Young Technical Memorandum Report No. 53 January 1977 Project Completion Report for INVESTIGATION OF THE KANEOHE MARINE CORPS AIR STATION LAND DISPOSAL SYSTEM OWRT Project No. A-064-HI Grant Agreement No.: 14-34-0001-6012 Principal Investigator: Reginald H.F. Young Project Period: 1 July 1975 to 30 September 1976 The programs and activities described herein were supported in part by funds provided by the United States Department of the Interior as authorized under the Water Resources Act of 1964, Public Law 88-379; and the Water Resources Research Center, University of Hawaii.

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Page 1: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF

REUSE OF SEWAGE EFFLUENT AT THE

KANE'OH~ MARINE CORPS AIR STATION KLIPPER GOLF COURSE

~

. Steven Y.K. ChangReginald H.F. Young

Technical Memorandum Report No. 53

January 1977

Project Completion Reportfur

INVESTIGATION OF THE KANEOHE MARINE CORPS AIR STATIONLAND DISPOSAL SYSTEM

OWRT Project No. A-064-HIGrant Agreement No.: 14-34-0001-6012

Principal Investigator: Reginald H.F. YoungProject Period: 1 July 1975 to 30 September 1976

The programs and activities described herein were supported in part by fundsprovided by the United States Department of the Interior as authorized underthe Water Resources Act of 1964, Public Law 88-379; and the Water ResourcesResearch Center, University of Hawaii.

AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF

REUSE OF SEWAGE EFFLUENT AT THE

KANE'OHE MARINE CORPS AIR STATION KLIPPER GOLF COURSE

by

Steven Y.K. ChangReginald H.F. Young

Technical Memorandum Report No. 53

January 1977

Project Completion Reportfor

INVESTIGATION OF THE KANEOHE MARINE CORPS AIR STATIONLAND DISPOSAL SYSTEM

OWRT Project No. A-064-HIGrant Agreement No.: 14-34-0001-6012

Principal Investigator: Reginald H.F. YoungProject Period: 1 July 1975 to 30 September 1976

The programs and activities described herein were supported in part by fundsprovided by the United States Department of the Interior as authorized underthe Water Resources Act of 1964, Public Law 88-379; and the Water ResourcesResearch Center, University of Hawaii.

Page 2: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …
Page 3: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

iii

ABSTRACT

An investigation of waste water reuse by spray irrigation was conducted

at the Kane 'ohe Marine Corps Air Station (KMCAS) Klipper Golf Course on Oahu.

The study was conducted in three phases: (l) waste water characterization of

the KMCAS Sewage Treatment Plant3 (2) groundwater quality analysis~ and (3)

air quality analysis of indicator bacterial levels during spray irrigation

with waste water.

Waste water analyses showed that the KMCAS Sewage Treatment Plant3 em­

ploying the trickling filter process with a final polishing pond3 is capable

of removing a high percentage of biodegradable substances and suspended sol­

ids.The effluent appears to be of good quality for agricultural irrigation

use. .High concentrations of sodium and chloride3 due to brackish groundwater

infiltration into the sewage system3 were not considered to be a hazard to

the salt-tolerant be~dagrass.

The two predominant soils on the KMCAS KUpper GoZfCourse.3 the Ewa sil­

ty clay loam (Low Humic Latosois) and the Jaucas (Regosols).3 appeared to be

very effective in removing nitrogen3 phosphorus3 and fecalcoliforms from the

applied effluent. The quality of the percolate does not present a hazard to

the groundwater quality. Runoff from the golf course does not present a haz­

qrd to the adjacent surface waters.

Analyses of spray irrigation fallout samples at the KMCAS Klipper Golf

Course resulted in the isolation of coliform bacteria up to 91 m (300 ft)

downwind of the sprinkler sources. Coliform bacteria recovery rates depended

upon the initial coliform bacterial concentrations in tne effluent and upon.

wind velocities. The presence and concentration of aerosolized coliform bac­

teria were not considered a public health hazard to golf course users3 workers.3

or nearby residents.

iii

ABSTRACT

An investigation of waste water reuse by spray irrigation was conducted

at the Kane 'ohe Marine Corps Air Station (KiVJCAS) KUpper Golf Course on Oahu.

The study was conducted in three phases: (l) waste water characterization of

the KMCAS Sewage Treatment Plant3 (2) groundWater quality analysis3 and (3)

air quality analysis of indicator bacterial levels during spray irrigation

with waste water.

Waste water analyses showed that the KMCAS Sewage Trea-tment Plant3 em­

ploying the trickling filter process with a final polishing pond3 is capable

of removing a high percentage of biodegradable substances and suspended sol­

ids. The effluent appears to be of good quality for agricultural irrigation

use. High concentrations of sodium and chloride3 due to brackish groundWater

infiltration into the sewage system3 were not considered to be a hazard to

the salt-tolerant bermudagrass.

The two predominant soils on the KMCAS KUpper Colf Course3 the Ewa sil­

ty clay loam (Low Humic Latosols) and the Jaucas (Regosols)3 appeared to be

very effective in removing nitrogen3 phosphorus3 and fecal coli forms from the

applied effluent. The quaZity of the percolate does not present a hazard to

the groundwater quality. Runoff from the golf course does not present a haz­

ard to the adjacent surface waters.

Analyses of spray irrigation fallout samples at the KMCAS Klipper Colf

Course resulted in the isolation of coliform hacteria up to 91 m (300 ft)

downwind of the sprinkZer sources. Coliform hacteria recovery rates depended

upon the initial coliform hacterial concentrations in the effluent and upon

wind velocities. The presence and concentration of aerosolized coliform hac­

teria were not considered a puhlic health hazard to golf course users3 workers3or nearby residents.

Page 4: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …
Page 5: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

v

CONTENTS

SAMPLING STATIONS AND FIELD METHODS .

RESULTS AND DISCUSSION..

Waste Water Characterization .Groundwater Quality..Ai r Qual ity. . . . .

Waste Water Characterization of the KMCAS Treatment Plant..Groundwater Qual ity. . . . ... . .. .Air Quality. . ...

1

3

6

6

B

11

14

14

2127

36

37

37

41

iii

'.

. . . .

CONCLUSIONS . . .

ACKNOWLEDGMENTS ..

REFERENCES.

APPENDICES.

ABSTRACT. . .

INTRODUCTI ON.

BACKGROUND STUDY.

FIGURES

. . . .. .

l.

2.

3.

4.5.

6.7.B.,

9.

10.

11.

12.

Kane'ohe Marine Corps Air Station, Mokapu Peninsula, Oahu.Location Map of the Sewage Treatment Plant .Sewage Treatment Pl ant Layout. . . . . .. .....Location Map of Test Well No.1 .Schematic Cross Sections of Test Well Nos. 1, 2, and 3 •Location Map of Test Well No.2 .Location Map of Test Well No.3 .Determined Downwind Azimuth for Air Sampling ....Air Sampling Configuration .Hourly Flow Pattern, KMCAS Sewage Treatment Plant.Klipper Golf Course and Groundwater Test Wells ..Coliform Bacteria Densities Downwind of Spray IrrigationSource . . . . . . . . . . . . . . . . . . . . . . . . . .

2

6

7

9

10

121315

16

lB23

31

CONTENTS

ABSTRACT. . .

INTRODUCTION.

BACKGROUND STUDY ..

SAMPLING STATIONS AND FIELD METHODSWaste Water Characterization .Groundwater Quality..Air Quality.....

RESULTS AND DISCUSSION..Waste Water Characterization of the KMCAS Treatment Plant.Groundwater Quality. ..Air Qual ity.

CONCLUSIONS . .

ACKNOWLEDGMENTS

REFERENCES.

APPENDICES.

FIGURES

v

1

3

6

6

8

11

14

14

21

27

36

37

37

41

l.

2.

3.

4.5.

6.

7.8.

9.

10.

ll.

12.

K~ne'ohe Marine Corps Air Station, M6kapu Peninsula, Oahu.Location Map of the Sewage Treatment Plant.Sewage Treatment Plant Layout .Location Map of Test Well No.1 .Schematic Cross Sections of Test Well Nos. 1, 2, and 3 .

Locati on Map of Test Well No.2. . . . . .Location Map of Test Well No.3•..•..

Determined Downwind Azimuth for Air Sampling ..Air Sampling Configuration .Hourly Flow Pattern, KMCAS Sewage Treatment Plant ..Klipper Golf Course and Groundwater Test Wells ..Coliform Bacteria Densities Downwind of Spray IrrigationSource . . . . . . . . . . . . . . . . . . . . . . . . . .

2

6

7

9

10

1213

15

1618

23

31

Page 6: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

vi

13. Coliform Bacteria Densities Downwind of Spray IrrigationSource. · · · · · · · · · · . . . . · · · . . . · · · 31

14. Coliform Bacteria Densiti es Downwind of Spray IrrigationSource. · · · · · · · · · · . . . . · · . . · · . . . · · · 32

15. Coliform Bacteria Densiti es Downwind of Spray IrrigationSource. · · · · · · · · · · · · . . · 32

16. Normalized Air Quality Data for No. 2 Green · · · · · . 3317. Normalized Air Quality Data for No. 15 Green. · · · · . 33

18. Normalized Air Quality Data for No. 16 Green. · 34

19. Normalized Air Quality Data for Putting Green · 34

TABLES

5.

8.

6.

7.

24

30

19

19

21

30

25

29

25

26

l.

2.

3.4;

IWaste Water Analyses of Treatment Plant Efficiencies. . ...Suspended Solids Removal in the KMCAS STP Polishing Pond ..Runoff Analysis, 6 February 1976........•....•

Mean Constituent Concentration Changes between KMCAS STPPond Effluent and Klipper Golf Course Sprinkler Effluent.Mean Constituent Concentration Change Between Test WellNos. 1 and 3 Groundwater Samples•.............Mean Constituent Concentration Change of Effluent throughLow Humic Latosols on the KMCAS Golf Course. . . • . . .. ..Mean Constituent Concentration Change of Applied Effluentthrough Jaucas Sands (Test Well No.2) on the KMCAS GolfCourse. . . ... . . . . . . . . . . . . '.' . . ....Meteorological, Environmental, and BacteriologicalConditions during Air Sampling on the KMCAS KlipperGolf Course ........•...... ; .... ~ .•....

9. Air Sampling Results of Aerosolized Coliform BacteriaCollected at the KMCAS Klipper Golf Course.Normalized Data for the Air Sampling at the KMCAS KlipperGolf Course ..............•...•.....

10.

vi

13. Coliform Bacteria Densities Downwind of Spray IrrigationSource. · · · · · · · · · . . . · · · . . . . . . . . . 31

14. Coliform Bacteria Densities Downwind of Spray IrrigationSource. · · · · · · . · · · . . . . · · · . . . . . . . . . 32

15. Coliform Bacteria Densiti es Downwind of Spray IrrigationSource. · · · · · · . · · · · · . . . 32

16. Normalized Air Quality Data for No. 2 Green . · 33

17. Normalized Air Quality Data for No. 15 Green. · 33

18. Normalized Air Quality Data for No. 16 Green. 3419. Normalized Air Quality Data for Putting Green 34

TABLES

l.

2.

3.

4.

5.

6.

7 .

8.

9.

10.

I

Waste Water Analyses of Treatment Plant Efficiencies ....Suspended Solids Removal in the KMCAS STP Polishing Pond.Runoff Analysis, 6 February 1976 .Mean Constituent Concentration Changes between KMCAS STPPond Effluent and Klipper Golf Course Sprinkler Effluent.Mean Constituent Concentration Change Between Test WellNos. 1 and 3 Groundwater Samples .Mean Constituent Concentration Change of Effluent throughLow Humi c La toso1s on the KMCAS Golf Course . . . . . . . . . . .I~ean Constituent Concentration Change of Applied Effluentthrough Jaucas Sands (Test Well No.2) on the KMCAS GolfCourse. . . . . . . . . . . . . . . . . . . . . . .Meteorological, Environmental, and BacteriologicalConditions during Air Sampling on the KMCAS KlipperGo1f Course . . . . . . . . . . . . . . . . . . . . • . • . . . .Air Sampling Results of Aerosolized Coliform BacteriaCollected at the KMCAS Klipper Golf Course.Normalized Data for the Air Sampling at the KMCAS KlipperGo1f Course . . . . . . . . . . . . . . . . . • . . . . . . . . .

19

19

21

24

25

25

26

29

30

30

Page 7: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

INTRODUCTION

The Kane'ohe Marine Corps Air Station (KMCAS) is located on the M6kapuPeninsula, adj acent to the Class "AA'I coastal waters of Kane' ohe Bay (Fig. 1).The Hawaii State Department of Health (1974, chaps. 37-A, 38) restricts thedisposal of point pollution into coastal waters classified "AN'. The lGJICASSewage Treatment Plant (STP) presently disposes its effluent irito Kane'oheBay, near the KMCAS small boat harbor (Class "B" waters). However, the KMCASSTP will be redirecting its sewage effluent to the City and County ofHonolulu's M6kapu Outfall (presently under construction) located outsideKailua Bay. The ~lCAS will be assessed a service charge for the use andmaintenance of the Mokapu Outfall.

The Air Station has sought an alternative for the disposal of its wastewaters because of the restrictions on the disposal of wastewaters intoKane'ohe Bay and the future service charges for the use of the M6kapu Outfall.Since June 1973, the KMCAS has been irrigating the base golf course with aportion of its secondary treatment plant effluent. Between 29 and 93% of theplant's effluent daily flow has been utilized for the Klipper Golf Courseirrigation during a year. Approximately 1,060 m3 (280,000 gal) of freshwater is saved each day due to the irrigation practice~

During the past two decades, there have been numerous studies on wastewater reuse for various applications in industrial, recreational, and agri­cultural products for human consumption. The reuse of waste waters can be analternative to the expensive advanced waste treatment facilities that may berequired by 1 July 1983 to satisfy the requirements of Public Law 92-500(u.S. Congress 1972). However, the disposal of waste waters through an irri­gation system must be examined to determine if any adverse environmentaleffects can occur. The reuse of waste water for the irrigation of a recrea­tional facility, such as the Klipper Golf Course, must be carefully evaluatedto assure the public health safety.

The purpose of this study was to determine the effects of waste waterreuse on groundwater and air quality at the Kane'ohe Marine Corps Air StationKlipper Golf Course. Specifically, the investigation \vas to determine theremoval of some selected chemical and biological pollutants from waste waterpercolating through the soils on the golf course and the presence of aero­solized organisms dispersed into the air by spray irrigation practices.

INTRODUCTION

The Kane'ohe Marine Corps Air Station (KMCAS) is located on the M6kapu

Peninsula, adj acent to the Class "AA'I coastal waters of Kane' ohe Bay (Fig. 1).

The Hawaii State Department of Health (1974, chaps ..37-A, 38) restricts the

disposal of point pollution into coastal waters classified "AN'. The KMCAS

Sewage Treatment Plant (STP) presently disposes its effluent into Kane'ohe

Bay, near the KMCAS small boat harbor (Class "B" waters). However, the KMCAS

STP will be redirecting its sewage effluent to the City and County of

Honolulu's M6kapu Outfall (presently under construction) located outside

Kailua Bay. The KMCAS will be assessed a service charge for the use and

maintenance of the M6kapu Outfall.

The Air Station has sought an alternative for the disposal of its waste

waters because of the restrictions on the disposal of wastewaters into

Kane'ohe Bay and the future service charges for the use of the MBkapu Outfall.

Since June 1973, the KMCAS has been irrigating the base golf course with a

portion of its secondary treatment plant effluent. Between 29 and 93% of the

plant's effluent daily flow has been utilized for the Klipper Golf Course

irrigation during a year. Approximately 1,060 m3 (280,000 gal) of fresh

water is saved each day due to the irrigation practice.

During the past two decades, there have been numerous studies on waste

water reuse for various applications in industrial, recreational, and agri­

cultural products for human consumption. The reuse of waste waters can be an

alternative to the expensive advanced waste treatment facilities that may be

required by 1 July 1983 to satisfy the requirements of Public Law 92-500

(u.s. Congress 1972). However, the disposal of waste waters through an irri­

gation system must be examined to determine if any adverse environmental

effects can occur. The reuse of waste water for the irrigation of a recrea­

tional facility, such as the Klipper Golf Course, must be carefully evaluated

to assure the public health safety.

The purpose of this study was to determine the effects of waste water

reuse on groundwater and air quality at the Kane'ohe Marine Corps Air Station

Klipper Golf Course. Specifically, the investigation was to determine the

removal of some selected chemical and biological pollutants from waste water

percolating through the soils on the golf course and the presence of aero­

solized organisms dispersed into the air by spray irrigation practices.

Page 8: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

N

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PI.

N j

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kapu

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::::::::::::;::::::.««:} I.:-:-:-:-:.:-:-:.:-:.................... I.............................

-::::::::::::::::::1 11111

. .

MOKAPU

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Klineohe Bay

oIo

III1I11111 Kl i pper Go 1f Course

...... Hi 1ita ry Hous i ng::::::::::::

FIGURE 1. KANE'OHE MARINE CORPS AIR STATION, HOKAPU PENINSULA, OAHU

Page 9: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

3

Research in this study was done in three phases: waste water character­

ization, grotmdwater quality analysis, and air quality analyses. The waste

water characterization of the KMCAS STP was used to determine the quality of

the applied sewage effluent on the golf course. Parameters for monitoring

the waste water quality included, temperature, dissolved oxygen, pH, biochem­

ical oxygen demand, suspended solids, total dissolved solids, nitrogen (ammo­

nia, organic, nitrate and nitrite), phosphorus, sodium, potassium, chloride,

sulfate, and total and fecal coliform bacteria. The groundwater quality be­

low the Klipper Golf course was monitored to determine the effects of the

waste water reuse. The parameters for observing the movement of sewage ef­

fluent through the two predominant soils (Ewa silty clay loam and Jaucus

sand) included, temperature, pH, dissolved oxygen, nitrogen (ammonia, organ­

ic, ili trate and nitrite) ,phosphorus, sodium, potassium, chlo:I-lde, and fecal

coliform bacteria. Parameters for the monitoring of air quality, during the

spray irrigation of the golf course, included, temperature, relative humidi­

ty, wind velocity and direction, and total coliform and fecal coliform bac­

teria.

BACKGROUND STUDY

The reuse of man's waste water has been practiced in the United States

for at least 75 years. Municipalities and industries in the arid and semi­

arid areas of the western United States have pioneered reuse systems (Merz

1956). Today, waste waters are being reused inindustry~ agriculture, and

recreation. This reuse provides a practical alternative and method for the

disposal of waste waters as well as a supplement to our freshwater demands.

In an agronomic sense, waste waters can provide irrigation water of agricul­

tural value for plant crops and recreational areas. In the past, the dis­

posal of waste waters was often considered a major problem. Now, waste

waters can be considered as an asset, a recovered resource, when applied

through a reuse system.

The reuse of sewage in the state of Hawaii extends back at least 50

years but no documentation has been available on past or most present systems.

Various sugar companies located in Wailua and Waimea on Kaua'i and Lahaina on

Maui,have indirectly used sewage. Waste waters from th.e plantation. housing

were emptied into nearby ditches. The diluted sewage eventually was stored

3

Research in this study was done in three phases: waste water character­

ization, groundwater quality analysis, and air quality analyses. The waste

water characterization of the n1CAS STP was used to determine the quality of

the applied sewage effluent on the golf course. Parameters for monitoring

the waste water quality included, temperature, dissolved oxygen, pH, biochem­

ical oxygen demand, suspended solids, total dissolved solids, nitrogen (ammo­

nia, organic, nitrate and nitrite), phosphorus, sodium, potassium, chloride,

sulfate, and total and fecal coliform bacteria. The groundwater quality be­

low the Klipper Golf course was monitored to determine the effects of the

waste water reuse. The parameters for observing the movement of sewage ef­

fluent through the two predominant soils (Ewa silty clay loam and Jaucus

sand) included, temperature, pH, dissolved oxygen, nitrogen (ammonia, organ­

ic, nitrate and nitrite), phosphorus, sodium, potassium, chloride, and fecal

coliform bacteria. Parameters for the monitoring of air quality, during the

spray irrigation of the golf course, included, temperature, relative humidi­

ty, wind velocity and direction, and total coliform and fecal coliform bac­

teria.

BACKGROUND STUDY

The reuse of man's waste water has been practiced in the United States

for at least 75 years. Municipalities and industries in the arid and semi­

arid areas of the western United States have pioneered reuse systems (Merz

1956). Today, waste waters are being reused in industry, agriculture, and

recreation. This reuse provides a practical alternative and method for the

disposal of waste waters as well as a supplement to our freshwater demands.

In an agronomic sense, waste waters can provide irrigation water of agricul­

tural value for plant crops and recreational areas. In the past, the dis­

posal of waste waters was often considered a major problem. Now, waste

waters can be considered as an asset, a recovered resource, when applied

through a reuse system.

The reuse of sewage in the state of Hawaii extends back at least 50

years but no documentation has been available on past or most present systems.

Various sugar companies located in Wailua and Waimea on Kaua I i and Lahaina on

Maui,have indirectly used sewage. Waste waters from the plantation housing

were emptied into nearby ditches. The diluted sewage eventually was stored

Page 10: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

4

in a reservoir and used for the irrigation of sugarcane. This practice of

sewage disposal has probably been used by most of the sugar companies in the

past. 1

Sewage effluents for irrigation have been used at the Royal Ka'anapali

Golf Course on Maui and at a baseball park in Kailua, Kona on Hawaii. 2 Since

1969, the Makaha Nursery on Oahu has obtained septic tank effluent from the

Makaha Inn on Oahu. 3 In 1972, use of oxidation pond effluent as a partial

supplement for golf course irrigation began at the Kuilima Hotel on Oahu. 4

At the Kane'ohe Marine Corps Air Station Klipper Golf Course, use of the

trickling filter effluent frOTII the station waste water-treatment plant for

irrigation began in 1973. 5 Activated silldge effluent has been used at the

Hawaii-Kai Golf Course on Oahu since 1973. s

The increasing reuse of waste water -for agricultural and recreational

activities has resulted in many studies on the movement of chemical and bio­

logical pollutants through soils. The high removal of various forms of ni­

trogen in percolating waters through soils has been observed by many inves­

tigators (McMichael and McKee 1966; Bouwer, Lance, and Riggs 1974; Lau et al.

1975). However, this removal is often due to the conversion from one form

to another. The disappearance of ammonium ion from percolating systems can

be partially attributed to oxidation by nitrifying bacteria. Adsorption by

clays retains anunonium ions, but this is not necessarily a stable condition

because biological oxidation can occur (Lance 1972). This oxidation is mere­

ly a conversion of anunoniuni ion to nitrates. The actual removal of nitrogen

from a soil system can be obtained by the reduction of nitrates to nitrogen

gas by biological denitrification and the removal of plant tissue from the

soil system after plant uptake of the nitrate.

A high removal of phosphorus from percolating waters has been observed

in clays. The immobility of phosphorus is attributed to the adsorptive ca­

pacity of soils (Taylor 1967). The latosol soils of Hawaii have a high fix­

ing capacity for phosphorus (Fox 1972; Chu and Sherman 1952; Coleman 1944).

In some areas, the soil competes with plants for the available phosphorus.

Very little movement of adsorbed phosphorus has been observed over a period

IDr. Paul C. Ekern 1975: personal communication.2 Dennis Lau 1976: personal communication.3Makaha Nursery caretaker 1976:, personal cOTIlffiunication.4Herbert Hirota 1976: personal communication.5Melvyn A. Yoshinaga 1975: personal communication.6Herbert Yamaguchi 1976: personal communication ..

4

in a reservoir and used for the irrigation of sugarcane. This practice of

sewage disposal has probably been used by most of the sugar companies in the

past. 1

Sewage effluents for irrigation have been used at the Royal Ka'anapali

Golf Course on Maui and at a baseball park in Kailua, Kona on Hawaii. 2 Since

1969, the Makaha Nursery on Oahu has obtained septic tank effluent from the

Makaha Inn on Oahu. 3 In 1972, use of oxidation pond effluent as a partial

supplement for golf course irrigation began at the Kuilima Hotel on Oahu. ~

At the Kane'ohe Marine Corps Air Station Klipper Golf Course, use of the

trickling filter effluent from the station waste water treatment plant for

irrigation began in 1973. 5 Activated sludge effluent has been used at the

Hawaii-Kai Golf Course on Oahu since 1973. 6

The increasing reuse of waste water -for agricultural and recreational

activities has resulted in many studies on the movement of chemical and bio­

logical pollutants through soils. The high removal of various forms of ni­

trogen in percolating waters through soils has been observed by many inves­

tigators (McMichael and McKee 1966; Bouwer, Lance, and Riggs 1974; Lau et al.

1975). However, this removal is often due to the conversion from one form

to another. The disappearance of ammonium ion from percolating systems can

be partially attributed to oxidation by nitrifying bacteria. Adsorption by

clays retains ammonium ions, but this is not necessarily a stable condition

because biological oxidation can occur (Lance 1972). This oxidation is mere­

ly a conversion of ammonium ion to nitrates. The actual removal of nitrogen

from a soil system can be obtained by the reduction of nitrates to nitrogen

gas by biological denitrification and the removal of plant tissue from the

soil system after plant uptake of the nitrate.

A high removal of phosphorus from percolating waters has been observed

in clays. The immobility of phosphorus is attributed to the adsorptive ca­

pacity of soils (Taylor 1967). The latosol soils of Hawaii have a high fix­

ing capacity for phosphorus (Fox 1972; Chu and Sherman 1952; Coleman 1944).

In some areas, the soil competes with plants for the available phosphorus.

Very little movement of adsorbed phosphorus has been observed over a period

IDr. Paul C. Ekern 1975: personal communication.2Dennis Lau 1976: personal communication.3Makaha Nursery caretaker 1976: personal communication.4Herbert Hirota 1976: personal communication.5~!elvyn A. Yoshinaga 1975: personal communication.6Herbert Yamaguchi 1976: personal communication.

Page 11: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

5

of several years. The removal of phosphorus in sand and gravel requires

longer underground travel. High concentrations of phosphorus in percolating

groundwater, up to 91 m (300 ft) from the source, may be attributed to the

lmver fixation capacity of sands and gravels (Bouwer, Lance, and Riggs 1974).

Coliform bacteria and viruses have been successfully removed from perco­

lating waste water by sand and gravel as well as by clay soils. The nearly

complete removal of the bacteria and viruses has been attributed to surface

straining (clogging) and physical adsorption. Laboratory and epidemiological

studies on human contact with reclaimed waters have revealed no health haz­

ards (Lau et al. 1975; Houser 1970; Merrell 1968; Tanimoto et al. 1968).

The presence of bacteria has long been associated with waste waters.

Aerosolized bacteria have been collected up to 1.6 kill (1 mile) downwind of

trickling filter and activated sludge units of sewage treatment plants. Lab­

oratory and field studies have found that 1mv temperature, high relative hu­

midity, high wind velocities, and darkness results in higher recoveries and

greater downwind travel of coliform bacteria. The mechanism of aerosol for­

mation has been studied by several investigators (Brownet al. 1950; Druet

et al. 1953; Woodcock 1955; Wozniack 1976). Water droplets dispersed into

the air from spray irrigation may carry bacteria into the atmosphere. Upon

evaporation, nuclei of dissolved and suspended matter may be retained in the

air. Pathogenic organisms are present in most waste waters and may also be­

come aerosolized. The transfer of waterborne contaminants into the atmos­

phere may result in gastrointestinal and/or respiratory infections.

Ledbetter and Randall (1969) studied the bacterial emissions from acti­

vated sludge units. They used three sampling procedures during their inves­

tigations. The most successful procedur~.which was also the simplest, con­

sisted of exposing poured agar plates up to 30 m (100 ft) downwind from the

aeration tank. They concluded that the bacterial population of air is in­

creased with passage over an activated sludge unit. Despite a rapid die-off

of bacteria, the bacterial population increase persisted over a long distance

and time. They also found that the distance of bacterial presence was depen­

dent on wind velocity. However, no correlation of bacterial concentrations

with either relative humidity or temperature was observed.

Adams and Spendlove in 1970 investigated the aerosols emitted by trick­

ling filter sewage treatment plants and observed the presence of coliforms to

a downwind distance of 1.3 km (0.8 mile). High wind velocities, high rela­

tive humidity, darkness, and low temperature were determined to produce the

5

of several years. The removal of phosphorus in sand and gravel requires

longer underground travel. High concentrations of phosphorus in percolating

groundwater, up to 91 m (300 ft) from the source, may be attributed to the

1mver fixation capacity of sands and gravels (Bouwer, Lance, and Riggs 1974).

Coliform bacteria and viruses have been successfully removed from perco­

lating waste water by sand and gravel as well as by clay soils. The nearly

complete removal of the bacteria and viruses has been attributed to surface

straining (clogging) and physical adsorption. Laboratory and epidemiological

studies on human contact with reclaimed waters have revealed no heal th haz~

ards (Lau et al. 1975; Houser 1970; Merrell 1968; Tanimoto et al. 1968).

The presence of bacteria has long been associated with \vaste waters.

Aerosolized bacteria have been collected up to 1.6 km (1 mile) downwind of

trickling filter and activated sludge units of sewage treatment plants. Lab­

oratory and field studies have found that low temperature, high relative hu­

midity, high wind velocities, and darkness results in higher recoveries and

greater downwind travel of coliform bacteria. The mechanism of aerosol for­

mation has been studied by several investigators (Brownet al. 1950; Druet

et al. 1953; Woodcock 1955; Wozniack 1976). Water droplets dispersed into

the air from spray irrigation may carry bacteria into the atmosphere. Upon

evaporation, nuclei of dissolved and suspended matter may be retained in the

air. Pathogenic organisms are present in most waste waters and may also be­

come aerosolized. The transfer of waterborne contaminants into the atmos­

phere may result in gastrointestinal and/or respiratory infections.

Ledbetter and Randall (1969) studied the bacterial emissions from acti­

vated sludge units. They used three sampling procedures during their inves­

tigations. The most successful procedur~which was also the simplest, con­

sisted of exposing poured agar plates up to 30 m (100 ft) downwind from the

aeration tank. They concluded that the bacterial population of air is in­

creased with passage over an activated sludge unit. Despite a rapid die-off

of bacteria, the bacterial population increase persisted over a long distance

and time. They also found that the distance of bacterial presence was depen­

dent on wind velocity. However, no correlation of bacterial concentrations

with either relative humidity or temperature was observed.

Adams and Spendlove in 1970 investigated the aerosols emitted by trick­

ling filter sewage treatment plants and observed the presence of coliformsto

a downwind distance of 1. 3 km (0.8 mile). High wind velocities, high rela­

tive humidity, darkness, and low temperature were determined to produce the

Page 12: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

6

greatest recoveries, also at greater dm~wind distances, of coliforms.

King, Mill, and Lawrence (1973) examined the bacterial emissions from

an activated sludge plant. Their recovery scheme also incorporated an iden­

tification of colony groups collected. The BaciUus species was the most

predominant organism upwind and downwind of the aeration unit. Escherichia

coli was found solely downwind of the aeration unit. Staphylococcus av~eus

was also found and suggested the probability of primary pathogenic bacterial

dispersion from the plant process. In general, an in-colony count was ob­

served with an increase of temperature, but only in excess of 24°C (76°F).

A combination of low humidity and elevated temperature reduce colony counts

more than either factor alone.

Clark (1974) studied the coliform-containing aeTosols emitted by

activated-sludge (AS) and trickling-filter (TF) units at the Kailua TF and

the Maunawili AS treatment plants on Oahu. Fewer coliform organisms were

emitted from the trickling-filter unit than from the activated sludge unit.

In both cases, colonies were collected as far as a mile dO\~wind of the

respective plants.

SAMPLING STATIONS AND FIELD METHODSWaste Water Characterization

The KMCAS STP is located on the south side of the Air Station, adjacent

to Kane'ohe Bay (Fig. 2). The STP utilizes a single stage trickling filter

K~ne'ohe Ma~ine Corps Air Station

o 1000 fee'I , L

o 300 melers

N

\Kane' ohe Bay

o ao 0

GKMCAS STP

FIGURE 2. LOCATION MAP OF THE ~1CAS SEWAGE TREATMENT PLANT

6

greatest recoveries, also at greater downwind distances, of coliforms.

King, Mill, and Lffivrence (1973) examined the bacterial emissions from

an activated sludge plant. Their recovery scheme also incorporated an iden­

tification of colony groups collected. The Bacillus species was the most

predominant organism upwind and downwind of the aeration unit. Escherichia

co Zi was found so Ie ly downwind of the aeration unit. Staphy lococcus aureus

was also found and suggested the probability of primary pathogenic bacterial

dispersion from the plant process. In general, an in-colony count was ob­

served with an increase of temperature, but only in excess of 24°C (76°F).

A combination of low humidity and elevated temperature reduce colony counts

more than either factor alone.

Clark (1974) studied the coliform-containing aerosols emitted by

activated-sludge (AS) and trickling-filter (TF) units at the Kailua TF and

the Maunawili AS treatment plants on Oahu. Fewer coliform organisms were

emitted from the trickling-filter unit than from the activated sludge unit.

In both cases, colonies were collected as far as a mile downwind of the

respective plants.

SAMPLING STATIONS AND FIELD METHODSWaste Water Characterization

The KMCAS STP is located on the south side of the Air Station, adjacent

to Kane'ohe Bay (Fig. 2). The STP utilizes a single stage trickling filter

Kane'ohe Marine Corps Air Station

a 1000 feelI , I

a 300 malers

o 0o 0

6KMCAS STP

-:-~.~---,*",,_ ....~ .....- ..-

-- .~~---~~~

'i~~~~-'~:­~~..~~~=:~

-.-··-A __ ":-

,;;;{ftj"

Kcme 'ohe BayN

\

FIGURE 2. LOCATION MAP OF THE ~~CAS SEWAGE TREATMENT PLANT

Page 13: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

7

for the biological treatment of the waste water. Following secondary treat­ment, the effluent is chlorinated and passed through an aerated polishingpond (Fig. 3). Flow from the pond is either pumped to the golf course forirrigation or through an outfall into Kane'ohe Bay~

~. . Sump Pumps______12~~R~MAIN~~L~OURS!-~ • _ • _ ~

Grit

J>r"l;;u

Pol i shi ng ~

~PondFinal

Clarifier

~Q... ~erf'- N' /0' .D~~bo,'

2 ~ Chlori neIContactl, ~

Cumm i nu I orc:CDSAMPLING STATION

- --0- O'"l:andfi 11 :1-1-,--.J..I""'!"';"'""T:d~...J~::::Anarobic Digesters

FIGURE 3. KMCAS SEWAGE TREATMENT PLANT LAYOUT

Four, 24-hr composite samples were obtained at the STP on 8 to 9 Octo­ber 1975, 20 to 21 November 1975, 11 to 12 February 1976, and 12 to 13 July1976. Three stations were established for grab sampling. Station 1 was lo­cated at the raw sewagein£low, prior to comminution, Station 2 was locatedin the final clarifier at the outlet pipe, and Station 3 was located next tothe golf course irrigation pumps in the polishing pond (Fig. 3).

Twenty-four, hourly grab samples of raw sewage at Station 1 were col­lected during each of the four sampling dates. During the October and Novem­ber sampling dates, grab samples were collected at Station 2 every fourhours. Grab samples were collected every two hours at Station 3 during theOctober and November sampling dates. During the February sampling period,six grab samples were collected at random at Station 3. During the Julysampling period, hourly grab samples were collected at Station 3.

Grab samples from Stations 1, 2, and 3 were collected with a plastic

7

for the biological treatment of the waste water. Following secondary treat­

ment, the effluent is chlorinated and passed through an aerated polishing

pond (Fig. 3). Flow from the pond is either pumped to the golf course for

irrigation or through an outfall into Kane'ohe Bay.

12 in. FORCE MAIN TO GOLF COURSE------------------------

........:Sump Pumps

-- ==:G)

Pond

ChlorineIContact/ J ~

J­III:II

Po 1ish i ng ~az

rove,f'- ,..;, too -.,c8MlMe b<Jy.

FinalClarifier

~Q.... 2"'

Cumm i nul a r c::::(D SAMPLING STATION

- --0 -O""Landfill :f-I--r-.L'T!-""i~...J~::::Anarobic Digesters

Grit Chamber

FIGURE 3. KMCAS SEWAGE TREATMENT PLANT LAYOUT

Four, 24-hr composite samples were obtained at the STP on 8 to 9 Octo­

ber 1975, 20 to 21 November 1975, 11 to 12 February 1976, and 12 to 13 July

1976. Three stations were established for grab sampling. Station 1 was lo­

cated at the raw sewage inflow, prior to comminution, Station 2 was located

in the final clarifier at the outlet pipe, and Station 3 was located next to

the golf course irrigation pumps in the polishing pOnd (Fig. 3).

Twenty~four, hourly grab samples of raw sewage at Station 1 were col­

lected during each of the four sampling dates. During the October and Novem­

ber sampling dates, grab samples were collected at Station 2 every four

hours. Grab samples were collected every two hours at Station 3 during the

October and November sampling dates. During the February sampling period,

six grab samples were collected at random· at Station 3. During the July

sampling period, hourly grab samples were collected at Station 3.

Grab samples from Stations 1, 2, and 3 \.,rere collected with a plastic

Page 14: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

8

"scoop" bucket and then placed into plastic bottles, for all four sampling

dates. During the February and July composites, automatic samplers were used

as a supplement for early morning sample collection. A refrigerated sampler

(Sigma motor automatic sequential sampler) was used for the February compos­

ite and an Isco automatic sequential sampler was used in July.

Individual plastic bottles were used to collect two 500-m£samplesat

Station I and t\'1O, 1,OOO-m£ samples at Stations 2 and 3 for each sampling

hour. All samples were kept in iced containers or refrigerated at 4°C. All

sample bottles were cleaned with chromic acid and rinsed with distilled de­

ionized water prior to sample collection. Two milliliters of concentrated

sulfuric acid were added, as a preservative, to one sample 'bottle of each

sampling for nutrient analysis.

The collected grab samples from each station were analyzed individually.

This provided information on the composition as well as the hourlyfluctua- .

tions of various constituents in the waste water.

Groundwater Quality

SELECTION AND ESTABLISHMENT OF S.AMPLING SITES. , Three factors determined

the location of the wells for groundwater sampling:

1. Soil characteristics of the area (soil descriptions for the Jaucas

sand and the Ewa silty clay loam are in App. A)

2. Depth of soil to the groundwater

3. Distance of wells from sprinkler heads.

The location, description, and construction details of the sampling

wells are as follows:

Tes t We 11 1. Control well; located 46 m (ISO ft) east of the golf course

clubhouse, adjacent to the NCO Club building and 38 m (125 ft) from the near­

est sprinkler (Fig. 4). A 4-m (13-ft) deep trench was dug using a backho3

from the KMCAS Public Works department. The top l-ft of soil appeared to be

fill material of a different clay group. The surface cover was bermudagrass.

The remaining soil down to the groundwater had the characteristic reddish­

brown color of the Ewa silty clays. A 4-m long, 3. 8-cm (1. 5 in.) ID poly­

vinylchloride (PVC) pipe was positioned vertically in the backfilled trench.

The ground surface was at 109.96 (datum plane of 100.00 is mean low water

[MLW]). The groundwater level was at 101.8, 2.68 m (8.78 ft) below the ground

surface. The bottom cap of the well was 0.98 ill (3.20 ft)below the ground­

water level (Fig. 5).

8

"scoop" bucket and then placed into plastic bottles, for all four sampling

dates. During the February and July composites, automatic samplers were used

as a supplement for early morning sample collection. A refrigerated sampler

(Sigma motor automatic sequential sampler) was used for the February compos­

ite and an Isco automatic sequential sampler was used in July.

Individual plastic bottles were used to collect two SOO-m~ samples at

Station 1 and two, 1,000-m~ samples at Stations 2 and 3 for each sampling

hour. All samples were kept in iced containers or refrigerated at 4°C. All

sample bottles were cleaned with chromic acid and rinsed with distilled de­

ionized water prior to sample collection. Two milliliters of concentrated

sulfuric acid were added, as a preservative, to one sample bottle of each

sampling for nutrient analysis.

The collected grab samples from each station were analyzed individually.

This provided information on the composition as \vell as the hourly fluctua­

tions of various constituents in the waste water.

Groundwater Quality

SELECTION AND ESTABLISHMENT OF SAMPLING SITES .. Three factors determined

the location of the wells for groundwater sampling:

1. Soil characteristics of the area (soil descriptions for the Jaucas

sand and the Ewa silty clay loam are in App. A)

2. Depth of soil to the groundwater

3. Distance of wells from sprinkler heads.

The location, description, and construction details of the sampling

wells are as follows:

Test WeI I I. Control well; located 46 m (150 ft) east of the golf course

clubhouse, adjacent to the NCO Club building and 38 m (125 ft) from the near­

est sprinkler (Fig. 4). A 4-m (13-ft) deep trench was dug using a backho3

from the KMCAS Public Works department. The top l-ft of soil appeared to be

fill material of a different clay group. The surface cover was bermudagrass.

The remaining soil down to the groundwater had the characteristic reddish­

brown color of the Ewa silty clays. A 4-m long, 3.8-cm (1.5 in.) ID poly­

vinyl chloride (PVC) pipe was positioned vertically in the backfilled trench.

The ground surface was at 109.96 (datum plane of 100.00 is mean low water

[MLW]). The groundwater level was at 101.8, 2.68 m (8.78 ft) below the ground

surface. The bottom cap of the well was 0.98 m (3.20 ft)belOlv the ground­

water level (Fig. 5).

Page 15: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

\ 0N

OSPRINl<I.ER HeAD

10

0 0 0 0 1.0 0

pullill9 Driv i ng0 graen /:> 0

~0 Range

0 ....... - Tees11/ KMCAS~?

Course Clu

[KMCASTEST WELL

Showboot ] • NO. 1~ concrete I

slob

N.C.O. Club~ c 1.r:--tMANNING stREET :::J

0 100 faet -...... r---:::I iII I

,0 30met~ I

..-

FIGURE 4. LOCATION MAP OF TEST WELL NO. 1

9

I \J

NOSPRWKL.ER HEAD

10

0 0 0 0 .0 0

pulling(

0 0 .~ grae" p 0 Driving0 Range\,

Tees0

1[1 KMCAS G:'J?Course Club11

-[KMCAS

TEST WELLShowboot ] • NO. 1

[ concr.t. 1slob

( N.C.O. Club.J t= 1r--,

MANNING STREEt :::::J

0 100 feel J'::I III I

I

0 30 metere

~

FIGURE 4. LOCATION MAP OF TEST WELL NO.1

9

Page 16: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

Gr0

r---

-1I

Su

rfa

ce

Gro

un

d

RS

urf

ace

106.

62I

II

107.

64.....

.... .... 4-

........

a....

"4

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a.....

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........

...::r a

EN

.NG

rou

nd

'wa

ter

--I10

1.14

aL

eve

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CV

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Gro

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Jw

ate

rl--

19

8.7

2

Le

ve

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,..-

.--

~!<

cGro

un

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urf

ace

•10

9.96

......... .... 4-

a:> " a:> ........ E a:>

-..0 N ,

101.

80

Gro

un

dw

ate

r--

Le

ve

l

-

TE

ST

WE

LLNO

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ES

T.W

EL

LN

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&.-

TE

ST

WE

LLN

O.3

·

a

FIG

UR

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SC

HE

MA

TIe

CR

OS

SS

EC

TIO

NS

OF

TE

ST

WE

LLN

OS

.1

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,an

d3.

----

-:-.

--~..~,----

~

lei; CG round Surface! 109.96

........j...J

4-

cor---

co----

E

co'-D

N,101.90

Groundwater -- Level

L.-.-

TEST WELL NO. 1

-

Ground Surface! 106.62

.......ol-'4-

00\

0\

----E

N0

r

CV\

,99.72

Groundwater - - Level""""-

TEST \-JELL NO. 2

Ground r--l SurfaceI 107.84

E

...::t'oN

l----...!.'--~ __ l--_--.:..:10:.:.;1.~14:....__ _J

Groundwater Level

TEST WELL NO. 3

FIGURE 5 SCHEMATIC CROSS SECTIONS OF TEST WELLNOS.1, 2, and 3- ------

Page 17: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

11Test Well 2. Located 11 m (35 ft) southeast of the No. 11 tee (Fig. 6).This well was located 0.61 m (2 ft) from a sprinkler head. A hole 3.5 m(11.5 ft) deep was drilled using a 6.4-cm (2.5 in.) diameter hand auger (Fig;5). The surface cover was bermudagrass and the soil material down to thegroundwater was Jaucas sand. A 3.l7-cm (1.25-in.) ID PVC pipe was insertedinto the hole and the zone around the pipe was compacted. The ground surfacewas 2.02 m (6.62 ft) above MLW (106.62). The groundwater level was 3 m(9.90 ft) below the ground surface at 96.72. The depth of water in the wellwas 0.51 m (1.68 ft).

Test Well 3. Located 12.2 m (40 ft) north of the No.3 women's tee andsprinkler heads (Fig. 7). The surface cover was bermudagrass. The PublicWorks department's backhoe was used to dig a 4.6-m (15 ft) deep trench atthis site (Fig. 5). The soil here resembled a typical Ewa silty clay loam.A 4.9-m (16-ft) long, 3.8 em PVC pipe was placed vertically into the back­filled trench. The ground surface level was at 107.84 (2.39 m [7.84 ft]above MLW). The groundwater level was 2.0 m (6.70 ft) below the ground sur­face at 101.14. The depth of water in the well was 2.6 m (8.4ft).The PVC pipe served as a casing for the sampling wells. Each casingwas capped on the bottom. A series of four, 0.32-cm (0.125-in.) diameterholes were drilled into the PVC pipe at 2.54-cm (I-in.) intervals from thebottom cap. A total of 48 holes (a30.48-cm [12-in.] sectlon of pipe) pro­vided entry for groundwater infiltration. into the sampling wells.Groundw~ter from Test Wells 1, 2, and 3 and the sprinkler effluent werecollected during March through May 1976. Eighteen sets of test well samples(Test Wells 1, 2, 3) and nine sprinkler effluent samples were collectedduring the three months. The duration between the collection of sample setsvaried from one to fourteen days.

A Masterflex No. 7015 pump head adapted onto a "D.C. Puppy" pump motor(for 12 V battery operation) was used to draw groundwater samples from thetest wells. Sprinkler effluent was collected by "tapping" a sprinkler head.

Air Quality

The Klipper Golf Course is spray irrigated daily between 6 PM and 6 AM.All 18 greens and the putting green are irrigated each night. One-half ofthe fairways and tees are irrigated on alternate nights. The three majorfactors determining site selection were: accessibility, visibility, and time

11

Test Well 2. Located 11 ill (35 ft) southeast of the No. 11 tee (Fig. 6).

This well was located 0.61 m (2 ft) from a sprinkler head. A hole 3.5 ill

(11.5 ft) deep was drilled using a 6.4-cm (2.5 in.) diameter hand auger (Fig.

S). The surface cover was bermudagrass and the soil material do~m to the

groundwater was Jaucas sand. A 3.l7-cm (l.2S-in.) ID PVC pipe was inserted

into the hole and the zone around the pipe was compacted. The ground surface

was 2.02 m (6.62 ft) above MLW (106.62). The grounmvater level was 3 ill

(9.90 ft) below the ground surface at 96.72. The depth of water in the well

was 0.51 ill (1.68 ft).

Test Well 3. Located 12.2 m (40 ft) north of the No.3 women's tee and

sprinkler heads (Fig. 7). The surface cover was bermudagrass. The Public

Works department's backhoe was used to dig a 4. 6-m (15 ft) deep trench at

this site (Fig. 5). The soil here resembled a typical Ewa silty clay loam.

A 4.9-m (16-ft) long, 3.8 em PVC pipe was placed vertically into the back­

filled trench. TIle ground surface level was at 107.84 (2.39 m [7.84 ft]

above MLW). The groundwater level was 2.0 m (6.70 ft) below the ground sur­

face at 101.14. The depth of water in the well was 2.6 m (8.4 ft).

The PVC pipe served as a casing for the sampling wells. Each casing

was capped on the bottom. A series of four, O.32-cm (0.12S-in.) diameter

holes were drilled into the PVC pipe at 2. 54-em (I-in.) intervals from the

bottom cap. A total of 48 holes (a 30.48-cm [12-in.] section of pipe) pro­

vided entry for groundwater infiltration into the sampling ~vells.

Groundwater from Test Wells 1, 2, and 3 and the sprinkler effluent were

collected during March through May 1976. Eighteen sets of test well samples

(Test Wells 1, 2, 3) and nine sprinkler effluent samples were collected

during the three months. The duration between the collection of sample sets

varied from one to fourteen days.

A Masterflex No. 7015 pump head adapted onto a "D.C. Puppy" pump motor

(for 12 V battery operation) was used to draw groundwater samples from the

test wells. Sprinkler effluent was collected by "tapping" a sprinkler head.

Air Quality

The Klipper Golf Course is spray irrigated daily between 6 PM and 6 AM.

All 18 greens and the putting green are irrigated each night. One-half of

the fairways and tees are irrigated on alternate nights. The three major

factors determining site selection were: accessibility, visibility, and time

Page 18: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

12

oo

o

o

o

Kane 'ohe Bay

oo

oo

oo

b

o

o

o 0

o

o o o

OND. °11 Tee

o 0 • TEST WELL NO. 2

o

(c;) 0

U Women' 5 Tee·

o

N

1 o

o IOOf.et11--.....,...--1.'.,.,_.,.,...J'o 30 meters

o o

o SPRINKLER HEAD

FIGURE 6. LOCATION MAP OF TEST WELL NO.2

12

a

aa

a

a

Kane'ohe Bay

aa

aa

aa

b

a

a

a a

a

a a a

OND. 11 Tee

a o. TEST WELL NO.2

o

aWomen I~ Tee­

o

N

1 a

o 100 feel11---....-1-'.-,-'-,...,o 30melers

a a

o SPRINKLER HEAD

FIGURE 6. LOCATiON MAP OF TEST WELL NO.2

Page 19: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

13

o

o

o

o

o

o

N

j

o

o

~O"'.tw.

o

o,o

• TEST WELL NO ~ 3o

o

o

o

o

o

o

o

o

o

o

HOUSING

o Sprinkler head

MI UTARY

FIGURE 7. LOCATION MAP OF TEST WELL NO.3

13

N

j100 lee.

:domeme

aIo

oHOUSING

o Sprinkler head

00

0 0

0

0

0

0

00

• TEST WELL NO. 30

0 0

v~omen's0

0 Tee0

0 00

0

MILITARY0

0

0

FIGURE 7. LOCATION MAP OF TEST WELL NO.3

Page 20: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

14

of night.

The area near the greens \l1as selected for air quality analysis because

of three qualifying factors. Most greens are accessible from adjacent roads.

During the month of June, the greens were irrigated during the twilight hours

between 6:20 PM and 8 PM when sufficient light was available for the setup

and removal of test equipment. The early evening period of sampling was also

ideal because there was minimal interference and inconvenience to the resi-

dents adjacent to the golf course.

The greens selected for the air quality sampling were Nos. 2,15, and 16

and the practice putting green.

Once wind speed and direction were determined at each green, a downwind

azimuth was selected through the center line of the green (Fig. 8). Covered

petri dishes were mounted on O.9l-m (3-ft) long, 0.32-cm diameter wQoden dow­

els. These mounted dishes were then staked into the ground along the deter­

mined downwind azimuth .. The dishes were placed at distances up to 91 m

(300 ft) from the nearest downwind sprinkler (Fig. 9). The only modification

of the sampling procedure was at green Nos. 15 and 2. The farthest downwind

station was located at 60.96 m (200 ft) because of physical obstructions (a .

steep hill near No. 15 and residential housing near No.2).

The petri dishes with M-Endo medium were exposed to the air between 2

and 4 min. prior to the start of the irrigation ata specific green. The··

petri dishes remained exposed to the atmosphere during the irrigation of the

specific green. At the conclusion of the irrigation cycle, the petri dishes

were covered and collected beginning at the dish nearest the green.

Between 9 and 16 June 1976, 18 sets of air samples were collected at the

four greens.

RESULTS AND DISCUSSION

Waste Water Characterization of the KMCAS Treatment Plant

The primary purpose of the waste water characterization of the KMCAS

treatment plant was to determine the quality of sewage effluent that was be­

ing used for the irrigation of the air station golf course. A secondary pur­

pose was to determine the overall efficiency of the STPoperation. The re­

sults of the four waste water composites are reported in Appendix B.

The average waste water flows through the ~1CAS STP were 2,233, 1,136,

1,438, and 3,709 m3 /day (0.59, 0.30, 0.38, and 0.98 mgd) for the October,

14

of night.

The area near the greens was selected for air quality analysis because

of three qualifying factors. Most greens are accessible from adjacent roads.

During the month of June, the greens were irrigated during the twilight hours

between 6 :20 PM and 8 PM when sufficient light was available for the setup

and removal of test equipment. The early evening period of sampling was also

ideal because there was minimal interference and inconvenience to the resi-

dents adjacent to the golf course.

The greens selected for the air quality sampling were Nos. 2, 15, and 16

and the practice putting green.

Once wind speed and direction were determined at each green, a downwind

azimuth was selected through the center line of the green (Fig. 8). Covered

petri dishes were mounted on O.9l-m (3-ft) long, 0.32-cm diameter wooden dow­

els. These mounted dishes were then staked into the ground along the deter­

mined downwind azimuth. The dishes were placed at distances up to 91 m

(300 ft) from the nearest downwind sprinkler (Fig. 9). The only modification

of the sampling procedure was at green Nos. 15 and 2. The farthest downwind

station was located at 60.96 m (200 ft) because of physical obstructions (a

steep hill near No. 15 and residential housing near No.2) .

The petri dishes with M-Endo medium were exposed to the air between 2

and 4 min. prior to the start of the irrigation at a specific green. The

petri dishes remained exposed to the atmosphere during the irrigation of the

specific green. At the conclusion of the irrigation cycle, the petri dishes

\vere covered and collected beginning at the dish nearest the green.

Between 9 and 16 June 1976, 18 sets of air samples were collected at the

four greens.

RESULTS AND DISCUSSION

Waste Water Characterization of the KMCAS Treatment Plant

The primary purpose of the waste water characterization of the KMCAS

treatment plant was to determine the quality of sewage effluent that was be­

ing used for the irrigation of the air station golf course. A secondary pur­

pose was to determine the overall efficiency of the STP operation. The re­

suI ts of the four \vaste water composites are reported in Appendix B.

The average waste water flows through the JGvlCAS STP were 2,233, 1,136,

1,438, and 3,709 m3 /day (0.59, 0.30, 0.38, and 0.98 mgd) for the October,

Page 21: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

15

• TEST WELL NO. 3

N

~Wind

DirectiOft

100 feeti'

30 meters.1o

oI

HOUSING

MILITARY

FIGURE 8. DETERMINED DOWNWIND AZIMUTH FOR AIR SAMPLING

15

• TEST WELL NO. 3

N

~Wind

Direction

Tee

100 feeti'

30 met"""o

oI

HOUSING

MI LlTARY

FIGURE 8. DETERMINED DOWNWIND AZIMUTH FOR AIR SAMPLING

Page 22: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

16

No. 1 Tee

N

om. iDire~

C2 11 Tee

100 feetoIo

o SPRINKLER HEAD

OAIR SAMPLER

FIGURE 9. AIR SAMPLING CONFIGURATION

16

C2 11 Tee

oNo. 1 Tee

o SPRINKLER HEAD

o AIR SAMPLERoIo

IOOf",

I30metMS

N

",' jm~-r1

FIGURE 9. AIR SAMPLING CONFIGURATION

Page 23: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

17

November, February; and July composite dates, respectively. The higher flows

during the October and July composites can be attributed to higher water

usage at the air station. A general trend was observed in the pattern of

hourly flow fluctuations during each of the 24-hr composites (Fig. 10). Peak

flows occurred at about 7 AM, 1· PM, and 7 PM; the low flow period \vas between

1 AM and 6 AM.

In general, the raw sewage, secondary effluent, and pond effluent were

of fairly uniform composition.

The mean values for BODs, suspended solids, total nitrogen, and total

phosphorous concentrations in the raw sewage were respectively, 116, Ill,

21.6, and 7.2 mg/~. These low concentrations are indicative of a mild or

weak domestic sewage (Metcalf and Eddy 1972). TheKMCAS sewage system is lo­

cated close to the brackish water table of the M6kapu Peninsula. The rela~

tively weak domestic sewage at the KMCAS sewage treatment plant can beattri­

buted to the infiltration of brackish groundwater into the sewage system.

The mean values of chloride concentrations in the raw sewage and ground­

water were respectively 450 and 18,000 mg/~~ The chloride concentration in

the drinking water on the KMCAS was 30 mg/L Between 20 and 28% of the flow

into the STP can be attributed to the infiltration of brackish or saline

groundwater.

The KMCAS sewage system is fairly old and its close proximity to the

groundwater table results in the high infiltration into the system.

Grab samples of secondary effluent, prior to chlorination, were collect­

ed in October and November 1975. The various removal efficiencies of the

treatment plant process (raw to secondary effluent, secondary effluent to

pond effluent, and raw to pond effluent) are listed in Table 1. Removal of

82% of the BODs and 80% of the suspended solids was accomplished between the

influent raw sewage and the trickling filter effluent. These removal rates

are typical of many trickling filter plants in Hawaii and the mainland U.S.

(Chun, Young, and Anderson 1972; McGauhey 1968).

Removal of an additional 33% BODs, 59% suspended solids~ and 12.5% organ­

ic nitrogen was accomplished in the polishing pond (between the secondary ef­

fluent and the polishing pond effluent). This removal of BODs and organic

nitrogen can be attributed to the settling of organic solids and biological

activity in the pond. Between 17 and 25 kg/day (38 and 54 lb/day) of sus­

pended solids are settling into the pond (Table 2). This accumulation of··

solids eventually will require the dredging of the polishing pond. However,

17

November, February; and July composite dates, respectively. The higher flows

during the October and July composites can be attributed to higher water

usage at the air station. A general trend was observed in the pattern of

hourly flow fluctuations during each of the 24-hr composites (Fig. 10). Peak

flows occurred at about 7 AM, l· PM, and 7 PM; the low flow period was between

1 AM and 6 AM.

In general, the raN sewage, secondary effluent, and pond effluent were

of fairly uniform composition.

The mean values for BODs, suspended solids, total nitrogen, and total

phosphorous concentrations in the raw sewage were respectively, 116, Ill,

21.6; and 7.2 mg/5I,.These low concentrations are indicative of a mild or

weak domestic sewage (Metcalf and Eddy 1972). The KMCAS se\vage system is lo­

cated close to the brackish water table of the M6kapu Peninsula. The rela­

tively weak domestic sewage at the KMCAS sewage treatment plant can beattri­

buted to the infiltration of brackish groundwater into the sewage system.

The mean values of chloride concentrations in the raw sewage and ground­

water were respectively 450 and 18,000 mg/~. The chloride concentration in

the drinking water on the KMCAS was 30 mg/5I,. Between 20 and 28% of the flow

into the STP can be attributed to the infi! tration of brackish or saline

groundwater.

The KMCAS sewage system is fairly old and its close proximity to the

groundwater table results in the high infiltration into the system.

Grab samples of secondary effluent, prior to chlorination, were collect­

ed in October and November 1975. The various removal efficiencies of the

treatment plant process (raw to secondary effluent, secondary effluent to

pond effluent, and raw to pond effluent) are listed in Table 1. Removal of

82% of the BODs and 80% of the suspended solids was accomplished between the

influent raw sewage and the trickling filter effluent. These removal rates

are typical of many trickling filter plants in Hawaii and the mainland u.s.(Chun, Young, and Anderson 1972; McGauhey 1968).

Removal of an additional 33% BODs, 59% suspended solids, and 12.5% organ­

ic nitrogen was accomplished in the polishing pond (between the secondary ef­

fluent and the polishing pond effluent). This removal of BODs and organic

nitrogen can be attributed to the settling of organic solids and biological

activity in the pond. Between 17 and 25 kg/day (38 and 54 lb/day) of sus­

pended solids are settling into the pond (Table 2). This accumulation of

solids eventually will require the dredging of the polishing pond. However,

Page 24: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

-0 01

'E ~

~ ......J

IJ...

ii

I2.

0,I

08

-9O

ctob

er19

75o

20~21

Nov~mber

1975

A11

-12

Feb

ruar

y19

76o

12-1

3Ju

ly19

76

1.6

1.2

0.0

,I

I,

I

6AM

1.2N

6PM

12M

6AM

TIM

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RE.

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OU

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MC

AS

SE

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TP

LAN

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00

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0.8

0.4

o 8-9 October 1975o 20-21 November 19756 11-12 February 1976o 12-13 July 1976

O. a'-- ---1.- --l- --l.- ,-----J

6 AM 12 N 6 PM 12 M 6 AMTIME

FljJURE 10. HOURLY FLOU PATTERN, l<.MCAS SEVlAGE TREATMENT PLANT

Page 25: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

19

TABLE 1. \~ASTE WATER ANALYSES OF KMCAS 'TREATMENT PLANT EFFI·CIENCIES.. ... . .

. 10/75a 11/756 2/76c 7/76d--'0 +J O+J 0 +J O+J O+J O+J+J o e +J e +J oe +J e +J e +J e>- >-+J OJ OJ >- >-+J OJ (l) OJ OJOJ 1-+J 1- ::J OJ ::J OJ 1- +J 1- ::J OJ ::J OJ ::J OJ ::JOlroe ro+J~ Ol~ Olro e ·ro+J~ Ol~ Ol~ Ol~

Constituent l'O-o OJ -oe4- ro4- ro-o OJ -oe4- l'O4- l'O4- ro4-3 e ::J e OJ 4- 34- 3 e ::J e OJ 4- 34- 34- 34-OJ o·~ O::JW OJW OJ 0""'" O::JW OJW OJW OJWV') U4- u~ V') V') U4- u~ V') V') V')OJ 4- OJ 4--0 -0 OJ 4- OJ 4- -0 "'0 "'0 -0·3V')W V') 4- e 3 e 3V')W V') 4- e 3: e 3 e 3 ero W 0 l'O 0 ro W 0 ro 0 l'O 0 ro 00::: 0- 0:::0- 0::: 0... 0:::0... 0:::0... 0::: 0..-~-------------------------(mg/t)----------------------------

TDS10. 1

SS 82.7 57·9 92.7 78. 1 60.0 91.2 93.9 88.7BODs 82.3 33.3 88.2 90.3 93~7NH 3 -N 56.7 - 6.8 53.5 45.3 0.0 45.3 33. 1 36.8Org. N 59.7 -";25.0 46.3 65.6 25.0 74.2 74.4 62.2N02 + N0 3 -N -99.5 59.5 -98.8 -98.6 65.8 ~96.0 -97.1 -98.8Total N 36.7 15.0 46.2 47. 1 14.6 54.5 47.9 42.0Total P 9.4 - 2.7 11.9 7.4 - 1.1 6.4 3.7 -24.5Na

K

e1- 20.8 0.8 - 7.9 - L8 - 9.6 - '. 1.0 - 7.9S04 14.2NOTE: Constituent reduction reported as percent removal.aBase1ine values obtained from App. Tables B.1-B.3.bBaseline values obtained from App. Tables B.4-B.6.cBaseline values obtained from App. Tables B.7-B.8.dBase 1ine values obtained from App. Tables B.9-B.10.

TABLE 2. SUSPENDED SOLIDS REMOVAL IN THEKMCAS STP POLISHING POND

Date Avg. Sec. Pond RemovalFlow Eff. Eff.------(mg/t)----- (mg/t) (1 b/day)

Oct. 1975 0.59 19 8 11 54. 1Nov. 1975 0.30 25 10 15 37.5

19

TABLE l. WASTE WATER ANALYSES OF KMCAs TREATMENT PLANT EFFICIENCIES

lO/75a 11/756 2/76 c 7/76 d0 +J O~ 0 .j..J O+.J O+.J o -I-'.j...J o C .j...J C .j...J o C +.J C .j..J C .j..J C

>- >- +J O.l O.l >- >- +-' O.l O.l <Il (!)<Il\.....j...J \.... ::J O.l :::J <Il L. +.J \.... ::J (J) :::J (!) ::J (!) ::JOlCOC CO-l-'~ tn~ tnCOC CO.j..J~ OJ~ tJ) ~ tJ)~

Constituent CO"'D O.l "'Dc4- C04- CO"'D O.l "'DC4- CO 4- ro4- CO 4-3 C :::J C(J)4- 3:4- 3: C ::::l C<lJ4- 3:4- 34- 3:4-O.lO~ O:::JW (!)W O.lO~ O::JW (J)W (!)W (!)W

if) U 4- u~ if) (./)U4- u~ (./) (./) (./)

<Il4- 0.l4-"'D "'D (1)4- Q) 4- -0 -0 -0 -03:(./)w (./)4-C 3: C 3: (./) W (./) 4- C 3: C 3: c 3 Cro W 0 co 0 co w 0 co 0 ro 0 ro 0

rr: 0- rr: 0- rr: 0- rr: CL rr: 0- rr: 0..

---------------------------(mg/l)----------------------------

TDS 10. 1

SS 82.7 57.9 92.7 78. 1 60.0 91.2 93.9 88.7

BODs 82.3 33.3 88.2 90.3 93·7NH 3 -N 56.7 - 6.8 53.5 45.3 0.0 45.3 33. 1 36.8

Org. N 59.7 -25.0 46.3 65.6 25.0 74.2 74.4 62.2

N0 2 + N0 3 -N -99.5 59.5 -98.8 -98.6 65.8 -96.0 -97. 1 -98.8

Total N 36.7 J5.0 46.2 47. 1 14.0 54.5 47.9 42.0

Total P - 9.4 - 2.7 11.9 7.4 - 1.1 6.4 3.7 -24.5

Na

K

Cl- 20.8 0.8 - 7.9 - 1.8 - 9.6 - .1.0 - 7.9

S04 14.2

NOTE: Constituent reduction reported as percent removal.aBaseline values obtained from App. Tables 8.1-B.3.bBaseline values obtained from App. Tables 8.4-B.6.cBaseline values obtained from App. Tables 8.7-B.8.dBase 1i ne values obtained from App. Tables B.9-B.l0.

TABLE 2. SUSPENDED SOLIDS REMOVAL IN THEKMCAS STP POLISHING POND

Date Avg. Sec. Pond RemovalFlow Eft. Eff.------(mg/l)----- (mg/l) (lb/day)

Oct. 1975 0.59 19 8 I1 54.1

Nov. 1975 0.30 25 10 15 37.5

Page 26: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

20

the polishing pond's maj or function appears to be that of anequalization and

retention basin.

In general, the quality of the effluent used for golf course irrigation

is considered good. The overall reduction of BODs and suspended solids (raw

sewage to the pond effluent) of 90% is achieved by the sewage treatment plant.

The total nitrogen and phosphorous levels of the waste waters are not de­

creased by the treatment plant operation. This is expected because removal

of nitrogen and phosphorus is not among the primary objectives of secondary

treatment plants. On 6 June 1976, a single grab salilple ofchlorinated pond

effluent from the STP was collected for preliminary viral analysis. The re­

sults of the viral analysis by Dr. Roger S. Fujioka at the University of

Hawaii's Virology Labo:ratory \'las negative, i. e., no viruses were isolated.

The KMCAS STP operation produces a high quality effluent that can be attri­

buted to the relatively weak domestic sewage and the use of the polishing

pond.

From an agricultural standpoint, the quality of the applied pond efflu­

ent is acceptable for the irrigation of the golf course. According to Dye

(1958), sewage effluent containing total solids between 800 and 1,200 ~g/~,

total nitrogen between 16 and 20 mg/~, total phosphorus between 7 and 13 mg/~,

and sulfates between 120 and 180 mg/~ is of good agricultural value. The

pond effluent at the KMCAS STP has characteristics similar to those cited by

Dye. The two major plant nutrients, nitrogen (total N)and phosphorus (total

P), have been applied (through the irrigation system) onto the golf course at

respective rates of 94 and 66 kg/wk (208 and 145 lb/wk). This application is.

an additional supplement to regular fertilization.

The mean sodium and chloride concentrations in the applied effluent were

high (230 mg/~ and 342 mg/~, respectively). A high concentration of sodium

in irrigation water can produce an undesirable condition in soils. Sodium

can react with the clay in some soils to decrease permeability. This is a

common occurrence in Hawaiian Vertisols (tropical black earths). However,

the Oxisols (low humic latosols) are tropical red earths that are not affected

by the high sodium concentration (El-pwaify and Swindale 1968).

Sodium and chloride concentration (salinity) can reduce the growth rates

of various types of plants (Ackerson and Younger 1975), The high salt concen­

tration in irrigation water can damage grass. The KMCAS uses various types

of bermudagrasses for the golf course. In general, bermudagrasses are salt­

tolerant grasses that survive well in coastal areas (Ackerson and Younger

20

the polishing pond's major function appears to be that of an equalization and

retention basin.

In general, the quality of the effluent used for golf course irrigation

is considered good. The overall reduction of BODs and suspended solids (raw

sewage to the pond effluent) of 90% is achieved by the sewage treatment plant.

The total nitrogen and phosphorous levels of the waste waters are not de­

creased by the treatment plant operation. This is expected because removal

of nitrogen and phosphorus is not among the primary objectives of secondary

treatment plants. On 6 June 1976, a single grab sample of chlorinated pond

effluent from the STP was collected for preliminary viral analysis. The re­

sults of the viral analysis by Dr. Roger S. Fujioka at the University of

Hawaii's Virology Laboratory was negative, i.e., no viruses were isolated.

The KMCAS STP operation produces a high quality effluent that can be attri­

buted to the relatively weak domestic sewage and the use of the polishing

pond.

From an agricultural standpoint, the quality of the applied pond efflu­

ent is acceptable for the irrigation of the golf course. According to Dye

(1958), sewage effluent containing total solids between 800 and 1,200 mg/~,

total nitrogen between 16 and 20 mg/~, total phosphorus between 7 and 13 mg/~,

and sulfates between 120 and 180 mg/~ is of good agricultural value. The

pond effluent at the KMCAS STP has characteristics similar to those cited by

Dye. The two major plant nutrients, nitrogen (total N) and phosphorus (total

P), have been applied (through the irrigation system) onto the golf course at

respective rates of 94 and 66 kg/wk (208 and 145 Ib/wk). This application is

an additional supplement to regular fertilization.

The mean sodium and chloride concentrations in the applied effluent were

high (230 mg/~ and 342 mg/~J respectively). A high concentration of sodium

in irrigation water can produce an undesirable condition in soils. Sodium

can react with the clay in some soils to decrease permeability. This is a

common occurrence in Hawaiian Vertisols (tropical black earths). However,

the Oxisols (low humic latosols) are tropical red earths that are not affected

by the high sodium concentration (Eli$waify and Swindale 1968).

Sodium and chloride concentration (salinity) can reduce the growth rates

of various types of plants (Ackerson and Younger 1975). The high salt concen­

tration in irrigation water can damage grass. The KMCAS uses various types

of bermudagrasses for the golf course. In general, bermudagrasses are salt­

tolerant grasses that survive well in coastal areas (Ackerson and Younger

Page 27: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

21

1975). None of the species on the KMCAS golf course have shown adverseeffects due to the high salinity of the applied effluent; however, the sprayirrigation should be carefully monitored. During hot and sunny days, therapid evaporation of the effluent may result in the additional concentrationof salt on the grass blades. This could cause damage (discoloration) to thebermudagrasses.

Due to the large scale use of sewage effluent for irrigation, runofffrom the golf course could result in the contamination of nearby surfacewaters. On 6 February 1976, surface water runoff was collected during aheavy rainstorm. Runoff samples were collected near the No. 2 and No. 18greens. Total Kjeldahl nitrogen, combined nitrate and nitrite nitrogen, andtotal phosphorous analyses were performed on the samples. The results ofthe Tunoffanalysis (Table 3) indicate that pollution of surface water isnot due to runoff from the KMCAS Klipper Golf Course.

TABLE 3. RUNOFF ANALYSIS, KMCAS KUPPER GOLF COURSE,6 FEBRUARY 1976

Constituent No.2Green

No. 18Green

Contro 1Area~\-

-------------(mg/~)----~--------~

Groundwater Quality

The groundwater test wells permitted the observation of the movement ofvarious waste water constituents through the two major soils on the golfcourse. The Ewa silty clay loam is the pr~dominant soil type over approxi-

\mately 50% of the golf course. The Jaucas sand is the second most abundantsoil type, covering approximately 25% of the golf course. The remaining soiltypes on the golf course are: Mokuleia clay loam (15%), Makalapa clay (2%),and fill land (8%). Soil descriptions are listed in Appendix A. The Ewasil ty clay loam and the Mokuleia clay loam belong to the same soil order(Mollisols) . In general, both soils have some similarqualities.

21

1975). None of the species on the KMCAS golf course have shmm adverse

effects due to the high salinity of the applied effluent; however, the spray

irrigation should be carefully monitored. During hot and sunny days, the

rapid evaporation of the effluent may result in the additional concentration

of salt on the grass blades. This could cause damage (discoloration) to the

bermudagrasses.

Due to the large scale use of sewage effluent for irrigation, runoff

from the golf course could result in the contamination of nearby surface

waters. On 6 February 1976, surface water runoff was collected during a

heavy rainstorm. Runoff samples were collected near the No.2 and No. 18

greens. Total Kjeldahl nitrogen, combined nitrate and nitrite nitrogen, and

total phosphorous analyses were performed on the samples. The results of

the runoff analysis (Table 3) indicate that pollution of surface water is

not due to runoff from the KMCAS Klipper Golf Course.

TABLE 3. RUNOFF ANALYSIS, KMCAS KLIPPER GOLF COURSE,6 FEBRUARY 1976

Constituent No.2Green

No. 18Green

Contro 1Area*

-------------(mg/~)----~--------~

TKN 1• I 1.5 1.3

N02 + N03-N 0.02 0.03 0.02

Total P 0.68 0.69 0.68

*Control area was located 61 m (200 ft) due south ofthe No.2 green, and adjacent to a drainage ditchacross Lawrence Rd. near the baseball diamond.

Groundwater Quality

The groundwater test wells permitted the observation of the movement of

various waste water constituents through the two major soils on the golf

course. The Ewa silty clay loam is the pr~dominant soil type over approxi-\

mately 50% of the golf course. The Jaucas sand is the second most abundant

soil type, covering approximately 25% of the golf course. The remaining soil

types on the golf course are: Mokuleia clay loam (15%), Makalapa clay (2%),

and fill land (8%). Soil descriptions are listed in Appendix A. The Ewa

silty clay loam and the Mokuleia clay loam belong to the same soil order

(Mollisols) . In general, both soils have some similarquali ties.

Page 28: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

22

The Ewa silty clay loam and the Jaucas sand were selected for the loca­

tion of the groundwater test wells. The two soil types were representative

of the soil characteristics that are predominant on the ~~CAS golf course.

The specific test well sites were selected with respect to the soil

depth to the grounrnvater and their distance to the spray irrigation sprink­

lers (Fig. 11). The test wells were constructed using a 6-cm (2.5 in.) hand

auger and a trench digger (backhoe). These methods of contruction limited

the effective depth of the wells to approximately 4.6 m (15 ft). Test Well

No. 1 was established as a control \vell outside the effective range of the

sprinklers on the southern boundary of the golf course. Test Well No. I was

used to examine the quality of uncontaminated groundwater near the golf

course. Test Well Nos. 2 and 3 were established within the spray irrigation

range of the sprinklers. These two wells were used to examine the quality

of groundwater below the spray irrigation system of the golf course. The

movement of groundwater appeared to be toward the ocean (south to north

across the golf course)~ thus the use of Test Well No. I as a control well.

The determination of the actual quantity of applied effluent proved to

be quite difficult. The quantity of waste water applied onto the golf

. course was controlled by the groundskeeper and varied according to the re­

quirements of each grass species. The automatic sprinkler system controls

are usually modified every few months to maintain the desired quality of the

greens and fairways. The greens and fairways received different quantities

of effluent. The effluent discharge pump system at the STP was not metered.

The quantity of effluent is not necessarily distributed evenly through­

out the, golf course and the variations in types of sprinkler heads, water

pressure, and wind patterns also complicated the analysis of applied efflu­

ent applied onto the golf course was indirectly determined. Determination

of the application rate was based on the following: (1) number of sprinkler

heads on the golf course, (2) average flow of the sprinkler heads, (3) aver­

age "on time" of the sprinklers, and (4) average area covered by the sprink­

ler heads. Approximately I cm (0.4 in.) of pond effluent per week is applied

on the fairways and tees of the golf course. The greens receive six times as

much effluent than the fairways (S. 6 em [2.2 in.] per week).

The Klipper Golf Course receives treated waste water pumped through a

30.S-cm (12 in.) diameter force main. Minor quality changes of pond effluent

occurs during the retention time in the force main (Table A) . The most sig-.

nificant change occurs in the concentration of nitrogen. Combined nitrite

.122

The Ewa silty clay loa~m and the Jaucas sand were selected for the loca­

tion of the groundwater test wells. The two soil types were representative

of the soil characteristics that are predominant on the KMCASgolf course.

The specific test well sites were selected with respect to the soil

depth to the groundNater and their distance to the spray irrigation sprink­

lers (Fig. 11). The test wells were constructed using a 6-cm (2.5 in.) hand

auger and a trench digger (backhoe). These methods of contruction limited

the effective depth of the wells to approximately 4.6 m (15 ft). Test Well

No. I was established as a control well outside the effective range of the

sprinklers on the southern boundary of the golf course. Test Well No. 1 was

us ed to examine the quality of uncontaminated groundwater near the golf

course.· Test Well Nos. 2 and 3 were established within the spray irrigation

range of the sprinklers. These two wells were used to examine the quality

of groundwater below the spray irrigation system of the golf course. The

movement of groundwater appeared to be toward the ocean (south to north

across the golf course), thus the use of Test Well No. I as a control well.

The determination of the actual quantity of applied effluent proved to

be quite difficult. The quantity of waste water applied onto the golf

. course was controlled by the groundskeeper and varied according to the re­

quirements of each grass species. The automatic sprinkler system controls

are usually modified every few months to maintain the desired quality of the

greens and fainvays. The greens and fairways received different quantities

of effluent. The effluent discharge pump system at the STP was not metered.

The quantity of effluent is not necessarily distributed evenly through­

out the golf course and the variations in types of sprinkler heads, water

pressure, and wind patterns also complicated the analysis of applied efflu­

ent applied onto the golf course was indirectly determined. Determination

of the application rate was based on the following: (1) number of sprinkler

heads on the golf course, (2) average flow of the sprinkler heads, (3) aver­

age "on time" of the sprinklers, and (4) average area covered by the sprink­

ler heads. Approximately 1 cm (0.4 in.) of pond effluent per week is applied

on the fairways and tees of the golf course. The greens receive six times as

much effluent than the fairways (5.6 ern [2.2 in.] per week).

The Klipper Golf Course receives treated waste water pumped through a

30.5-cm (12 in.) diameter force main. Minor quality changes of pond effluent

occurs during the retention time in the force main (Table A) . The most sig­

nificant change occurs in the concentration of nitrogen. Combined nitrite

Page 29: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

~Q·'':P5

........

..·..i

iilft:

i'f.

.::::z

;;:::;

:;;:...

....

....

...c

;;;

•TE

ST

WE

LLK

ane'

ohe

Ba

y

@G

REE

N

FIG

UR

E11

.KM

CAS

KLI

PPER

GO

LFCO

URSE

AND

GRO

UNDW

ATER

TEST

WEL

LSN tN

• TEST WELL

Ka:ne 'ohe Bay

@ GREEN

FIGURE 11. KMCAS I<LlPPER GOLF COURSE AND GROUNDWATER TES, WELLS

6

Page 30: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

24

TABLE 4. MEAN CONSTITUENT CONCENTRATION CHANGESBETV/EEN KMCAS STP POND EFFLUENT ANDKLIPPER GOLFtbuRSE SPRINKLER ~FFLUENT

Constituent Pond Sprinkler PercentEffluent* Effluent t Reduction------- (mg/ Q.) --------

NH 3 -N 7.8 10.9 -28.4

Organic N 2.8 1.84 +34.3

NO z + NO -N 1.0 I 0.03 +97.03 .

Total N 1J .39 12.75 -10.7

Total P 7.78 8.9 -12.6

K 20 22 - 9.0

Cl- 475 329 +30.7

*Baseline values obtained from App.Tables B:3,B.6, B.8, and B.l0.

tBaseline values obtained from App. Table c.4;

and nitrate concentration was decreased to 0.01 mg/Q.. Apparently, denitrifi­

cation occurs during the retention period. The force main is 1. 6 kin (1 mile)

long and contains 117 m3 (31,000 gal) of pond effluent. Therefore, only 11%

of the total quantity of pond effluent (1,060 m3 or 280,000 gal used for one

night of irrigation) is retained in the force main for the 12-hr period.

The results of the groundwater sampling are listed in AppendixE. Two

groundwater testing wells (Nos. 1 and 3) on the Klipper Golf Course are lo­

cated in Ewa silty clay loam. Test Well 1 was the control well located out­

side the influence of the spray irrigation system and Test Well 3 was locat­

ed in the area receiving waste water irrigation. Changes in groundwater

quality were observed between Test Wells 1 and 3. Irrigation with waste

water resulted in the increase of ammonia nitrogen (0.20 mg/Q.), organic ni­

trogen (0.20 mg/Q.), sodium (177 mg/Q.), and chloride (10 mg/Q.) in the ground­

water (Table 5).

In Table 6, the change in constituent concentration can be noted with

the passage of sewage effluent through the low humic latosol on the KMCAS

golf course. Substantial decreases occurred for total nitrogen (98.2%),

total phosphorus (100%), and fecal coliforms (100%). Similar results were

obtained in the Mililani Recycling Project (King, Mill, and Lawrence 1973;

Clark 1974; Metcalf and Eddy, Inc. 1972). TIle Mililani soil was also a low

humic latosol (Lahaina series) in which nitrogen removal of 97.5 to 99.9%

was at.tributed to: (1) sorption to the soil complex, (2) uptake bymacro~

24

TABLE 4. MEAN CONST ITUENT CONCENTRAT ION CHANGESBETIJEEN KMCAS STP POND EFFLUENT ANDKLIPPER GOLF COURSE SPRINKLER EFFLUENT

Constituent Pond Sprinkler PercentEffluent* Effluent t Reduction-------(mg/~)--------

NH 3 -N 7.8 10.9 -28.4

Organic N 2.8 1.84 +34.3

N0 2 + N0 3 -N 1.01 0.03 +97.0

Tota 1 N 1J .39 12.75 -10.7

Total P 7.78 8.9 -12.6

K 20 22 - 9.0

Cl- 475 329 +30.7

*Basel ine values obtained from App. Tables B.3,B.6, B.8, and B.l0.

tBaseline values obtained from App. Table c.4.

and nitrate concentration was decreased to 0.01 mg/~. Apparently, denitrifi­

cation occurs during the retention period. The force main is 1.6 km (1 mile)

long and contains 117 m3 (31,000 gal) of pond effluent. Therefore, only 11%

of the total quantity of pond effluent (1,060 m3 or 280,000 gal used for one

night of irrigation) is retained in the force main for the 12-hr period.

The results of the groundwater sampling are listed in Appendix E. Two

groundlvater testing wells (Nos. 1 and 3) on the Klipper Golf Course are lo­

cated in Ewa silty clay loam. Test Well I was the control well located out­

side the influence of the spray irrigation system and Test Well 3 was locat­

ed in the area receiving waste water irrigation. Changes in groundwater

quality were observed between Test Wells 1 and 3. Irrigation with waste

water resulted in the increase of ammonia nitrogen (0.20 mg/~), organic ni­

trogen (0.20 mg/~), sodium (177 mg/~), and chloride (10 mg/~) in the ground­

water (Table 5).

In Table 6, the change in constituent concentration can be noted with

the passage of sewage effluent through the low humic latosol on the KMCAS

golf course. Substantial decreases occurred for total nitrogen (98.2%),

total phosphorus (100%), and fecal coliforms (100%). Similar results were

obtained in the Mililani Recycling Project (King, Mill, and Lmvrence 1973;

Clark 1974; Metcalf and Eddy, Inc. 1972). TIle Mililani soil was also a low

humic latosol (Lahaina series) in which nitrogen removal of 97.5 to 99.9%

was attributed to: (1) sorption to the soil complex, (2) uptake by macro-

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25

TASLE 5. MEAN CONSTITUENT CONCENTRATION CHANGEBETWEEN TEST WELL NOS. 1 AND.3GROUNDWATER SAMPLES

Constituent

NH3-NOrganic NN02 + N03-NTotal NTotal PCl-NaK

FecalCo 1i form

Test Well Test Well Net.No. ]'" No. 2t Increase

-------~-----(mg/~)-------------·0.10 0.30 +0.200.43 0.63 +0.200.26 0.16 -0.100.76 1.04 +0.280.66 0.11 -0.55

2087 2097· +102041 .2218 +177

90 82 - -8--~-~----(No./I00 m~)-----~---­000

*Baseline values obtained from App. Table C.l.tBaselinevalues obtained from App. Table C.2.

TABLE 6. MEAN CONSTITUENT CONCENTRATION CHANGEOF EFFLUENT THROUGH LOW HUMIC LATOSOLSON THE KMCAS GOLF COURSE

ConstituentPond Low Humic Percent

Effluent* Latosols ReductiQnPerc. Ql tyt

NH3- NOrganic NN02 + N03-NTotal NTotal PCl-NaK

Feca 1 Co 1i form

--------(mg/~)----~--10.9 0.201.84 0.200.03

12.75 0.288.9

329 10230 17722

-----(No./I00 m~)-~--160 0

·+98.2+89.1

+100+97.8

+100+97.0+23.0

+100

+100*Baseline values obtained from App. Tables B.3,B.6, B.8, and B.IO.tBaseline values obtained from Table 5.

and microorganisms (including plants), (3) volatilization to ammonia gas athigher pH values, (4) biological oxidation (nitrification of ammonia tonitrate), and (5) denitrification (reduction of nitrates to nitrogen gas).

According to Lance (1972), a significant amount of the removal of nitro­gen in soil can be attributed to denitrification and the adsorption of the

.'ammonium ion. Denitrification of nitrate to nitrogen gas can occur in anae-

25

TAS LE 5. MEAN CON STITU ENT CON (EN TRATION CHANG EBETWEEN TEST WELL NOS. 1 AND 3GROUNDWATER SAMPLES

Can s t i tuen t

NH3-NOrganic NN02 + N03-NTotal NTotal PCl -NaK

FecalCo 1iform

Test Well Test Well NetNo. ]"- No. 2t Increase

-------------(mg/~)-------------·

0.10 0.30 +0.200.43 0.63 +0.200.26 0.16 -0.100.76 1.04 +0.280.66 0.11 -0.55

2087 2097' +102041 2218 +177

90 82 -8--~------(No./IOO m2)---------­000

*Baseline values obtained from App. Table C. l.tSaselinevalues obtained from App. Table C.2.

TABLE 6. MEAN CONSTITUENT CONCENTRATION CHANGEOF EFFLUENT THROUGH Lm" HUMI C LATOSOLSON THE KMCAS GOLF COURSE

Pond low Humic PercentCons t i tuent Eftl uent* Latosols Reduction

Perc. Q1 tyt

--------(mg/t)-------NH3- N 10.9 0.20 +98.2Organic N 1. 84 0.20 +89.1N0 2 + N0 3-N 0.03 +100Total N 12.75 0.28 +97.8Total P 8.9 +100Cl - 329 10 +97.0Na 230 177 +23.0K 22 +100

-----(No./100 mi)----Fecal Coliform 160 0 +100

*Base1ine values obtained from App. Tables B.3,B.6, B.8, and B.10.

tBase1ine values obtained from Table 5.

and microorganisms (including plants), (3) volatilization to ammonia gas at

higher pH values, (4) biological oxidation (nitrification of ammonia to

nitrate), and (5) denitrification (reduction of nitrates to nitrogen gas).

According to Lance (l972), a significant amount of the removal of nitro­

gen in soil can be attributed to denitrification and the adsorption of the

ammonium ion. Denitrification of nitrate to nitrogen gas can occur in anae-

Page 32: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

26

Tobic pockets in the soil. The adsorption of the ammonium ion is not a

stable condition because of biological oxidation which can occur, producing

nitrates. However, the temporary adsorption can retain nitrogen in the root

zone of the grass. This retention may provide substantial time for the up­

take of nitrogen by the grass.

The removal of 99.7% of the phosphorus in the Mililani Recycling Project

(Lau et ale 1975) was attributed to soil fixation and/or to uptake by plants

(Goudy 1931; Butler,Orlob, and McGauhey 1954). The high fixing capacity of

the Hawaiian latosols has been confirmed by Fox (1972) .. Taylor (1967) ob­

served that phosphorus applied as fertilizer on a clay soil was converted to

water-insoluble forms within a few hours.

In Table 7, the change in constituent concentrations can be observed

when the sewage effluent passed through the regosol (Jaucas sand atTest Well

2). Losses between 77.2 and 100% of nitrogen, phosphorus, and fecal coliform

occurred. The oxidation of ammonium ion to nitrate, asdlscussed by Lance ..

(1972), accounts for some reduction in ammonia levels and the .large increase

of combined nitrite and nitrate nitrogen (0.3 mg/~ to 1.47mg/~). Movement

of nitrates through the Jaucas sand appeared to be unrestricted as evidenced

by the high concentration in the percolate. The high removal of nitrogen can

be attributed to plant uptake, biological oxidation, volatilization of ammo­

nia, and possible adsorption by the soil.

TABLE 7. MEAN CONSTITUENT CONCENTRATION CHANGEOF APPLIED EFFLUENT THROUGH JAUCASSANDS (TEST WELL NO.2) ON THE KMCASGOLF COURSE

Pond Perc. from PercentConstituent

...Test Wellt ReductionEff 1uen t'-

No. 2

------(mg/~)------~--

NHrN 10.9 0.01 +99.1Organic N 1. 84 0.42 +77.2NOz + N03-N 0.03 1.47 ~-98.0

Total N 12.75 1.82 +85.7Total P 8.9 O. 15 +98.4Cl- 329 447 -'26.4Na 230 306 -24.8K 22 22 0

Fecal ---(No./100 m~)------

Col iform 160 +100

*Baseline values obtained from App. Tables B.3,B.6, B.8, and B.l0.

tBasel ine values obtained from App. Table C.2.

26

Tobie pockets in the soil. The adsorption of the ammonium ion is not a

stable condition because of biological oxidation which can occur, producing

nitrates. However, the temporary adsorption can retain nitrogen in the root

zone of the grass. This retention may provide substantial time for the up­

take of nitrogen by the grass.

The removal of 99.7% of the phosphorus in the Mililani Recycling Project

(Lau et al. 1975) was attributed to soil fixation and/or to uptake by plants

(Goudy 1931; Butler, Grlob, and McGauhey 1954). The high fixing capacity of

the Hmvaiian latosols has been confirmed by Fox (1972). Taylor (1967) ob­

served that phosphorus applied as fertilizer on a clay soil was converted to

water-insoluble forms within a few hours.

In Table 7, the change in constituent concentrations can be observed

when the sewage effluent passed through the regosol (Jaucas sand at Test Well

2). Losses between 77.2 and 100% of nitrogen, phosphorus, and fecal coliform

occurred. The oxidation of ammonium ion to nitrate, as discussed by Lance

(1972), accounts for some reduction in ammonia levels and the large increase

of combined nitrite and nitrate nitrogen (0.3 mgj£ to 1.47 rngj£). Movement

of nitrates through the Jaucas sand appeaTed to be unrestricted as evidenced

by the high concentration in· the peTcolate. The high Temoval of nitTogen can

be attributed to plant uptake, biological oxidation, volatilization of ammo­

nia, and possible adsorption by the soil.

TABLE 7. MEAN CONSTITUENT CONCENTRATION CHANGEOF APPLIED EFFLUENT THROUGH JAUCASSANDS (TEST WELL NO.2) ON THE KMCASGOLF COURSE

ConstituentPond

Effluent;',Perc. fromTest Wellt

No.2

PercentReduction

NH 3-NOrganic NN02 + NOrNTotal NTotal PCl-NaK

FecalCo 1iform

------(mg/£)------~--

10.9 0.011. 84 0.420.03 1.47

12.75 1.828.9 0.15

329 44]230 306

22 22

---(No./100 m£)-----­160

+99.1+77.2-98.0+85.7+98.4-26.4-21f.8

a

+100

*Base1 ine values obtained from App. Tables 8.3,8.6, 8.8, and 8.10.

tBase1 ine values obtained from App. Table C.2.

Page 33: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

27

Phosphorous removal for the Flushing Meadoh's Project (Bouwer, Lance, andRiggs 1974) was due to the precipitation of calcium phosphate compounds,ammonium magnesium phosphate, and other insoluble compounds because the sandand gravels of the infiltration basin contained no iron and aluminum oxidesor other phosphate-fixing material. The high removal of 98.4% phosphorus atTest Well 2 (Jaucas sand) may be due to the alkaline character of the soilattributed to such precipitation as well as plant uptake. However, the shortdistance of percolate travel (3m [9.9 ft]) is suggestive that phosphorous fix­ing occurred. In the Flushing Meadows Project, at least 91 m (300 ft) ofunderground travel was required for 90% removal of phosphorus.·

Percolate from the two test wells in the spray irrigation area (TestWells 2 and 3) contained no fecal coliform bacteria. During the 3-mo. periodof analysis (March, April, and May), no fecal coliform organism was isolatedfrom the test wells. These results are comparable to the Flushing Meadowsand Mililani projects. Surface straining and adsorption are probably themechanisms for the removal of fecal coliform bacteria.

Air Quality

The sampling procedure for air quality was very simple. However, thetechnique was excellent for the collection of air samples in a short timeperiod. Between five and seven air samples could be collected at varyingdo\~wind distances from the green being sprayed with effluent. Alternativesampling methods (vacuum and impinger systems) were too bulky and the sa~plerset-up time too long. This would result in only one air sample collection ateach green.

The agar plate air sampling method was selected because of its simpli­city, versatility, and effectiveness. M-Endo agar culture media was selectedfor air sampling. This media provided the recovery of total. coliform bac­teria that was settling out of the atmosphere. The total coliform bacterialmedia was selected over fecal coliform media because of the high concentra­tion of total coliform bacteria (15,000 and 400,000 colonies/lOa m~) in theeffluent increased the probability of isolating bacterial aerosols from thespray irrigation. The low concentration of fecal coliform bacteria (20 to420 colonies/lOa m ) did not assure the positive recovery of bacterialaerosols.

Air quality analysis at the KMCAS golf course was ·performed during the

27

Phosphorous removal for the Flushing Meadows Project (Bouwer, Lance, and

Riggs 1974) was due to the precipitation of calcium phosphate compounds,

ammonium magnesium phosphate, and other insoluble compounds because the sand

and gravels of the infiltration basin contained no iron and aluminum oxides

or other phosphate-fixing material. The high removal of 98.4% phosphorus at

Test Well 2 (Jaucas sand) may be due to the alkaline character of the soil

attributed to such precipitation as well as plant uptake. However, the short

distance of percolate travel (3m [9.9 ft]) is suggestive that phosphorous fix­

ing occurred. In the Flushing Meadm'ls Project, at least 91 m (300 ft) of

underground travel was required for 90% removal of phosphorus.

Percolate from the two test wells in the spray irrigation area (Test

Wells 2 and 3) contained no fecal coliform bacteria. During the 3-mo. period

of analysis (March, April, and May), no fecal coliform organism was isolated

from the test wells. These results are comparable to the Flushing Meadows

and Mililani projects. Surface straining and adsorption are probably the

mechanisms for the removal of fecal coliform bacteria.

Air Quality

The sampling procedure for air quality was very simple. However, the

technique was excellent for the collection of air samples in a short time

period. Between five and seven air samples could be collected at varying

downwind distances from the green being sprayed with effluent. Alternative

sampling methods (vacuum and impinger systems) were too bulky and the sa~pler

set-up time too long. This would result in only one air sample collection at

each green.

The agar plate air sampling method was selected because of its simpli­

city, versatility, and effectiveness. M-Endo agar culture media was selected

for air sampling. This media provided the recovery of total coliform bac­

teria that was settling out of the atmosphere. TIle total coliform bacterial

media was selected over fecal coliform media because of the high concentra­

tion of total coliform bacteria (15,000 and 400,000 colonies/IOO m~) in the

effluent increased the probability of isolating bacterial aerosols from the

spray irrigation. The low concentration of fecal coliform bacteria (20 to

420 colonies/lOa m ) did not assure the positive recovery of bacterial

aerosols.

Air quality analys is at the KMCAS golf course was performed during the

Page 34: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

28

early evening hours of June 1976. The meteorological and environmental con­

ditions, during each of the sampling periods, are listed Table 8. The condi­

tions existing at the golf course, during the spray irrigation, were consid­

ered to be the optimal conditions for the survival of bacterial aerosols.

Adams and Spendlove (1970) obtained the greatest recoveries of bacterial

aerosols during periods of high relative humidity, 1mV' temperature, high wind

velocities, and darkness. Solar radiation during the daylight hours had a

deleterious effect on the recovery rates of coliforms. Twilight and evening

operation of the sprinkler system eliminated the adverse effect of solar ra­

diation. Clark (1974) also noted that ultraviolet radiation in sunlight may

result in the higher death rate of bacteria.

The results of ai~ sampling are reported in Table 9. This actually rep­

resents the fallout concentration of coliform bacterial aerosols and not of

the concentration of bacteria in the air. The coliform bacteria isolated on

the agar dishes are those that are settling out of the atmosphere. A zero

colony isolation for this study does not necessarily mean the nonexistence

of coliform bacterial aerosols.

The graphical relationship between agar dish densities of total coliform

bacteria and the downwind distances from the sprinkler sources are in Figures

12 to 15. No distinct pattern of bacterial fallout is discernable in the

graphs. Variations in wind velocities and initial coliform densities (from

the sprinkler effluent) resulted in varying recovery rates of the' coliform

bacteria.

Data plots were normalized in an attempt to dampen the effects of the

varied initial coliform concentrations. The highest coliform plate density

collected for each sampling set was assigned a value of 100%. This reference

plate assignment was independent of the downwind distance from the sprinkler

source because the highest plate density occurred at varying downwind dis­

tances. All the other coliform plate densities, for the respective set, were

then assigned a percentage with respect to the reference plate. Table 10

lists the results of the normalized data.

The normalized air quality data was plotted with respect to the downwind

distances (Figs. 16 to 19). In Appendix D, the graphs were grouped with re­

spect to the various ini tial effluent coliform concentrations (15 , 000 to

20,000 colonies/lOO mQ" 46,000 colonies/IOO m!l.,and 319,000 to 400,000 colo­

nies/IOO m!l.). Appendix E presents the normalized data with respect to the

varying \\find velocities (0 to 8 kn, 9 to 12 kn, and 13 to 18 kn) .In all

28

early evening hours of June 1976. The meteorological and environmental con­

ditions, during each of the sampling periods, are listed Table 8. The condi­

tions existing at the golf course, during the spray irrigation, were consid­

ered to be the optimal conditions for the survival of bacterial aerosols.

Adams and Spendlove (1970) obtained the greatest recoveries of bacterial

aerosols during periods of high relative humidity, low temperature, high wind

velocities, and darkness. Solar radiation during the daylight hours had a

deleterious effect on the recovery rates of coliforms. Twilight and evening

operation of the sprinkler system eliminated the adverse effect of solar ra­

diation. Clark (1974) also noted that ultraviolet radiation in sunlight may

result in the higher death rate of bacteria.

The results of ai:;: sampling are reported in Table 9. This actually rep­

resents the fallout concentration of coliform bacterial aerosols and not of

the concentration of bacteria in the air. The coliform bacteria isolated on

the agar dishes are those that are settling out of the atmosphere. A zero

colony isolation for this study does not necessarily mean the nonexistence

of coliform bacterial aerosols.

The graphical relationship between agar dish densities of total coliform

bacteria and the downwind distances from the sprinkler sources are in Figures

12 to 15. No distinct pattern of bacterial fallout is discernable in the

graphs. Variations in wind velocities and initial coliform densities (from

the sprinkler effluent) resulted in varying recovery rates of the coliform

bacteria.

Data plots were normalized in an attempt to dampen the effects of the

varied initial coliform concentrations. The highest coliform plate density

collected for each sampling set was assigned a value of 100%. This reference

plate assignment was independent of the downwind distance from the sprinkler

source because the highest plate density occurred at varying downwind dis­

tances. All the other coliform plate densities, for the respective set, were

then assigned a percentage with respect to the reference plate. Table 10

lists the results of the normalized data.

The normalized air quality data was plotted with respect to the downwind

distances (Figs. 16 to 19). In Appendix D, the graphs were grouped with re­

spect to the various initial effluent coliform concentrations (15,000 to

20,000 colonies/laO ~, 46,000 colonies/laO m£, and 319,000 to 400,000 colo­

nies/lOa m£). Appendix E presents the normalized data with respect to the

varying \vind velocities (0 to 8 kn, 9 to 12 kn, and 13 to 18 kn). In all

Page 35: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

29TABLE 8. METEOROLOGICAL, ENVIRONMENTAL, AND BACTERIOLOGICAL CONDITIONSDURING AIR SAMPLING ON THE KMCAS KLIPPER GOLF COURSE

Rei. Wind Vel. Wind TotalTime'-' Green Temp. Humidity and Range Dir. Coliform -r(PM) (No.) (oF) . (%) (kn)· (#/100 m£)6:45 16 75 76 10 ENE 15,000

9-127:30 2 75 .76 2 ENE 15,000

1-86:45 16 76 69 7 ENE 16,000

6-8.57:00 15 76 69 10 ENE 16;000·

8-116:20 PGr 76 66 4 ENE 17,000

3-56:45 16 76 66 4 ENE 17,000

3-57:00 15 76 66 4 ENE 17,000

3-56:20 PGt 76 69 4 ENE 319,000

3-57:00 1576 69 5 ENE 319,000

5-:-76:20 PG~ 76 79 9 ENE 46,000

8-116:45 16 76 79 9 ENE 46,000

8-11. 57:00 15 76 79 10 ENE 46,000

9-137:30 2 76 79 7 ENE 46,000

6-9.56:20 PGt 75 87 10 ENE 400,000

9-14.56:45 16 75 87 10 ENE 400,000

9-14.57:00 15 75 87 14 ENE 400,000

12-18

Date(1976)

June 9

June 9

June 10

June 10

June 11

June 11

June 11

June 12

June 12

June 14

June 14

June 14

June 14

June 16

June 16

June 16

June 16 7:30 2 75 87 97-13

ENE 400,000

*Starting time for the 15-min spray irrigation of the greens.tl nitia1 concentration found in the sprinkler effluent.fPutting green.

29

TABLE 8. METEOROLOG ICAL, ENVIRONMENTAL, AND BACTERIOLOGICAL CONDITIONSDURING AIR SAMPLING ON THE KMCAS KLIPPER GOLF COURSE

Re I. Wind Vel. \lInd TotalDate Time'-' Green Temp. Humidity and Range Oi r. Coliform-r

( 1976) (PM) (No. ) ( oF) (%) (kn) (#/100 m£)

June 9 6:45 16 75 76 10 ENE 15,0009-12

June 9 7:30 2 75 76 2 ENE 15,000~

1-8

June 10 6:45 J6 76 69 7 ENE 16,0006-8.5

June 10 7:00 15 76 69 10 ENE 16,0008-11

June 11 6:20 PGt 76 66 4 ENE 17,0003-5

June 11 6:45 16 76 66 4 ENE 17,0003-5

June 11 7:00 15 76 66 4 ENE 17,0003-5

6:20J.

76 69 4June 12 PGt ENE 319,0003-5

June 12 7:00 15 76 69 5 ENE 319,0005-7

June 14 6:20 PGf 76 79 9 ENE 46,0008- J 1

June 14 6:45 16 76 79 9 ENE 46,0008-11 .5

June 14 7:00 15 76 79 10 ENE 46,0009-13

June 14 7:30 2 76 79 7 ENE 46,0006-9.5

June 16 6:20 PGf 75 87 10 ENE 400,0009-14.5

June 16 6:45 16 75 87 10 ENE 400,0009-14.5

June 16 7:00 15 75 87 14 ENE 400,00012-18

June 16 7:30 2 75 87 9 ENE 400,0007-13

*Starting time for the IS-min spray irrigation of the greens.tl nitia1 concentration found in the sprinkler effluent.:FPutting green.

Page 36: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

30

TABLE 9. AIR SAMPLING RESULTS OF AEROSOLIZED COLIFORM BACTERIACOLLECTED AT THE KMCAS KLIPPER GOLF COURSE

Upwind Downwind Distance l ( i n ft)

Date Time Green Con- -75 -100 -125 -150 -200· -250 -300(1976) (PH) (No. ) t ro 1 (No .. tota 1 col iform colonies/plate)

June 9 6:45 16 0 4 2 ";'~ 0 0 0 0June 9 7:30 2 0 7 1 It, 0 0 "l: "';~

June 10 6:45 16 0 2 1 2 3 2 0 '";'~

June 10 7:00 15 0 15 13 0 0 '1~ '1: -;',

June 11 6:20 PGt 0 -;': 1 a *~ * ,'~ .;:

June 11 6:45 16 a 10 3 10 0 1 aJune 11 7:00 15 0 9 7 2 0 4 ";" oJ:

June 12 6:20 PGt a 5 5 2 2 0 1 aJune 12 . 6:45 16 0 4 5 12 2 2 5 1June 12 7:00 15 a 64 24 19 7 5 i':: ?'-;

June 14 6:20 PGt 0 11 6 8 8 2 10 0June 14 6:45 16 0 37 42 80 43 21 10 6June 14 7:00 15 0 311 86 36 4 14 ~~ '1::

June 14 7:30 2 0 107 25 25 12 7 * *June 16 6:20 PGt 0 12 10 8 5 3 2 1June 16 6:45 16 0 77 36 38 38 35 13 8June 16 7:00 15 0 109 ,,;':: 1 2 25 ";': *June 16 7:30 2 0 86 75 95 21 15 ,;':: -;'"

IFrom sprinkler source.*No sample collectedtPutting green.

TABLE 10. NORMALJ ZED DATA FOR THE AIR SAMPL ING ATTHE KMCAS KLIPPER GOLF COURSE

Date Green Downwind Distance ( in ft)-75 -100 -125 -150 -200 -250 -300

(1976) (No. )

June 9 16 100 50 * 0 a 0 aJune 9 2 100 14 ~': 0 0 oJ:: i~

June 10 16 67 33 67 100 67 0 ;~

June 10 15 100 87 0 0 ";'; * iT;

June 11 PGt oj:: 100 0 -;" oJ:: ,,;': *June 11 16 100 30 100 0 10 0 10June 11 15 100 78 22 0 44 * *June 12 PGt 100 100 40 40 a 20 0June 12 16 33 42 100 17 17 42 8June 12 15 100 38 30 27 8 ':I': 1:

June 14 PGt 100 55 73 73 18 91 aJune 14 16 46 53 100 54 26 13 8June 14 15 100 28 12 1 5 ,,;':: 1::

June 14 2 100 23 23 11 7 ;':: "";~

June 16 PGt 100 83 67 42 25 17 8June 16 16 100 48 49 49 45 17 10June J6 15 100 ,,;':: 1 2 23 ";'\ it,

June 16 2 91 80 100 22 16 ;':: ·k

;'~No samp 1e collected.tPutting green.

Page 37: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

31

10

0 6/09, No. 2w 0 6/09, No. 16f- B<t: 6/10, No . 16....J •a. 6/11, No. 15........ l:>

.U'lW D, 6/11, P.G.-:z:0 6 0 6/12, P.G.. ....J0u

<t:

ecu.!f-u -4.:r.o:l

::<::0:::: -0

.!.L.~

....J0 -2u

O'__ __'___...u..__"'--.,----'-_~-%J<"':--....L...---'----'---;u

-75 -100 -125 -150 -200 -250 -300DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ft \

FIGURE 12. COLIFORM BACTERIA DENSITIES DOWNWIND OF SPRAYIRRIGATION SOURCE

wf-<t:....Ja.........U'lW

Z0....J0u

<t:

ecwf-uc:(en

:::<::~

0I.L..

....J0U

15

0 6/10 No. 150 6/11 No. 16 .

6/12 16l:> No.

D, 6/14 P.G.10

0 6/16 P.G.

5

O'-_--'-.,--_-A-__==--- -'-----,. -="'-- ...<J

·-75 -100 -125 -150 -200 -250 -300DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ft

FIGURE 13. COLIFORM BACTERIA DENSITIES "DOWNWIND O~.SPRAY

IRRIGATION SOURCE

31

10

0 6/09, No. 2uJ 0 6/09, No. 16I- 8« 6/10, No . 16-l •0- 6/11, No. 15........ 6.V"luJ

b,. 6/11, P.G.:z.c 6 0 6/12, P.G.. -l0U

«0::wI-u -4«ca~0::: -0

.LL...:.-.-l0 -2u

0-75 -100 -125 -150 -200 -250 -30~

DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ftFIGURE 12. COLIFORM BACTERIA DENSITIES DO\·nI'.4 IND OF SPRAY

IRRIGATION SOURCE

15

L.LJ 0 6/10 No. 15I- 6/11 No. 16-« 0-li:L 6. 6/12 No. 16........V"l

6/14uJ b,. P.G.:z: 10- .0 0 6/16 P.G.-l0U

«0::uJI-u

5«co

:=::~

0LL

-l0U

0'-75 -100 -125 -150 -200 -250 -300

DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ft

FIGURE 13. COLIFORM BACTERIA DENSITIES DOWNVIND OF SPRAYIRRIGATION SOURCE

Page 38: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

-.1.0- i

j~200 -250 -300

IRRIGATION SPRINKLERS, ftDOWNWIND OF A SPRAY IRRIGATION SOURCE

OL-_-,L-_-"......=~_--JL-_-,l.-_----l__-L-_----i._~

',75 -100 -125 -150DOWNWIND DISTANCES FROM

14. COLIFORM BACTERIA DENSITIES320 ~----,---...-----r---.--------r----.-------,r----r---'---;

32 120

° 6/12 No, 150 6/14 No. 2

• 6/14 No . 16lJJ

A 6/i6 No. 2I-« 6/16 No, 15...J ...a.......... o 6/16 No, 16V> 80w

z0...J0U

«0::wI-u«co

r 400';0lL.

...J0U

FI GURE

° 6/14 No. 15wI-«...J 240a..........V>W

Z0...J0U

« 1600::wI-u«co

20lL. 80...J0U

0L--_---l.__-L.__.l.L--...,..-_L-_-.L__-'-_---:~----J'---_:_'

~75 -100 -125 -150 -200 -250 -300DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ft

FIGURE 15. COLIFORM BACTERIA DENSITIES DOWNWIN~ OF A SPRAY lRRIGATION SOURCE

~200 -250 -300IRRIGATION SPRINKLERS, ftDOW'NWIND OF. A SPRAY IRRIGATION SOURCE

o'"75 -100 -125 -150

DOWNWIND DISTANCES FROM14•. COLIFORM BACTERIA DENSITIES

320

0 6/14 No. 15wI-«....:I 2400...--...tilW

:z0....J0U

« 160a:::wI-u«co

.~a:::0l.1.. 80....J0U

o-75 -100 -125 -150 -200 -250 . -300

DOWNHIND DISTMCES FROM IRRIGATION SPRINKLERS, ftFIGURE 15. COLIFORM BACTERIA DENSI.TIES DOWNWIN~ OF A SPRAY IRRIGATION SOURCE

32120

0 6/12 No. 150 6/1 Lf No. 2

• 6/14 No . 16w

.b. 6/i6 No. 2l-e:(

6/16 No . 15....J ....0...--... o 6/16 No. 16VJ 80w

z0....J0U

e:(

a:::wI-u«co

~ 40cr~

0l.1..

....J<)

U

FIGURE

Page 39: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

33

0 6/096/140

6/16A

50

>­t-

::E0:::o\J..

....JoU

r.nzUJa

100 cr-----,-----,;r--...----r---.---.---,.--------,---~

«.. 0:::

UJt­u«co

....J.«::Ea:.oz

OL--_-..L__-'-_~_=___ _"'__""'O'__~ ~_"____4

-75 -150 -225 -300DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS

0 6/10o 6/11A 6/12

6/14•• 6/16

....Jou

aUJN

FIGURE 16. NORMALIZED AIR QUALITY PATA FOR THE NO.2 GREEN

100

«0:::UJt­u«co::E 500:::o\J..

r.n:z:UJa

~

>­t-

....J«::Ecr:o:z:

o L_.1...-__i!t:::::::::lt::::::=:~_ __l........c._---L.-_ __l...__ _L__...J-75

FIGURE 17. NORMALIZED AIR QUALITY DATA FOR THE NO. 15 GREEt"

a 6/09o 6/14[:, 6/16

-150 -225 -300DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS

NORMALIZED AIR QUALITY DATA FOR THE NO.2 GREEN

o 6/10o 6/11[:, 6/12• 6/14• 6/16

o L_.1---__k::==:::::lf::::::::::~_...L....o..._ _L..__ ___l..__ ___1.__....J-75 -150 -225 -300

DOWNWIND DiSTANCES FROM IRRIGATION SPRINKLERS

FIGURE 17. NORMALIZED AIR QUALITY DATA FOR THE NO. 15 GREEN

33

Page 40: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

III

. I

0 6/090 6/10Do 6/11

• 6/12

• 6/14.... 6/16

06/11o 6/12Do 6/14• 6/16

-100 -125"'" 150 -200 -250 -30P~~DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ft ".

FIGURE 18: ~ORMALIZED AIR QUALITY DATA FOR THE NO~ 16 GREEN

100 .,....---.::.._---r-,----,.--~-.._-_r--.,_--_r_-__,~~__,

0'---~'__--.:A---:_=_:~-~-_::":7_---'--__::_':_:_--'----IJ-75 -100 -125 -150 -250 -300

DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ftFIGURE 19. NORMALIZED AIR QUALITY DATA FOR THE PUTTING GREEN

~

>­r

oWN

...J<:t:::::a:::oz

:::::a:::oLL.

...JoU

34

100

&<

>-rV'l:zw0

<:t

0::wru.«co 50:::::0::0LL.

...J0U

0IJ-!N

...J<:t

~0z

0-75

o 6/09o 6/10[:,. 6/11• 6/12• 6/14A 6/16

-100 -125-150 -200 . -30p::DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ft'

FIGURE 18: NORMALIZED AIR QUALITY ,DATA FOR THE NO, 16 GREEN

100

eN

~

>-I-

Vl:<:::LLJCl

c:l::

c:::LLJI-uc:l::co:::;:c:::0~

-'0U

ClLLJN

-'«:::;:c:::0:z

a-75

FIGURE

06/11o 6/12[:,. 6/14• 6/16

-100 -125 -150 -200 '-250 . -300,DOWNWIND DISTANCES FROM IRRIGATION SPRINKLERS, ft

19. NORMALIZED AIR QUALITY DATA FOR THE PUTTING GREEN

Page 41: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

35three cases, there was still no distinct pattern in the distribution of aero­sols containing coliform bacteria. However, general trends can be observedin the normalized curves. An approximately 90% decrease in coliform bacteriaconcentration was observed within 91 m downwind of sprinkler heads. Windvelocities during the air sample collection affected the recovery patterns.Wind velocity ranges of 0 to 8 kn (low) and 13 to 18 kn (high) resulted in arapid decrease in bacterial aerosols within 46 m(150 ft) dowmvindof thesprinklers. The mid-range wind velocity (9 to 12 kn) did not appear to fol­low the pattern. It is possible that, between 9 and 12 kn, more irregular"gust:lng" may occur. This could result in the "masking" of the normal set­tling pattern of the bacteria.

The presence of aerosols containing pathogenic organisms can only be.im­plied by this study. The presence of aerosols of coliform bacteria mayormay riot be·indicative of the presence of pathogens in these aerosols. How­ever, even the presence of coliform bacteria in the air poses a very seriousquestion: is the continued use of the KMCAS STP effluent for spray irriga~

tion on the golf course safe?The health hazards from the spray irrigation system must be similar to

that from other systems that generate aerosolized coliform bacteria. In paststudies, activated sludge and trickling filter plants have been examined, andfound to be positive, for the emission of aerosols of coliform bacteria (Led­better and Randall 1965; Adams and Spendlove 1970; King, Mill, and Laurence1973).

From the present air sampling results at the KMCAS Klipper Golf Course,three observations can be made:

1. Aerosols of coliform bacteria can be found at least 91 m downwindfrom the spray irrigation sprinkler source.

2. Higher concentrations of coliform bacteria in the sprinkler effluentresulted in recovery of a greater concentration of aerosolized bac­teria and at greater distances from the source.

3. The downwind transport of aerosolized coliform bacteria was depen­dent on wind velocity. Higher wind velocities for a s.imilar efflu­ent concentration of coliform bacteria resulted in the isolation ofbacteria at greater distances from the source.

The results of the air quality analysis were obtained at the optimumcondition (high relative humidity, high wind velocities, darkness, and mildtemperatures) for the recovery of· bacteria emitted by spray irrigation with

35

three cases, there was still no distinct pattern in the distribution of aero-

sols containing colifonn bacteria. HO\",rever, general trends can be observed

in the normalized curves. An approximately 90% decrease in coliform bacteria

concentration was observed within 91 m downwind of sprinkler heads. Wind

velocities during the air sample collection affected the recovery patterns.

Wind velocity ranges of 0 to 8 kn (low) and 13 to 18 kn (high) resulted in a

rapid decrease in bacterial aerosols within 46 m (150 ft) downwind of the

sprinklers. The mid-range wind velocity (9 to 12 kn) did not appear tofol­

low the pattern~ It is possible that, between 9 and 12 kn, more irregular

"gusting" may occur. This could result in the "masking" of the nonnal set­

tling pattern of the bacteria.

The presence of aerosols containing pathogenic organisms can only beim­

plied by this study. The presence of aerosols of coliform bacteria mayor

may not be·indicative of the presence of pathogens in these aerosols. How­

ever, even the presence of colifonn bacteria in the air poses a very serious

question: is the continued use of the KMGAS STP effluent for spray irriga-:­

tion on the golf course safe?

The health hazards from the spray irrigation system must be similar to

that from other systems that generate aerosolized coliform bacteria. In past

studies, activated sludge and trickling filter plants have been examined, and

found to be positive, for the emission of aerosols of colifonn bacteria (Led­

better and Randall 1965; Adams and Spendlove 1970; King, Mill, and Laurence

1973) .

From the present air sampling results at the ~lCAS Klipper Golf Course,

three observations can be made:

1. Aerosols of coliform bacteria can be found at least 91 m downwind

from the spray irrigation sprinkler source.

2.. Higher concentrations of colifonn bacteria in the sprinkler effluent

resulted in recovery of a greater concentration of aerosolized bac­

teria and at greater distances from the source.

3. The doWnwind transport of aerosolized colifonn bacteria was depen­

dent on \vind velocity. Higher wind ve locities for a similar efflu­

ent concentration of coliform bacteria resulted in the isolation of

bacteria at greater distances from the source.

The results of the air quality analysis were obtained at the optimum

condition (high relative humidity, high wind velocities, darkness, and mild

temperatures) for the recovery of· bacteria emitted by spray irrigation with

Page 42: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

36

sewage effluent; therefore, this probably represents the extreme condition

for public health and safety. However, at this extreme condition, the levels

and range of indicator bacterial emissions from the KMCAS spray irrigation

system are still lower than those reported for most trickling filter and

activated sludge units at waste water treatment plants. The incidence of

disease directly due to bacterial aerosols to sewage treatment plant workers

has not been reported in the literature (Hickey and Reist 1975). On this

basis, the continued use of sewage effluent for spray irrigation at the KMCAS

Klipper Golf Course should not be considered a health hazard.

CONCLUS IONS

The following conclusions may be drawn from the results of this study:

1. The KMCAS raw sewage is a weak se\vage of fairly consistentquality

2. The KMCAS sewage treatment plant achieves a high overall efficiency

through its biological process and final polishing pond

3. Settling of organic matter and the biological uptake resulted in

the decrease of BODs, suspended solids, and organic nitrogen in the

KMCAS STP polishing pond

4. The quality of the effluent from theKMCAS STP appears to be a good

source of irrigation water for the KMCAS KlipperGolf Course

5. The effective removal of nitrogen, phosphorus, and fecal coliform

bacteria on the KMCAS golf course can be attributed to the bermuda­

grass soil cover, the Ewa silty clay (low humic latosol soil group),

and the Jaucas sand (regosols soil group)

6. On the basis of nitrogen, phosphorus, and fecal coliform bacteria,

the quality of the percolate from the effluent-irrigated golf course

soil does not detrimentally alter the quality of the groundwater.

7. On the basis of total Kjeldahl nitrogen, combined nitrate and

nitrite nitrogen, and total phosphorus, the quality of runoff from

the KMCAS golf course is not a source of contamination for the adj a­

cent surface waters

8. Airborne coliform bacteria were isolated up to 91 m downwind of

various effluent sprinkler sources. Higher concentrations of coli­

form bacteria in the sprinkler effluent resulted in greater recovery

of bacterial aerosols and at farther distances downwind from the

36

sewage effluent; therefore, this probably represents the extreme condition

for public health and safety. However, at this extreme condition, the levels

and range of indicator bacterial emissions from the KMCAS spray irrigation

system are still lower than those reported for most trickling filter and

activated sludge units at waste water treatment plants. The incidence of

disease directly due to bacterial aerosols to sewage treatment plant workers

has not been reported in the literature (Hickey and Reist 1975). On this

basis, the continued use of sewage effluent for spray irrigation at the KMCAS

Klipper Golf Course should not be considered a health hazard.

CONCLUS IONS

The following conclusions may be drawn from the results of this study:

1. The KMCAS raw sewage is a weak sewage of fairly consistent quality

2 . The KMCAS sewage treatment plant achieves a high overall efficiency

through its biological process and final polishing pond

3. Settling of organic matter and the biological uptake resulted in

the decrease of BODs, suspended solids, and organic nitrogen in the

KMCAS STP polishing pond

4. The quality of the effluent from theKMCAS STP appears to be a good·

source of irrigation water for the KMCAS KlipperGolf Course

5. The effective removal of nitrogen, phosphorus, and fecal coliform

bacteria on the KMCAS golf course can be attributed to the bermuda­

grass soil cover, the Ewa silty clay (low humic latosol soil group),

and the Jaucas sand (regosols soil group)

6. On the basis of nitrogen, phosphorus, and fecal coliform bacteria,

the quality of the percolate from the effluent-irrigated golf course

soil does not detrimentally alter the quality of the groundwater.

7. On the basis of total Kjeldahl nitrogen, combined nitrate and

nitrite nitrogen, and total phosphorus, the quality of runoff from

the KMCAS golf course is not a source of contamination for the adj a­

cent surface waters

8. Airborne coliform bacteria were isolated up to 91 m downwind of

various effluent sprinkler sources. Higher concentrations of coli­

form bacteria in the sprinkler effluent resulted in greater recovery

of bacterial aerosols and at farther dist.ances downwind from the

Page 43: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

37

source. Coliform baCteria density downwind from the source was alsodependent on wind velocity.

9. The reuse of sewage effluent for the spray irrigation of the KMCASgolf course is an effective method of waste water disposal and canbe continued, as well as expanded, to other areas of the !O'ICAS.

ACKNOWLEDGr~ENTS

The authors would like to thank Melvyn A. Yoshinaga, Chief Engineer,Department of Public Works; Jeffrey P. Havlin, Field Superintendant, Depart­ment of Public Works; Lt. Col. David L. Ross, Services and Recreation Officer,and Francis Reynon, Klipper Golf Course Manager, of the Kane 'oheMarine CorpsAir Station for their assistance and cooperation during this research.

REFERENCES·

Ackerson, R.C., and Younger, V.B. 1975. Responses of Bermuda grass tosalini ty. Agron. Jour. 67 :678-8l.Adams, A.P., and Spendlove, J.C. 1965. Coliform aerosols emitted by sewagetreatment plants. Science 169 (9) :1218-20.Bouwer, H.; Lance, J.C.; and Riggs, M.S. 1974. High-rate land treatment.II. Water quality and Economic aspects of the Flushing Meadows project.Jour. Water Poll. Control Fed. 46(5) :844-59.Brown, J.H.; Cook, K.M.; Ney, F.G.; and Hatch, T. 1950. Influence of par­ticle size upon the retention of particulate matter ln the human lung.Amer. Jour, Pub. Health 41:450-59.Butler, R.G.; Or1ob, G.T.; and McGauhey, P.H. 1954. Underground movement ofbacterial and chemical pollutants. Jov~. ArneI'. Water Works Assn. 46(2):97­Ill.

Chu, A.C., and Sherman, G.D. 1952. Differential fixation of phosphate by'typical soils of the HCJh)aii Great Soil Groups. Tech. BulL 16, Agricul­. tura1 Experiment Station, University of Hawaii.Chun, M.J.; Young, R.H.F.; and Anderson; G.K. 1972. Wastewater effluentsand surface runoff quality. Tech. Rep. No. 63, Water Resources ResearchCenter, University of Hawaii.Clark, W.N. 1974. A comparison of numbers of aerosolized coliforms asso­ciated \;'i th sewage treatment by the trickling filter and the activatedsludge processes. A report submitted to the University of Hawaii Schoolof Public Health.

Coleman, R. 1944. Phosphate fixation by the coarse and fine clay fractionsof kaolinitic and montmori11onitic clays. Soil Sci. 58:71-77.

37

source. Coliform bacteria density downwind from the source was also

dependent on wind velocity.

9. The reuse of sewage effluent for the spray irrigation of the KMCAS

golf course is an effective method of waste water disposal and can

be continued, as well as expanded, to other areas of the IO'!CAS.

ACKNOWLEDGr~ENTS

The authors would like to thank Melvyn A. Yoshinaga, Chief Engineer,

Department of Public Works; Jeffrey P. Havlin, Field Superintendant, Depart­

ment of Public Works; Lt. Col. David L. Ross, Services and Recreation Officer,

and Francis Reynon, Klipper Golf Course Manager, of the Kane'ohe Marine Corps

Air Station for their assistance and cooperation during this research.

REFERENCES

Ackerson, R.C., and Younger, V.B. 1975. Responses of Bermuda grass tosalinity. Agron. Jour. 67:678-81.

Adams, A.P., and Spendlove, J.C. 1965. Coliform aerosols emitted by sewagetreatment plants. Science 169(9):1218-20.

Bouwer, H.; Lance, J.C.; and Riggs, M.S. 1974. High-rate land treatment.II. Water quality and Economic aspects of the Flushing Meadows project.Jour. Water Poll. Control Fed. 46(5) :844-59.

Brown, J.H.; Cook, K.M.; Ney, F.G.; and Hatch, T. 1950. Influence of par­ticle size upon the retention of particulate matter in the human lung.Amer. Jour. Pub. Health 41:450-59.

Butler, R.G.; Orlob, G.T.; and McGauhey, P.H. 1954. Underground movement ofbacterial and chemical pollutants. Jov~. Amer. Water Works Assn. 46(2):97­Ill.

Chu, A.C., and Sherman, G.D. 1952. Differential fixation of phosphate bytypical soils of the Hawaii Great Soil Groups. Tech. Bull. 16, AgriCUl­tural Experiment Station, University of Hawaii.

Chun, M.J.; Young, R.H.F.; and Anderson, G.K. 1972. Waste0ater effluentsand surface runoff quality. Tech. Rep. No. 63, Water Resources ResearchCenter, University of Hawaii.

Clark, W.N. 1974. A comparison of numbers of aerosolized coliforms asso­ciated with sewage treatment by the trickling filter and the activatedsludge processes. A report submitted to the University of Hawaii Schoolof Public Health.

Coleman, R. 1944. Phosphate fixation by the coarse and fine clay fractionsof kaolinitic and montmoril1onitic clays. Soil Sci. 58:71-77.

Page 44: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

38

Druet, H.A.; Henderson, D.W.; Packman, L.P.; Peacock,S. 1953 .. Studies onrespiratory infection. I. The influence of particle size on respiratoryinfection 1'lith anthrax spores. Jour. Hyg. 51:359-7L

Dye, E.O. 1958. Crop irrigation with se\'lage effluent-Sew. & Ind. Wastes·30(6):825-28.

E1-Swaify, S.A., and Swinda1e, L.D. 1968. Hydraulic conductivity of sometropical soils as a guide to irrigation water quality. 9th InternationalCongress of SoiZ Science Transactions, vol. 1, paper 40.

Foote, D.E.; Hill, E.L.; Nakamura S.; and Stevens, F. 1972. Soil survey ofislands of Kauai., Oahu., Maui., Molokai.) and Lanai.) state of HaLJaii. u.s.Department of Agriculture Soil Conservation Service, in cooperation withthe University of Hawaii Agricultural Experiment Station. .

Fox, R.L. 1972. Solubility, uptake and leaching of plant nutrients: Phos­phate, sulfate and calcium. In Proc. 5th HaLJaii Fertilizer Conference,pp. 25-32, Misc. Pub. 86, Cooperative Extension Service, University ofHawaii.

Goudey, R.F. 1931. Reclamation of treated sewage. JoUr'. Amer. Water WorksAssn. 23:230-40.

. . .'.

Hickey, J.L.S., Reist, P.C. 1975. Health significance of airborne micro-organisms from wastewater treatment processes. Part 1. Summary of investi­gations. Jov.r. fvater Poll. Control Fed. 47(12) :2741-73.

Houser, E.W. 1970. Santee project continues to show the way. Water &Wastes Eng. 7(5):40-44.

King, E.n.; Mill, R.A.; and Lawrence, C.H. 1973. Airborne bacteria from anactivated sludge plant. Jour. Environ. Health 36(1):50-54.

Lance, J.C. 1972. Nitrogen removal by soil mechanisms. Jour. Water Pall.Control Fed. 44(7):1352-61.

Lau, L.S.; Ekern, P.C.; Loh, P.C.S.; Young, R.H.F.; Burbank, N.C., Jr.; andDugan, G.L. 1975. Water recycling of sewage effZuent by irrigation: Afield study on Oahu. Tech. Rep. No. 94,Water Resources Research Center,University of Hawaii. .

Ledbetter, J.O., and Randall, C.W. 1965. Bacterial emissions from activatedsludge units. Industrial Medicine & Surgery 32 (2) :130-33.

McGauhey, P.H. Engineering management of water quali-ty. New York: McGraw­Hill.

McMichael, F.C., and McKee, J.E. 1966. Wastewater reclamation at WhittierNarrows, State of California Resources Agency. Pub. No. 33, State WaterQuality Control Board, California.

Merrell, J.C., Jr. 1968. Virus control at the Santee, California project.Jour. Amer. Water Works Assn. 60(1) :145-53.

Merz, R. C. 1956. Direct utilization of waste waters. Proc. llth IndustrialWaste Conference.

Metcalf and Eddy, Inc. 1972. Wastewater engineering. New York: McGraw,­Hill.

State of Hawaii. 1974. Water quality standards. Public :health regulations.chaps. 37-A and 38.

38

Druet, H.A.; Henderson, D.W.; Packman, L.P.; Peacock, S. 1953. Studies onrespiratory infection. I. The influence of particle size on respiratoryinfection with anthrax spores. JoUX'. Hyg. 51:359-71.

Dye, E.G. 1958. Crop irrigation with sewage effluent. Sew. & Ind. Wastes30(6):825-28.

El-Swaify, S.A., and Swindale, L.D. 1968. Hydraulic conductivity of sometropical soils as a guide to irrigation water quality. 9th InternationalCongress of Soil Science Transactions, vol. 1, paper 40.

Foote, D.E.; Hill, E.L.; Nakamura S.; and Stevens, F. 1972. Soil sv~vey ofislands of Kauai~ Oahu~ Maui~ Molokai~ and Lanai~ state of Hawaii. U.S.Department of Agriculture Soil Conservation Service, in cooperation withthe University of Hawaii Agricultural Experiment Station.

Fox, R.L. 1972. Solubility, uptake and leaching of plant nutrients: Phos­phate, sulfate and calcium. In Froc. 5th Hawaii Fertilizer Conference,pp. 25-32, Misc. Pub. 86, Cooperative Extension Service, University ofHawaii.

Goudey, R.F. 1931. Reclamation of treated sewage. JoUX'. Amer. Water WorksAssn. 23:230-40.

Hickey, J.L.S., Reist, P.C. 1975. Health significance of airborne micro­organisms from wastewater treatment processes. Part 1. Summary of investi­gations. Jov~. Water Poll. Control Fed. 47(12) :2741-73.

Houser, E.W. 1970. Santee project continues to show the way. Water &Wastes Eng. 7(5):40-44.

King, E.D.; Mill, R.A.; and Lawrence, C.H. 1973. Airborne bacteria from anactivated sludge plant. Jour. Environ. Health 36(1):50-54.

Lance, J.C. 1972. Nitrogen removal by soil mechanisms. JoUX'. Water Poll.Control Fed. 44(7):1352-61.

Lau, L.S.; Ekern, P.C.; Loh, P.C.S.; Young, R.H.F.; Burbank, N.C., Jr.; andDugan, G.L. 1975. Water recycling of sewage effluent by irrigation: Afield study on Oahu. Tech. Rep. No. 94, Water Resources Research Center,University of Hawaii.

Ledbetter, J.G., and Randall, C.W. 1965. Bacterial emissions from activatedsludge units. Industrial Medicine & Surgery 32 (2) :130-33.

McGauhey, P.H. Engineering management of water quality. New York: McGraw­Hill.

McMichael, F.C., and McKee, J.E. 1966. Wastewater reclamation at WhittierNarrows, State of California Resources Agency. Pub. No. 33, State WaterQuality Control Board, California.

Merrell, J.C., Jr. 1968. Virus control at the Santee, California project.Jour. Amer. Water Works Assn. 60(1) :145-53.

Merz, R. C. 1956. Direct utilization of waste waters. Froc. Uth IndustrialWaste Conference.

Metcalf and Eddy, Inc. 1972. fvastewater engineering. New York: McGraw­Hill.

State of Hawaii. 1974. Water quality standards. Public health regulations~

chaps. 37-A and 38.

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39

Tanimoto, R.M.; Burbank, N.C., Jr.; Young, R.H.F.; and Lau, L.S. 1968.Migration of bacteriophage TIf in percolating water through selected Oahusoils. Tech. Rep. No. 20, Water Resources Research Center, Universith ofHawaii.

Taylor, A.W. 1967. Phosphorus and water pollution. Jour. Soit & ivater Cons.22(6):228-30.

U.S., Congress, Senate. 1972. Federal ~later Pollution Control Act cunend­ments of 1972. Public Law 92-500, 92d Cong., S.2770.

Woodcock, A.H. 1955: Bursting bubbles and air pollution. Sew. & Ind.Wastes 27(10) :1189-92.

Wozniak, D.H.; Kiwak, C.; Cahoon, C.; and Edgerton, R.H. 1976. Water to airbacterial transfer by bursting bubbles. Jou:t'. Environ. Eng. Viv., Proc.Amer. Soc. Civil Engr. l02(EE3):567-70.

39

Tanimoto, R.M.; Burbank, N.C., Jr.; Young, R.H.F.; and Lau, L.S. 1968.Migration of bacteriophage Tit in percolating water through selected Oahusoils. Tech. Rep. No. 20, Water Resources Research Center, Universith ofHawaii.

Taylor, A.W. 1967. Phosphorus and water pollution. Jour. Soit & Water Cons.22(6) :228-30.

U.S., Congress, Senate. 1972. Federal "(later Pollution Control Act amend­ments of 1972. Public Law 92-500, 92d Cong., S. 2770.

Woodcock, A.H. 1955. Bursting bubbles and air pollution. Sew. &Ind.Wastes 27(10) :1189-92.

Wozniak, D.H.; Kiwak, C.; Cahoon, C.; and Edgerton, R.H. 1976. Water to airbacterial transfer by bursting bubbles. Jour. Environ. Eng. Div., Proc.Amer. Soc. Civil Engr. 102(EE3) :567-70.

Page 46: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …
Page 47: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

41

APPENDICES

CONTENTS

APPENDIX A. KMCAS GOLF COURSE SOIL DESCRIPTIONS.

APPENDIX B. WASTE WATER QUALITY ANALYSIS, KMCAS STP.

APPENDIX C. GROUNDWATER QUALITY ANALYSIS, KMCAS KLIPPERGOLF COURSE _ .

APPENDIX D. NORMALIZED AIR QUALITY DATA FOR VARIOUS INITIALCOLIFORM BACTERIA DENSITIES IN THE SPRINKLEREFFLUENT . . . .. . . . . . . . . . . . . .

43

45

50

52

. APPENDIX E. NORMALIZED AIR QUALITY DATA AT VARIOUS WINDVELOCITIES ; .

FIGURES

. . ". . . .. . 55

D.l.

0.2.•..

0.3.

L1.

L2.

E.3.

Normalized Air Quality Data for Initial Coliform BacteriaConcentration Between 15,000 and 20,000 Colonies/lOO m.Q. ..

I

Normalized Air Quality Data for Initial Coliform BacteriaConcentration of 46,000 Colonies/100 m .Normalized Air Quality Data for Initial Coliform BacteriaConcentration Between 319,000 and 400,000 Colonies/100 m ....Normalized A-jr Quality Data for Wind Velocities Betweeno and 8 Knots . . . . . . . . . . . . . . . . . . . . .Normalized Air Quality Data for Wind Velocities Between9 and 12 Knots .Normalized Air Quality Data for Wind Velocities Between13 and 18 Knots . . . . . . . . . . . . . . . . . . . .

TABLES

52

53

54

55

56

57

A.l. Soil Descriptions of the KMCAS Klipper Golf Course, MokapuPeninsula, Oahu. . . . . . . . . . . . . . . . . . . . . . 43

B.l. Means, Standard Deviations, Medians, Minimums, and Maximumsof~~ater Qual ity Parameters of 24-hr Raw Sewage Composite,8-9 October 1975, Kane'ohe Marine Corps Air Sta. STP. . . . 45

B.2. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Secondary EffluentComposite, 8-9 O~tober 1975, Kane'ohe Marine Corps Air Sta.STP . . . . . . . . . . . . . . . . . . . . . . . . . . . . 45

41

APPENDICES

CONTENTS

APPENDIX A. KMCAS GOLF COURSE SOIL DESCRIPTIONS.

APPENDIX B~ WASTE WATER QUALITY ANALYSIS, KMCAS STP...

APPENDIX C. GROUNDWATER QUALITY ANALYSIS, KMCAS KLIPPERGOLF COURSE _ , .

APPENDIX D. NORMALIZED AIR QUALITY DATA FOR VARIOUS INITIALCOLIFORM BACTERIA DENSITIES IN THE SPRINKLEREFFLUENT . . . .. . . . . . . . . . . . . .

43

45

50

52

. APPENDIX E. NORMALIZED AIR QUALITY DATA AT VARIOUS WINDVELOCITIES ~ .

FIGURES

. . ". . . . . 55

D.l.

0.2....

0.3.

E.l.

E.2.

E.3.

Normalized Air Quality Data for Initial Coliform BacteriaConcentration Between 15,000 and 20,000 Colonies/lOa m~ . . 52Normalized Air Quality Data for Initial Coliform BacteriaConcentration of 46,000 Colonies/lOa m . . . . . . . . . 53Normalized Air Quality Data for Initial Coliform BacteriaConcentration Between 319,000 and 400,000 Colonies/lOa m 54Normalized Air Quality Data for Wind Velocities Betweeno and 8 Knots . . . .. . . . . . . . . . . . . . . . . 55Normalized Air Quality Data for Wind Velocities Between9 and 12 Knots. . . . . . . . . . . . . . . . . . . . . . 56

Normalized Air Quality Data for Wind Velocities Between13 and 18 Knots. . . . . . . . . . . . . . . . . . . . 57

TABLES

A.l. Soil Descriptions of the KMCAS Klipper Golf Course, MokapuPeninsula, Oahu. . . . . . . . . . . . . . . . . . . . . . 43

B.l. Means, Standard Deviations, Medians, Minimums, and Maximumsof l~ater Quality Parameters of 24-hr Raw Sewage Composite,8-9 October 1975, Kane'ohe Marine Corps Air Sta. STP. . . . 45

B.2. Means, Standard Deviations, Medians, Minimums, and Maximums·of Water Quality Parameters of 24-hr Secondary EffluentComposite, 8-9 O~tober 1975, Kane'ohe Marine Corps Air Sta.STP . . . . . . . . . . . . . . . . . . . . . . . . . . . . 45

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42

B.3. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Pond Effluent Composite,8-9 October 1975, Kane10he Marine Corps Air Sta. STP. . . . . 46

B.4. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Raw Sewage Composite,20-21 November 1975, Kane'ohe Marine Corps Air Sta. STP . . 46

B.S. Means, Standard Deviations, Medians, Minimums, and Maximumsof l~ater Quality Parameters of 24-hr Secondary Effl uent Com­posite, 20-21 November 1975, Kane'ohe Marine Corps Air Sta.STP . . . . . . . . . . . . . .. . . . . . . . • . . . . .' . '.' 47

B.6. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hrPondEffluent Composite,20-21 November 1975, Kane'ohe Marine Corps Air Sta. STP . . .. 47

B.7. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Raw Sewage Composite,11-12 February 1975, Kane'ohe Marine Corps Air Sta. STP . . 48

B.8. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Pond Effluent Composite,11-12 February 1975, Kane'ohe Marine Corps Air Sta. STP ... 48

B.9. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Raw Sewage Composite,12-13 July 1976, Kane'oheMarine Corps Air Sta. STP •. , . .. 49

B.10. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Pond Effluent Composite,12-13 July 1976, Kane'ohe Marine Corps Air Sta. STP . . . . 49

(

C.l. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of Groundwater Test Well No.1,KMCAS Golf Course . . . .. . . . . . . . . . . . . . . . . 50

C.2. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of Groundwater Test Well No.2,KMCAS Golf Course . . . . . . . . . . . . . . . . . . . . . 50

C.3. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Qual ity Parameters of Groundwater Test ~~e11 No.3,KMCAS Golf Course . . . . . . . . . . .. . . . . . . . ... 51

C.4. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of Sprinkler Effluent, KMCASGolf Course ~ . . . . . . . . . . . . . . . . . . . . . . . 51

42

B.3. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Pond Effluent Composite,8-9 October 1975, K~ne'ohe Marine Corps Air Sta. STP. . . . 46

8.4. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Raw Sewage Composite,20-21 November 1975, Kane'ohe Marine Corps Air Sta. STP . . 46

B.S. Means, Standard Deviations, Medians, Minimums, and Maximumsof ~~ater Qua I ity Parameters of 24-hr Secondary Effl uent COlll­posite, 20-21 November 1975, Kane'ohe Marine Corps Air Sta.STP . . . . . . . . . . . . . .. . . . . . . . . . . . . . . .. 47

8.6. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Pond Effluent Composite,20-21 November 1975, Kane'ohe Marine Corps Air Sta. STP . . 47

8.7. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Raw Sewage Composite,11-12 February 1975, Kane'ohe Marine Corps Air Sta. STP . . 48

B.8. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Pond Effluent Composite,11-12 February 1975, Kane'ohe Marine Corps Air Sta. STP . . .. 48

8.9. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Raw Sewage Composite,12-13 July 1976, Kane'ohe Marine Corps Air Sta. STP . . . . 49

B.10. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of 24-hr Pond Effluent Composite,12-13 July 1976, Kane'ohe Marine Corps Air Sta. STP . . . . 49

C.l. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of Groundwater Test Well No.1,KMCAS Go1f Course . . . . . . . . . . . . . . . . . . . . . 50

C.2. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of Groundwater Test Well No.2,KMCAS Golf Course. . . . . . . . . . . . . . . . . . . . . 50

C.3. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of Groundwater Test Well No.3,Kl"1CAS Golf Course . . . . . . . . . . . . . . . . . . . . . 51

C.4. Means, Standard Deviations, Medians, Minimums, and Maximumsof Water Quality Parameters of Sprinkler Effluent, KMCASGolf Course. . . . . . . . . . . . . . . . . . . . . . . . 51

Page 49: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

APP

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APPENDIX A. KMCAS GOLF COURSE SOIL DESCRIPTIONS

APPENDIX TABLE A.l. SOIL DESCRIPTIONS OF THE KMCAS KLiPPER GOLF COURSE, MOKAPU PENINSULA,OAHU

Ewa Series l

Location: Test ~/ell No.3 Classification: Mollisols, Torroxic Haplustolls (Low Humic Latosols)Description: This series consists of well-drained soils in basins and on alluvial fans on the island of

Oahu. These soils developed in alluvium derived from basic igneous rock. They are nearlylevel to moderately sloping.

Ewa Si lty Clay Loam, moderately shallow, a to 2% (EmA) and 2 to 6% (EmB) ,slopes. In a representative pro-file, the subsurface layer is dark reddish-brown silty clay loam about 46 cm (18 in.) thick.The subsoil, about 107 em (42 in.) thick, 1s dark reddlsh-brownand dark red silty clay loamwith subangularblocky structure. The substratum 1s coral limestone, sand, and gravelly allu­vium. P~rmeability is moderate, runoff Is slow, and the erosion hazard is slight. The depthto coral limestone is 51 to 127 crrt (20 to 50 in.) deep.

The underlying materials had the following properties: 0 to 152 em (0 to 60 In.), dark reddish-brown siltyclay loam, dark reddish-brown when dry; cloddy, breaking to weak, fine, and very fine granularstructure; hard, friable, sticky and plastic; abundant fine and very fine roots. 152 to 457 em(60 to 180 in.), si lty clay loam, dark red~ fine subangular blocky structure; hard, friable,sticky and plastic; fin~ tubular pores; sand grains.

Jaucas Se ri es

Location: Test Well No.2 Classification: Entisols, Typic Ustipsamments (Regosols)Description: This serieS consists of excessively-drained, calcareous soi Is that occur as narrow strips on

coastal plains, adjacent to the ocean. They developed in wind- and water-deposited sand fromcoral and seashells.

Jaucas Sand, 0 to 15% slopes. In a representative profile, the soil is single grained,pale brown to verypale brown, sandy,and more than 3 m (11 ft) deep. In many places the surface layer is dark,brown as a result of accumulation of organic matter and alluvium. The soil is neutral to mod­erately alkaline throughout the profile. Permeability is rapid, and runoff is very slow toslow. The hazard of water erosion Is 51 ight but wlrid erosion is a severe hazard where vegeta-'tion has been removed. Workability is slightly difficult because the soil is loose and lacksstability for use of equipment. '

The underlying materials had the following properties: 0 to 30 em (0 to 12 in.), pale brown sand, lightyellowish-brown when dry; single-grained, loose, nonsticky and nonplastie;and plentiful roots.30 to 61 em (24 in.), light yellowish-brown sand, very pale brown when dry; single-grained,loose, nonstieky and nonplastie;andfew roots. 61 to 2]4 em (108 in.), very pale brown sand;single-grained; loose, nbnstieky and nonplastic. 2]4 to 335 em (132 In.), very plae brownsand; moist, single-grained; loose, nonstieky and nonplastic. 335 to 351 em (138 in.), verypale brown sand, organic matter, and alluvium; moistgranular clay; fIrm, sticky and plastic.

Page 50: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

APPE

NDIX

TABL

EA

.1-tO

NTI

NU

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Ser

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Cla

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Mo1

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crip

tio

n:

Thi

sse

ries

co

nsi

sts

of

wel

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ils

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nt

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(Mt)

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.j::>

. ..,.APPENDIX TABLE A.1-cONTINUED

Mokuleia SeriesClassification: Mol lisols, Typic Haplustolls (Alluvial)Description: This series consists of well-drained soils along the coast of Oahu~ These soils are formed in

recent alluvium deposited over coral sand. They are shallow and nearly level.Mokuleia Clay Loam (Mt). In a representative profile, the surface layer is very dark grayish-brown clay

loam about 41 cm (16 in.) thick. The next. layer, 86 cm (34 in.) to more than 122 cm (48 in.)thick, is dark brown and 1ight gray, single-grained sand and loamy snad. Permeabi 1ity is mod­erate in the surface layer and rapid in the subsoil. Runoff is very slow, and the erosionhazard is more than sl ight.

Makalapa SeriesClassification: Vertisols, Typic Chromusterts (Dark Magnesium Clays)Description: This series consists of well-drained soils on uplands of the Mokapu Peninsula. These soils

are formed in volcanic tuff. They are gently sloping to moderately steep.Maka1apa Clay, 6 to 12% slopes (MdC). In a representative profile the surface layer is very dark graylsh­

brown clay about 20 cm (8 in.) thick. The next layer, 20 to 91 cm (36 in.) thick, is verydark grayish-brown clay to silty clay loam with subangular blocky structure. It is underlainby light gray to dark grayish-brown, weathered volcanic tuff. The clays are very sticky andvery plastic, and crack widely upon drying .. Permeability is slow; runoff is slow to medium;the erosion hazard is slight to moder~te. Workability is difficult because the clay is verystick and ver lastic; the shrink-s~vell potential is high.

Fill Land FL

IFoote et al. (1972).

Description: This land type occurs mostly near the ocean. It consists of areas filled with materialdredged from the ocean or hauled from nearby areas and general material from other sources.Generally, these materials are dumped and spread over marshes, low-lying areas along thecoastal flats, coral sand, coral limestone, or areas shallow to bedrock.

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APPENDIX B. WASTE WATER QUALITY ANALYSIS, KMCAS STP

45

APPENDIX TABLE B.l. MEANS, STANDARD DEVIATIONS, MEDIANS, t1INlt1UMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR RAW SEWAGE COMPOSITE, 8-9 OCTOBER 1975,KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum

(mg/~) ---------(mg/~)------~----

TDSSS 24 110 ± 71 100 74 264BODs 24 102 ± 38 105 44 204NH3-N 23 12.7 ± 3.7 12.9 5·0 19.4Organic N 24 6.7 ±. 2.3 7.3 2.5 10.6NOz + N03-N 24 0.02 ± 0.02 0.02 0 0.08Total N 23 19.54 ± 5.34 20.97 2:83 29.68Total P 24 7.19 ± 2.76 7.67 2.32 11.47NaKCl- 24 596 ±181 540 370 950SOIf

APPENDIX TABLE B.2. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAX (MUMS OF WATER QUALI TY PARAMETERS OF24-HR SECONDARY EFFLUENT COMPOSITE, 8-9 OCTO-BER 1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. t1edi an Mini- Maxi-Constituent Samples Dev. mum mum

(mg/~) ~----------(mg/~)----------

TDSSS 6 19 ± 2 19 15 21BODs 6 18 ± 3 18 13 21NH 3-N 6 5.5 ± 1.1 5.9 3.6 6.6Organic N 6 2·7 ± 0.5 2.9 1.8 3. 1NOz + N03-N 6 4. 15 ± 0.30 3.99 3.89 4.66Total N 6 12·37 ± 1. 23 12.79 10.06 13.64Total P 6 7.94 ± 0.38 7.94 7.76 8.13NaKCl- 6 472 ±54 470 370 510SOIf

APPENDIX B. WASTE WATER QUALITY ANALYSIS, KMCAS STP

4S

APPENDIX TABLE B. l. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR RAW SEWAGE COMPOSITE, 8-9 OCTOBER 1975,KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples . Dev. mum mum

(mg/Q,) -----~---{mg/Q,)------~----

TDSSS 24 110 ± 71 100 74 264BODs 24 102 ± 38 105 44 204NHrN 23 12.7 ± 3.7 12.9 5·0 19.4Organ ic N 24 6.7 ± 2.3 7.3 2.5 10.6N02 + N03-N 24 0.02 ± 0.02 0.02 0 0.08Total N 23 19.54 ± 5.34 20.97 2.83 29.68Total P 24 . 7.19 ± 2.76 7.67 2.32 11.47NaK --Cl- 24 596 ±181 540 370 950SOlf

APPENDIX TABLE B.2. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR SECONDARY EFFLUENT COMPOSITE, 8-9 OCTO-BER 1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std.t~ed ian Mini- Maxi-

Constituent Samples Dev. mum mum(mg/Q,) --~--------(mg/Q,)----------

TDSSS 6 19 ,± 2 19 15 21BODs 6 18 ± 3 18 13 21NH 3-N 6 5.5 ± 1. 1 5.9 3.6 6.6Organic N 6 2·7 ± 0.5 2.9 1.8 3.1N02 + N03-N 6 4. 15 ± 0.30 3.99 3.851 4.66Total N 6 12·37 ± 1. 23 12.79 10.06 13.64Total P 6 7.94 ± 0.38 7.94 7.76 8.13NaKCl- 6 472 ±S4 470 370 510S04

Page 52: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

46

APPENDIX TABLE B.3. MEANS, STANDARD DEVIATIONS, MEDIANS,MINIMUMS,AND MAXI MUMS OF WATER QUALI TV PARAMETERS OF24-HR PQND EFFLUENT COMPOSITE, 8-9 OCTOBER1975, KANE 'OHE MARINE CORPS AIR STA. STP .

± 3 10 3 13± 3· 13 3 17± 0.5 6.0 5.0 6.9± 1.5 2.9 2.2 6.9± 0.30 1. 72 0.88 2.07± 0.61 10.47 9·37 11.95± 0.36 8.08 7.34 9.01

±30 480 420 510

Std. Min i-Maxi -Mean MedianDev. mum mum---~~------(mg/,Q,)---------

No. ofConstituent Samples

(mg/,Q,)

TDSSS 24 8

. BODs 24 12NH3-N 18 5.9Organic N 18 3.6N02 + N03-N 24 1.68Total N 24 10.51Tota 1 P 24 8. 16NaKCl- 24 468S04

APPENDIX TABLE 8.4. STANDARD DEVIATIONS, MEDIANS, MINIMUMS,I

MEANS, ,

AND MAXIMUMS OF WATER QUA~ITY PARAMETERS OF I24-HR RAW SEWAGE COMPOSITE, 20-21 NOVEMBER I

I

1975, KANE'OHE MARINE CORPS AIRSTA. STPI

No. of Mean Std. Median Mini- Maxi-Constituent . Samp 1es Dev. mum mum

(mg/,Q,) ---~~----~-(mg/,Q,)----------

TDS55 24 114 ± 92 104 20 332BOD 24 123 ± 58 124 40 261NH3-N 24 15.2 ± 2.9 14.8 9.2 21.0Organic N 24 9.3 ± 4.2 8.6 2.8 20.4N02 + N03- N 24 0.02 ± 0.01 0.02 0.01 0.05Tota 1 N 24 24.54 ± 6.86 .23.32 12.01 41.43Total P 24 8.00 ± 2.77· 8.83· 3.00· 14.75NaKCl- 24 444 ±156 420 240 840S04 --

46

APPENDIX TABLE B.3. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR PQND EFFLUENT COMPOSITE, 8-9 OCTOBER1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- t'1axi -Cons t i tuen t Samples Dev. mum mum

(mg/9.,) ----~------(mg/9.,)---------

TDS55 24 8 ± 3 10 3 13BOD5 24 12 ± 3 13 3 17NH3-N 18 5.9 ± 0.5 6.0 5.0 6.9Organic N 18 3.6 ± 1.5 2.9 2.2 6.9N02 + N0 3-N 24 1. 68 ± 0.30 1. 72 0.88 2.07Total N 24 10.51 ± 0.61 10.47 9·37 11.95Tota 1 P 24 8. 16 ± 0.36 8.08 7.34 9.01NaKCl- 24 468 ±30 480 420 510SOl.;

APPENDIX TABLE 8.4. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR RAW SEWAGE COMPOSITE, 20-21 NOVEMBER1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum

(mg/9.,) ---------~-(mg/9.,)----------

TD555 24 114 ± 92 104 20 332BOD 24 123 ± 58 124 40 261NH3-N 24 15.2 ± 2.9 14.8 9.2 21.0Organ i c N 24 9.3 ± 4.2 8.6 2.8 20.4N02 + N0 3-N 24 0.02 ± 0.01 0.02 0.01 0.05Total N 24 24.54 ± 6.86 .23.32 12.01 41.43Total P 24 8.00 ± 2.77 8.83 3.00 14.75NaKCl- 24 444 ±156 420 240 840SOl.;

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47

APPENDIX TABLE B.5. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR SECONDA~Y EFFLUENT COMPOS ITE, 20-21 NOV-EMBER 1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum

(mg/R.) -------~---(mg/R.)---------~

TDS _.-SS 6 25 ± 7 26 17 36BODsNH 3-N 6 8.3 ± 0.7 8.5 7.0 9.2Organic N 6 3.2 ± 0.5 3.3 2.4 3.8N0 2 + N0 3-N 6 1.46 ± 0.18 1. 38 1. 31 1. 78Total N 6 12.99 ± 0.73 13. 16 11.61 13.66Total P 6 7.41 ± 0.49 7.62 6.73 7.93NaKCl- 6 482 ±35 480 440 520S04

APPENDIX TABLE B.6. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS Of WATER QUALITY PARAMETERS OF24-HR PQND EFFLUENT COMPOSITE, 20-21 NOVEMaER1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum

(mg/R.) -----------(mg/R.)----------

TDSSS . 12 10 ±2 9 8 15BODsNH 3-N 12 8.3 ±0.3 8.3 7.8 8.7Organic N 12 2.4 ±0.2 2.4 2.1 2.7N02 + N03-N 12 0.50 ±0.01 0.50 0.40 0.59Total N 12 11. 17 ±0.22 11. 21 10.84 11; 54Total P 12 7.49 ±o.45 7.50 7.10 8.00NaKCl- 12 491 ±9 490 480 500SO 4

47

APPENDIX TABLE B.5. MEANS, STANDARD DEVIATIONS,MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR SECONDARY EFFLUENT COMPOSITE, 20-21 NOV-EMBER 1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples . Dev. mum mum

(mg/~) -----------(mg/~)----------

TDSSS 6 25 ± 7 26 17 36BODsNHa-N 6 8.3 ± 0.7 8.5 7·0 9.2Organic N .6 3.2 ± 0.5 3.3 2.4 3.8NO z + NOa-N 6 1. 46 ± 0.18 1. 38 1. 31 1. 78Total N 6 12.99 ± 0·73 13.16 1J .61 13.66Total P 6 7.41 ± 0.49 7.62 6.73 7.93NaKCl- 6 482 ±35 480 440 520S04

APPENDIX TABLE B.6. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR PQND EFFLUENT COMPOSITE, 20-21 NOVEHeER1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum

(mg/~) --------~--(mg/~)--------~-

TDSSS 12 10 ±2 9 8 15BODsNH3-N 12 8.3 ±0.3 8.3 7.8 8.7Organic N 12 2.4 ±0.2 2.4 2. 1 2.7NOz + NOa-N 12 0.50 ±O.Ol 0.50 0.40 0·59Total N 12 11. 17 ±0.22 11. 21 10.84 11054Total P 12 7.49 ±o.45 7.50 7.10 8.00NaKCl- 12 491 ±9 490 480 500S°lt

Page 54: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

48

APPENDIX TABLE B.7.

No. ofConstituent Samples

MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR RAW SEWAGE COMPOSITE, 11-12 FEBRUARY1975, KANE'OHE MARINE CORPS AIR STA. STP

Std. Md' Mini- Maxi-Mean I e I anDev. mum mum(mg/.Q,) ----------- (mg/.Q,)----------

TDSSSBODsNH 3-NOrganic NN02 + N03-NTotal NTotal PNaKCl-S04

24242424242424

24

11511313.88.60.03

22.4].64

485

± 68± 42± 5.7±3.4± 0.02± 8.26± 2.05

±143

9711912.98.40.02

21.967.85

460

30423.93.90.018.924.19

300

34118926.320.20.03

42.0311. 07

900

APPENDIX TABLE B.8. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR POND EFFLUENT COMPOSITE, 11~12 FEBRUARY1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median ~1 i ni- Maxi-Constituent Samples Dev. mum mum

(mg/.Q,) -----------(mg/t)----------

TDS --SS 5 7 ± 1 7 6 8BODs 5 11 ± 1 11 9 13 .NH 3-N 5 8.4 ± 0.2 8.5 8. 1 8.7Organic N 5 2.2 ± 0.2 2. 1 2. 1 2.5N0 2 + N0 3-N 5 1.02 ± 1.5 1.04 0.84 1. 23Total N 5 11. 66 ± 0.36 11.66 11. 14 12.03Tota 1 P 5 7.36 ± 0.62 7.00 6.77 8.05NaK --CI 5 490 ±10 490 480 500S04

48

APPENDIX TABLE B.7. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAX f MUMS OF WATER QUAL ITY PARAt1ETERS OF

. 24-HR RA....' SEWAGE COMPOSITE, 11-12 FEBRUARY1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- t1ax i -Constituent Samples Dev. mum mum

(mgj£) -----------(mgj£)----------

TDSSS 24 115 ± 68 97 30 341BODs 24 113 ± 42 119 42 189NH3-N 24 13.8 ± 5.7 12.9 3.9 26.3Organic N 24 8.6 ± 3.4 8.4 3·9 20.2N02 + N03-N 24 0.03 ± 0.02 0.02 0.01 0.03Total N 24 22.4 ± 8.26 21.96 8.92 42.03Total P 24 7.64 ± 2.05 7.85 4. 19 J 1.07NaKCl- 24 485 ±143 460 300 900S04

APPENDIX TABLE B.8. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR POND EFFLUENT COMPOSITE, 11-12 FEBRUARY1975, KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. t1ed ian ~1i ni - Maxi-Constituent Samples Dev. mum mum

(mgj£) -----------(mgj£)----------

TDSSS 5 7 ± 1 7 6 8BODs 5 11 ± 1 11 9 13 .NH 3-N 5 8.4 ± 0.2 8.5 8. 1 8.7Organic N 5 2.2 ± 0.2 2. 1 2. 1 2.5N0 2 + N0 3 -N 5 1. 02 ± 1. 5 1.04 0.84 1. 23Total N 5 11 .66 ± 0.36 11.66 11. 14 12.03Total P 5 7.36 ± 0.62 7.00 6.77 8.05NaKCl 5 490 ±JO 490 480 500SO 4

Page 55: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

49

APPENDIX TABLE B.9. MEANS, STANDARD DEVIATIONS,MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR RAW SEWAGE COMPOS ITE, 12-13 JULY 1976,KANEtOHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini"; Maxi-Constituent Samples Dev. mum mum(mg/.Q,) . -----------(mgj.Q,)------~~---

TDS 24 1227 ±366 1124 656 2212SS 24 106 ±65 106 31 326BODs 24 127 ± 55 132 44 260NH 3-N 24 13.6 ± 4.2 13.4 4.5 23.5Organic N 24 7.4 ± 2.5 8.4 2.8 10.6N02 + N03-N 24 0.01 ± 0.01 0.01 0.00 0.05Total N 24 21.06 ± 5.95 21.56 7.31 32.52Total P 24 6. 11 ± 2.57 6.62 1.54 9.85Na 24 351 ±1l5 316 223 643K 24 25 ± 4 22 22 33Cl-. 24 478 ±155 326 313 851504 24 113 ± 25 106 81 192

APPENDIX TABLE B. 10. MEANS, STANDARD DEV IAT IONS, MED IANS, MINI t1UMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF2~-HR POND EFFLUENT COMPOSITE, 12-13 JULY 1976,KANEtOHE MARINE CORPS AIR STA. STP

. No. ofMean Std . Median Mini- Maxi-Constituent Samples Dev. mum mum(mgj.Q,) . ~----------(mgj.Q,)-------~---

TDS 24 1103 ±30 1109 996 . 114755 24 12 ± 2 13 8 14BODs 24 8 ± 4 9 3 15NH 3-N 16 8.6 ± 0.5 8.6 8.0 9·3Organic N 16 2.8 ± 0.5 2.6 . 2.5 4.6N0 2 + N0 3-N 24 0.85 ± O. 11 0.83 0.67 1. 10Total N 16 12.21 ± 0.61 12.22 11.25 13.65Total P 12 8.09· ± 0.59 7.99 7.08 9.31NaK 12 20 ± 0.6 20 19 21Cl- 24 450 ± 7 450 440 46050 4 12 97 ± 7 96 92 120

49

APPENDIX TABLE B.9. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF24-HR RAW SEWAGE COMPOSITE, 12-13 JULY 1976,KANEJOHE MARINE CORPS AIR STA. STP

No. of Mean Std. MedianMini~ Maxi-

Constituent Samples Dev. mum mum(mg/Q,) -----------(mg/Q,)--~---~~---

TDS . 24 1227 ±366 1124 656 2212SS 24 106 ± 65 106 31 326BODs 24 127 ± 55 132 44 260NH 3-N 24 13.6 ± 4.2 13.4 4.5 23.5Organic N 24 7.4 ± 2.5 8.4 2.8 10.6N02 + N03-N 24 0.01 ± 0.01 0.01 0.00 0.05Total N 24 21.06 ± 5.95 21.56 7.31 32.52

. Tota 1 P. 24 6.11 ± ·2.57 6.62 1.54 9.85Na 24 . 351 ±115 316 223 643K 24 25 ± 4 22 22 . 33Cl- 24 478 ±155 326 313 851S04 24 113 ± 25 106 81 192

APPEND(X TABLE B.10. MEANS, STANDARD DEV IAT IONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OF2~-HR POND EFFLUtNT COMpOSITE, 12-13 JULY 1976,KANE'OHE MARINE CORPS AIR STA. STP

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum

(mg/Q,) . -----------(mg/Q,)-------~---

TOS 24 n03 ±30 1109 996 1147SS 24 12 ± 2 13 8 14BODs 24 8 ± 4 9 3 15NH 3-N 16 8.6 ± 0.5 8.6 8.0 9·3Organic N 16 2.8 ± O.S 2.6 2.5 4.6

. N0 2 + N0 3-N 24 0.85 ± O. 11 0.83 . 0.67 1.10Total N 16 12.21 ± 0.61 12.22 11.25 13.65Total P 12 8.09 ± 0.59 7.99 7.08 9.31NaK 12 20 ± 0.6 20 19 21Cl- 24 450 ± 7 450 440 460S04 12 97 ± 7 96 92 120

Page 56: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

50

APPENDIX C. GROUNDWATER QUALITY ANALYSIS, ~~CAS KLIPPER GOLF COURSE

APPENDIX TABLE C.l. MEANS, STANDARD DEVIATIONS, MEDIANS,MINIMUMS~

AND MAXI MUMS OF WATER QUALITY PARAMETERS OFGROUNDWATER TEST WELL NO.1, KMCAS GOLF COURSE

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum . mum

(mg/9-) -------~--(mg/9-)----------~-

. NH 3-N 16 O. 10 ± 0.04 0.10 0.06 0.17Organic N 16 0.43 ± 0.21 0.39 0.22 1. 12N02 + NO 3-N 18 0.26 ± 0.19 0.22 0.03 0.80Total N 14 0.76 ± 0.22 0.]0 0.41 1.34Total P 18 0.66 ±. 0.08 0.69 0.44 0.75Na 18 2041 ±186 1934 1747 2371K 18 90 ± 5 87 87 104Cl- 7 2087 ±196 2153 1761 2250Fecal Co 1i- (#/100 m9-) --------(#/100 m9-)---~------

form 18 0 0 0 0 0

APPENDIX TABLE C.2. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OFGROUNDWATER TEST WELL NO. 2, KMCAS GOLF COURSE

(mg/9-)Cons t i tuen t

No. ofSamples

Mean Std. Median Mini- Maxi-Dev. mum mum

-----~----(mg/9-)------------

NH3-NOrganic NN0 2 + N0 3-NTotal NTotal PNaKCl-Fecal Coli­form

161817141817187

18

0.010.421.471. 75O. 15

30622

447(#/100 m9-)

o

± 0.01± O. 19± 0·52± 0·30± 0.10±22

o±52

o

0.01 0.01 0.050.39 0.22 0.781.43 0.94 3.241. 67 l .36 2. 30O. 12 0.06 0.45

311.273 36022 22 22

489 391 489--------(#/100 m9-)----------00 0

50

APPENDIX C. GROUNDWATER QUALITY ANALYSIS, ~~CAS KLIPPER GOLF COURSE

APPENDIX TABLE C.l. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS J

AND MAX IMUMS OF WATER QUALITY PARAMETERS OFGROUNDWATER TE~T WELL NO.1, KMCAS GOLF COURSE

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum

(mglQ,) ------w~--(mg/Q,)---~--------

NH3-N 16 0.10 ± ·0.04 0.10 0.06 o. 17Organic N 16 0.43 ± 0.21 0.39 0.22 l. 12NOz + NO 3-N 18 0.26 ± 0.19 . 0.22 0.03 0.80..

Total N 14 0.76 ± 0.22 0.]0 0.41 1.34Total P 18 0.66 ± 0.08 0.69 0.44 0.75Na 18 2041 ±186· 1934 1747 . 2371K 18 90 ± 5 87 87 104Cl- 7 2087 ±196 2153 1761 ··2250Fecal Co 1i- (#/100 mQ,) --~-----(#/l00 mQ,)---~~-----

form 18 0 0 0 0 0

APPENDIX TABLE C.2. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAXIMUMS OF WATER QUALITY PARAMETERS OFGROUNDWATER TEST WELL NO. 2, KMCA~ GOLF COURS~

No. of Mean Std. Median Mini- Maxi-Cons t i tuen t Samples Dev. mum mum

(mglQ,) -----~----(mg/Q,)------------

NH3-N 16 0.01 ± 0.01 0.01 0.01 0.05Organ ic N 18 0.42 ± 0.19 0.39 0.22 0.78NO z + N0 3-N 17 1.47 ± 0.52 1.43 0.94 3.24Total N 14 1. 75 ± 0.30 1. 67 1. 36 2.30Total P 18 0.15 ± 0.10 O. 12 0.06 0.45Na 17 306 ±22 31 1 273 360K 18 . 22 0 22 22 22el- 7 447 ±52 489 391 489Feca 1 Col i- (#/100 rnQ,) --------(#/100 mQ,)----------form 18 0 0 0 0 0

Page 57: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

51

APPENDIX TABLE C.3. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS, ..AND MAXIMUMS OF WATER QUALITY PARAMETERS OF .GROUNDWATER TEST WELL NO.3, KMCAS GOLF COURSE

No. of Mean Std. Median Mini- Maxi-Constituent Samples Dev. mum mum(mgl,Q,) ----------(mg/,Q,)----~--~----

NH3-N 16 0.30 ± O. 10 0.31 0.08 0.49Organic N 18 0.62 ± 0.22 0.53 0.34 1. 01NOz + N0 3-N 18 O. 16 ± 0.18 0.09 0.01 0.62Total N 16 1.04 ± 0.42 0.84 0.47 1.79Total P 18 O. 11 ± 0.03 0.10 0.06 O. 16Na 17 2218 ± 186 2226 1914 2454K 17 82 ± 6 . 79 79 104Cl- 7 2097 ± 95 2055 1957 ·2250Fecal Co 1i- (#/100 m,Q,) --------- (#/100 mQ,) ----------form 18 a 0 0 a a

APPENDIX TABLE C.4. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAX I MUMS OF WATER QUALI TY PARAMETERS OFSPRINKLER EFFLUENT, KMCAS GOLF COURSE

420(#/100 m,Q,)

111

10.9 9.6 13.81. 79 1. 40 2.240.b1 0.01 . 0.13

12.77 11.63 J5.718.7 7.3 10.8

230 218 24022 22 22

328 323 342

M Std. Md' Mini- Maxi-ean elanDev. mum mum----------(mgl,Q,)~-----------

(mgl,Q,)

10.9 ± 1.11.84 ± 0.210.03 ± 0.04

12.75 ± 1. 128.9 ± 1.2

230 ± 1022 a

329 ± 12(#/100 m,Q,)

160 ±1508

121212121012126

No. ofSamplesConstituent

NH 3-NOrgani c NNOz + N0 3-NTotal NTotal PNaKCl-Fecal Col i­form

1. ~

51

APPENDIX TABLE C.3. ~EANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS, .AND MAXIMUMS OF WATER QUALITY PARAMETERS OF .GROUNDWATER TEST WELL NO.3, KMCAS GOLF COURSE

ConstituentNo. ofSamples Mean

(mg/i)

Std. Mini- Maxi-MedianDev. mum mum---------;.,(mg/i)------------

NH3-NOrganic NN02 + N0 3 -NTotal NTotal PNaKCl-Fecal Col i­form

1618181618I]177·

18

0.300.62O. 161.04o. 11

221882

2097(#/100 mi)

a

± 0.10± 0.22± 0.18± 0.42± 0.03±186± 6± 95

o

0.31 0.08 0.490.53 0.34 1.010.09 0.01 0.620.84 . 0.47 1.790.10 0.06 0.16

2226 1914 245479 79 104

2055 1957 2250--------- (#/100 mQ.) ----------000

APPENDIX TABLE c.4. MEANS, STANDARD DEVIATIONS, MEDIANS, MINIMUMS,AND MAX IMUMS OF WATER QUALI TY PARAMETERS OFSPRINKLER EFFLUENT, KMCAS GOLF COURSE

420(#/100 mi)

11 1

10.9 9.6 13.81.79 1.40 2.240.01 0.01 0.13

12.77 11.63 15.718.7 7.3 10.8

230 218 24022 22 22

328 323 342

M Std. M d· Mini- Maxi-.ean elanDev. mum mum----------(mglQ,)------------(mg/i)

10.9 ± 1.11. 84 ± 0.210.03 ± 0.04

12.75 ± 1. 128.9 ± 1.2

230 ± 1022 0

329 ± 12(#/l00 mi)

160 ±1508

121212121012126

No. ofSamplesConstituent

NH 3-NOrganic NN0 2 + N0 3 -NTotal NTotal PNaKCl-Fecal Col i­form

Page 58: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

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Page 63: AN INVESTIGATION INTO ENVIRONMENTAL EFFECTS OF REUSE …

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