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An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance Robert J. Cavagnaro and Dr. Brian Polagye Northwest National Marine Renewable Energy Center University of Washington APS DFD Meeting Pittsburgh, November 24, 2013

An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

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An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance. Robert J. Cavagnaro and Dr. Brian Polagye Northwest National Marine Renewable Energy Center University of Washington. APS DFD Meeting Pittsburgh, November 24, 2013. Motivation. - PowerPoint PPT Presentation

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Page 1: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

An Investigation into Blockage Corrections for Cross-Flow

Hydrokinetic Turbine Performance

Robert J. Cavagnaro and Dr. Brian PolagyeNorthwest National Marine Renewable Energy Center

University of Washington

APS DFD MeetingPittsburgh, November 24, 2013

Page 2: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Motivation Understand hydrodynamics of a full-scale vertical-axis

cross-flow turbine by testing at lab scale Explain variable turbine performance at different testing

facilities

Lab-scale – high variability of performance with velocity and faclity

Field-scale – limited variability of performance with velocity

Page 3: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Micropower Rotor Parameters High-Solidity, Helical Cross-flow

turbine N: Number of blades (4) H/D: Aspect Ratio (1.4) φ: Blade helix angle (60o) σ: Turbine solidity (0.3) Lab scale

H = 23.4 cm, D = 17.2 cm Field Scale

H = 101.3 cm, D = 72.4 cm

DNc

Page 4: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Performance Characterization Experiments

Niblick, A.L., 2012, “Experimental and analytical study of helical cross-flow turbines for a tidal micropower generation system,” Masters thesis, University of Washington, Seattle, WA.

Torque control Torque measurement Angular position

measurement Inflow velocity

measurement Upstream ADV

Thrust measurement

Page 5: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Experimental Facilities

8.04.0

19.015.0

Flow speed (m/s)

Blockage Ratio

35.02.0 FrFroude number

%4U

I UTurbulence Intensity

UW Aero Flume

1.14.0

09.006.0

Flow Speed (m/s)

Blockage Ratio

4.02.0 FrFroude number

%10U

I UTurbulence Intensity

Bamfield Flume

Reynolds Number Reynolds Number43 1010 cRe

43 1010 cRe

Cross Section (m2)80.0

Cross Section (m2)35.0

UcRec

Channel

RigTurbine

AAA )(

Page 6: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Blockage Corrections

Corrections rely on various experimental parameters

TU 2U

3U

WACA

TAT

h

1U

3

F

TPP UUCC

TF

F

TTF UU

3

F

T

P

PTF CC

UU

Page 7: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Blockage Corrections: Glauert (1933)

Becomes unstable for CT ≤ -1

TU 2U

3U

WACA

TAT

h

1U

T

TTF C

CUU14

1

Page 8: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Blockage Corrections: Maskell (1965)

Relies on knowledge of wake expansion or empirical constant

TU 2U

3U

WACA

TAT

h

1U

2

1

1

AAUUW

TF

Page 9: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Blockage Corrections: Pope & Harper (1966)

TU 2U

3U

WACA

TAT

h

1U44

1 C

Tt A

A

“… for some unusual shape that needs to be tested in a tunnel, the authors suggest”

)1( tTF UU

Page 10: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Blockage Corrections: Mikkelsen &Sørensen (2002)

TU 2U

3U

WACA

TAT

h

1U

Extension of Glauert’s derivation

uCuUU T

TF 41

12)23()1( 2

u

T

W

AA

Page 11: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Blockage Corrections: Bahaj et al. (2007)

TU 2U

3U

WACA

TAT

h

1U

Iterative solution of system of equations, incrementing U3/U2

Page 12: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Blockage Corrections: Werle (2010)

TU 2U

3U

WACA

TAT

h

1U

Approximate solution

2max, )1(27/16

PC

02

0 )()1( PP CC

Also reached by Garrett & Cummins, 2007

Page 13: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Case 1: Lab to Field ComparisonSame flow speed (1 m/s), different blockage

Lab0 09.0

LabcFieldc ReRe ,, 4

Field

No thrust measurements for lab test case

Case 1 RSSEUncorrected Werle Pope & Harprer

0.034 0.074 0.021

Page 14: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Case 2: Performance at Varying SpeedSame blockage ratio and facility 15.0

Case 2 Total RSSE Uncorrected Werle Pope & Harper Bahaj

0.983 0.717 0.883 0.938

Pope & Harper

Bahaj

Werle

Indicates strong dependence on Rec at low velocity

Page 15: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Case 3: Performance with Varying BlockageSame flow speed (0.7 m/s) at different facilities

Case 3 Total RSSE Uncorrected Werle Pope & Harper Bahaj

0.4618 0.2157 0.3582 0.3265

Pope & Harper

Bahaj

Werle

Page 16: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Conclusions Determining full-scale, unconfined hydrodynamics

through use of a model may be challenging All evaluated corrections reduced scatter of lab scale

performance data Thrust measurements may not be needed to apply a

suitable blockage correction

Caution is needed when applying blockage corrections Especially for cross-flow geometry

No corrections account for full physics of problem

Page 17: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

AcknowledgementsThis material is based upon work supported by the Department of Energy under Award

Number DE-FG36-08GO18179.

Adam Niblick developed the initial laboratory flume data.

Funding for field-scale turbine fabrication and testing provided by the University of Washington Royalty Research Fund.

Fellowship support for Adam Niblick and Robert Cavagnaro was provided by Dr. Roy Martin.

Two senior-level undergraduate Capstone Design teams fabricated the turbine blades and test rig (and a third is developing a prototype

generator).

Fiona Spencer at UW AA Department and Dr. Eric Clelland at Bamfield Marine Sciences Centre for support and use of their flumes

Page 18: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Re Dependence

Lift to drag ratio for static airfoil NACA 0018 at 25˚ angle of attack

Effect of blockage raises local Reynolds number by increasing flow speed through turbine

Effect less dramatic at higher Re

Page 19: An Investigation into Blockage Corrections for Cross-Flow Hydrokinetic Turbine Performance

Bahaj Velocity Correction (2007)

Bahaj, a. S., Molland, a. F., Chaplin, J. R., & Batten, W. M. J. (2007). Power and thrust measurements of marine current turbines under various hydrodynamic flow conditions in a cavitation tunnel and a towing tank. Renewable Energy, 32(3), 407–426. doi:10.1016/j.renene.2006.01.012

Linear Momentum Theory, Actuator Disk Model, thrust and rpm same in flume and free-stream

Solved iteratively by incrementing ratio of bypass flow velocity to wake velocity (U3/U2)

Free-stream performance and λ derived from velocity correction

Where U1 is the water speed through the disk

Depends on inflow velocity, blockage ratio, and thrust

4/)/(/2

1

1

TT

T

F

T

CUUUU

UU

)1)/(()1)/((11

23

223

2

1

UU

UUUU

1

2

3

2

1

2

3

2 UU

UU

UU

UUT

1)/(

1

223

2

UUCU

UT

T