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1
SHEET METAL PART QUALITY IMPROVEMENT THROUGH DIE
OPTIMIZATION USING AUTOFORM
AIRIC2015
2
OBJECTIVES:
Improvement of simulation accuracy and standardizing of sheet metal forming simulation
Phase transition of die quality improvement from final design to simulation and early CAD surface design
Decreasing of part development time Decreasing of part total cost
3Causes of project
Need in improvement of AUTOFORM predictions and results
Time and cost waste during manufacturing and sheet metal part development
Poor dimensional accuracy in past projects
4
1. Past method of simulation in AIRIC2. Important effective parameters3. Numerical and simulation investigations4. Experimental and real results 5. Results verifications
1. Optimization methodology2. Optimization of die surface based on successful try-out3. Optimization of die surface based on successful high production
rate
First part
Second part
5
Current method of simulation in AIRIC
There is no difference in simulation setup considering type of operation and die size
First part
6
Effective ParametersParameter G1 G2 G3 G4 G5
Error tolerance 0.1 0.1 0.1 0.05 0.05Max side length 30 30 20 10 10
Global sharp & fillet edge 1 1 1 1 1Global radius 3 3 3 3 3Max radius D D D D D
Max element angle 20 20 20 20 20Max radius penetration 0.16 0.16 0.16 0.16 0.16
Initial element size 2*R min 2*R min 2*R min 2*R min 2*R minInitial number of element
Max refinement level 7 7 6 5 5Max displacement 0.22 0.22 0.22 0.16 0.16
Refinement extension D D D 2.5 2.5Tangential refinement ON ON ON ON ONBoundary penetration 0.11 0.11 0.11 0.11 0.11
Stiffness value <10 30 50 100 >100Transient softening D D D D D
Stagnation ratio D D D D DYoung reduction factor D D D D DYoung reduction rate D D D D D
Number of end time step s 6 4 4 4 4End time step 0.2 0.4 0.4 0.4 0.4
Drawbead plastification ON ON ON ON ONBinder wrap steps
Crack limit D D D D DTool opening ON ON ON ON ON
Tool penetration to post D D D D D
D: dependent
7
Criteria of parameters categorizing
Type of operation Thickness of sheet metal Part complexity
HOLDER BRKT – G5REINF-ANCHORAGE LWR– G3
WHEEL HOUSE-G3
Standard simulation is the current method of simulationModified simulation is simulation based on parameters and values were listed in page 6
8
REINF-ANCHORAGE LWR
9
Verification of simulation results
10
FEM correlation OF wheel house
Experimental data:
Standard setting( 3.848mm)
Fine Setting(3.475mm)
User defined setting(2.734 mm)
×
11STROCKE AT ONCET OF FAILURE (SOF)
SOF: 53 mmMesh size: 4mm
SOF: 54.8 mmStandard setting of Autoform
MAT: SAPH 440Thickness: 2mmTonnage: 65 TN
SOF: 52 mmMesh size: 3mm
SOF:55.764 mmMesh size: 6mm
SIMPLE CUP DRAWING COMPARISON IN ONCET OF FAILURE USING AUTOFORM AND ABAQUS PREDICTIONS
SOF: 40 mmMesh size : 3 mm
12
Load - displacement
0 10 20 30 40 50 60 70 80 900
10000
20000
30000
40000
50000
60000
70000
AUTOFORM-ROUGH.AUTOFORM-FINEABAQUS-MESH3AUTOFORM-MESH4AUTOFORM-MESH3
13
COMPARISON OF THICKNESS DISTRIBUTION BETWEEN ABAQUS AND AUTOFORM MODIFIED
14
Sample done projects
1. Feasibility phase
2. Die surface design
3. Manufactured die
15
REINF RR HANGER BRKT, LH
DRAWBEADUNKNOWN
Drawbead design and optimization
Effect of drawbead design on failure prevention
Existence of failure on part
Feasibility phase
16
FR DOOR OTR RR VIEW MIRROR MTG PLATE UPR, LH
Existence of failure on part
Subjected fillet design and optimization
Feasibility phase
17
C-PILLAR UPRDie surface design
18
Extreme failure all around drawn part
Die surface design
19
Defect source
Absence of material flow
Lowest price solution
Drawbead design and optimization
Presence of flow and successful drawing
Die surface design
20
COMPARISON OF FLOW BEFORE AND AFTER OPTIMIZATION
Die surface design
21
Die surface design
Improvement part quality
Three different area optimization
Reaching minimum springback amount of 0.75 mm
22
BUMPER CENTERDie surface design
23
SPRING BACKDie surface design
24
Problem on part: severe failure & wrinkle on part
Solution: drawbead optimization based on lowest cost in order To eliminate failure and minimized springback
WHEEL HOUSE,RR Manufactured die
25
unknown38%
B12%B2
4%
B39%
B47%B5
4%
B67%
B73%
B82%
B92%
B103%
D14%
D23% D3
7%
D52%
D63%
D72%
formability objecftive function
B1 B2 B3 B4 B5 B6 B7 B8 B9 B10 D1 D2 D3 D4 D5 D6 D70
1
2
3
4
5
6
7
8
9
10
Manufactured die
Here there are parameters which affect formability of part
Above parameters are sections of drawbead
B-PILLAR-INR-EXTENSION Manufactured die
Manufactured die
Existence of severe failure on part
Manufactured die
Optimized areas Successful product
29
Distance blocks thicknessCushion pin variable Blank locators (Blank position deviation)
Optimization of die surface based on successful high production rate
30
SPRING BACK DURING TRY-OUT
Cpk = 1Cpk = 1.33Cpk = 0.66
SPRING BACK DURING PRODUCTION
UNKNOWN21%
X-B72%
Y-B5%
X-D1%
Y-D2%
31
Thank you for your attention